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Well ID: 34-009-21438 | Loading map...
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Country: United States | |
State: Ohio | |
County: Athens | |
Municipality: Bern Township | |
Operator Name: AM-TEK OIL INC | |
Well Pad ID: | |
Farm/Lease Name: WHITE THOS J | |
License Status: Producing | |
License Date: 1962-12-14 | |
Spud Date: 1963-01-11 | |
Spud Drilling Contractor: | |
Final Drill Date: 1963-01-19 | |
Well Total Depth: 1582.00 ft | |
Configuration: Vertical | |
Latitude: 39.380000 | |
Longitude: -81.940000 |
For data sources see[1]
Well Status | Well Status Date | Comment |
---|---|---|
Original Spud | 1963-01-11 | GL=718.4 |
Completed | 1963-01-19 | GL=718.4 |
Reached Total Depth | 1963-01-19 | GL=718.4 |
CO | 1991-06-20 | 3969 KAPLAN INTERESTS INC |
Change of Owner | 2004-07-08 | Operator changed from 3969, KAPLAN INTERESTS INC to 7671, KEITO GAS INC |
Change of Owner | 2016-11-03 | Operator changed from 7671, KEITO GAS INC to 9651, AM-TEK OIL INC |
Record Last Modified | 2016-11-03 | GL=718.4 |
For data sources see[2]
Stimulation Date | Chemical Agent | Chemical Agent Concentration (%) | Fracking Fluid Volume | Mass of Proppant Used (lb) | Fracking Company | Comments |
---|---|---|---|---|---|---|
H2O | 0 | 900 Bbl | 0 | RP. 8 HRS. |
For data sources see[3]
Period | Operator Name | Gas Quantity (mcf) | Oil Quantity (bbl) | Production Days |
---|---|---|---|---|
1987 | GLENEAYRE RESOURCES INC | 283.00 | 119.00 | 365 |
1988 | GLENEAYRE RESOURCES INC | 270.00 | 90.00 | 365 |
1989 | GLENEAYRE RESOURCES INC | 250.00 | 124.00 | 365 |
1990 | GLENEAYRE RESOURCES INC | 251.00 | 95.00 | 365 |
1992 | KAPLAN INTERESTS INC | 199.00 | 93.00 | 365 |
1993 | KAPLAN INTERESTS INC | 168.00 | 85.00 | 365 |
1994 | KAPLAN INTERESTS INC | 177.00 | 114.00 | 365 |
1995 | KAPLAN INTERESTS INC | 221.00 | 65.00 | 365 |
1996 | KAPLAN INTERESTS INC | 151.00 | 57.00 | 365 |
1997 | KAPLAN INTERESTS INC | 121.00 | 44.00 | 365 |
1998 | KAPLAN INTERESTS INC | 91.00 | 32.00 | 365 |
1999 | KAPLAN INTERESTS INC | 107.00 | 38.00 | 365 |
2000 | KAPLAN INTERESTS INC | 95.00 | 53.00 | 365 |
2001 | KAPLAN INTERESTS INC | 55.00 | 50.00 | 365 |
2002 | KAPLAN INTERESTS INC | 68.00 | 30.00 | 365 |
2003 | KAPLAN INTERESTS INC | 37.00 | 20.00 | 365 |
2004 | KEITO GAS INC | 4.00 | 18.00 | 180 |
2005 | KEITO GAS INC | 20.00 | 17.00 | 365 |
2006 | KEITO GAS INC | 18.00 | 38.00 | 365 |
2007 | KEITO GAS INC | 18.00 | 21.00 | 365 |
2008 | KEITO GAS INC | 32.00 | 32.00 | 365 |
2009 | KEITO GAS INC | 22.00 | 21.00 | 365 |
2010 | KEITO GAS INC | 36.00 | 51.00 | 365 |
2011 | KEITO GAS INC | 59.00 | 21.00 | 365 |
2012 | KEITO GAS INC | 34.00 | 48.00 | 366 |
2013 | KEITO GAS INC | 35.00 | 40.00 | 365 |
2014 | KEITO GAS INC | 29.00 | 28.00 | 365 |
2015 | KEITO GAS INC | 17.00 | 20.00 | 365 |
2016 | KEITO GAS INC | 1.00 | 24.00 | 270 |
2017 | AM-TEK OIL INC | 13.00 | 0.00 | 365 |
Period | Operator Name | Waste Type | Quantity (bbl) | Production Days |
---|---|---|---|---|
1987 | GLENEAYRE RESOURCES INC | Brine | 202 | 365 |
1988 | GLENEAYRE RESOURCES INC | Brine | 212 | 365 |
1989 | GLENEAYRE RESOURCES INC | Brine | 174 | 365 |
1990 | GLENEAYRE RESOURCES INC | Brine | 204 | 365 |
1992 | KAPLAN INTERESTS INC | Brine | 0 | 365 |
1993 | KAPLAN INTERESTS INC | Brine | 0 | 365 |
1994 | KAPLAN INTERESTS INC | Brine | 0 | 365 |
1995 | KAPLAN INTERESTS INC | Brine | 0 | 365 |
1996 | KAPLAN INTERESTS INC | Brine | 0 | 365 |
1997 | KAPLAN INTERESTS INC | Brine | 0 | 365 |
1998 | KAPLAN INTERESTS INC | Brine | 0 | 365 |
1999 | KAPLAN INTERESTS INC | Brine | 0 | 365 |
2000 | KAPLAN INTERESTS INC | Brine | 0 | 365 |
2001 | KAPLAN INTERESTS INC | Brine | 200 | 365 |
2002 | KAPLAN INTERESTS INC | Brine | 83 | 365 |
2003 | KAPLAN INTERESTS INC | Brine | 10 | 365 |
2004 | KEITO GAS INC | Brine | 0 | 180 |
2005 | KEITO GAS INC | Brine | 11 | 365 |
2006 | KEITO GAS INC | Brine | 0 | 365 |
2007 | KEITO GAS INC | Brine | 40 | 365 |
2008 | KEITO GAS INC | Brine | 14 | 365 |
2009 | KEITO GAS INC | Brine | 6 | 365 |
2010 | KEITO GAS INC | Brine | 5 | 365 |
2011 | KEITO GAS INC | Brine | 0 | 365 |
2012 | KEITO GAS INC | Brine | 19 | 366 |
2013 | KEITO GAS INC | Brine | 33 | 365 |
2014 | KEITO GAS INC | Brine | 36 | 365 |
2015 | KEITO GAS INC | Brine | 62 | 365 |
2016 | KEITO GAS INC | Brine | 270 | |
2017 | AM-TEK OIL INC | Brine | 0 | 365 |
Inspection ID | Inspection Date | Inspection Type | Inspection Result | Inspection Comments |
---|---|---|---|---|
-1282300567 | 2018-6-5 0:00:0 | PW | No Violations | 0.20 |
-1970611884 | 2018-5-17 0:00: | PW | No Violations | 0.10 |
0549390433 | 2018-06-07 | Production Wells | No Violations | The contaminated soils were removed, thus resolving this compliance notice |
1185071577 | 2018-07-11 | Production Wells | Violations Noted | The trash bags from the oily soil that were removed from this well are still sitting at the tank battery for this well. The bags of contaminated soil will need removed from the location. The area where the bags are will need remediated from any residual contamination that might have escaped the bags. |
1282300567 | 2018-06-05 | Production Wells | No Violations | While I was on the phone with Andrew Ulrich the owner of Am-Tek Oil concerning another matter. He arranged to meet me on Wednesday to get the mess cleaned up. |
1525265220 | 2018-05-02 | Production Wells | Violations Noted | This well is equipped with tubing, rods and a pumping unit. There was no motor present and power was disconnected. The horse head was all the way down in the down stroke and there was about 4 inches of slack in the bridle wire. The back of the unit was out of level and was about 3-4 inches low. There was no legible identification found at the wellhead. There was an identification tag but it was not filled out. The well is currently incapable of production. I spoke with Andrew Ulrich owner of the company at 10:15 am on 5/4/18 about this well and others that were issued. |
1527692412 | 2018-05-29 | Production Wells | Violations Noted | This well was written up for identification. However, there is now a small pool of oil around the wellhead that will need to be remediated. The source would appear to be the stuffing box or just below the stuffing box. Identification was posted and legible. |
1610758829 | 2020-8-4 0:00:0 | PW | No Violations | 0.30 |
1897313509 | 2018-08-14 | Production Wells | No Violations | The bags of contaminated soils have been removed from the tank battery. Violation is resolved. |
1970611884 | 2018-05-17 | Production Wells | No Violations | Well is properly identified. Violation is resolved. |
549390433 | 2018-6-7 0:00:0 | PW | No Violations | 0.50 |
Inspection ID | Violation ID | Violation Date | Violation Code | Violation Comments |
---|---|---|---|---|
1185071577 | US-OH-104892 | 2018-08-17 | 9-1-07 | Well operation causing pollution and contamination |
1185071577 | US-OH-104893 | 2018-08-17 | 9-9-02 | General Safety |
1525265220 | US-OH-114572 | 2018-05-31 | 9-9-05(A)10 | Failure to legibly identify well |
1527692412 | US-OH-114627 | 2018-06-25 | 9-1-07 | Well operation causing pollution and contamination |
For data sources see[8]