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Well ID: 34-009-21492 | Loading map...
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Country: United States | |
State: Ohio | |
County: Athens | |
Municipality: Ames Township | |
Operator Name: AM-TEK OIL INC | |
Well Pad ID: | |
Farm/Lease Name: WHITE THOMAS J | |
License Status: Producing | |
License Date: 1964-01-03 | |
Spud Date: 1964-02-13 | |
Spud Drilling Contractor: | |
Final Drill Date: 1964-02-24 | |
Well Total Depth: 1648.00 ft | |
Configuration: Vertical | |
Latitude: 39.380000 | |
Longitude: -81.950000 |
For data sources see[1]
Well Status | Well Status Date | Comment |
---|---|---|
Original Spud | 1964-02-13 | GL=796.7 |
Completed | 1964-02-24 | GL=796.7 |
Reached Total Depth | 1964-02-24 | GL=796.7 |
CO | 1991-06-20 | 3969 KAPLAN INTERESTS INC |
Change of Owner | 2004-07-08 | Operator changed from 3969, KAPLAN INTERESTS INC to 7671, KEITO GAS INC |
Change of Owner | 2016-11-03 | Operator changed from 7671, KEITO GAS INC to 9651, AM-TEK OIL INC |
Record Last Modified | 2016-11-03 | GL=796.7 |
For data sources see[2]
Stimulation Date | Chemical Agent | Chemical Agent Concentration (%) | Fracking Fluid Volume | Mass of Proppant Used (lb) | Fracking Company | Comments |
---|---|---|---|---|---|---|
H2O | 0 | 900 Bbl | 15000 |
For data sources see[3]
Period | Operator Name | Gas Quantity (mcf) | Oil Quantity (bbl) | Production Days |
---|---|---|---|---|
1984 | TRIPLE GAS CO | 212.00 | 418.00 | 0 |
1987 | GLENEAYRE RESOURCES INC | 283.00 | 119.00 | 365 |
1988 | GLENEAYRE RESOURCES INC | 270.00 | 90.00 | 365 |
1989 | GLENEAYRE RESOURCES INC | 251.00 | 125.00 | 365 |
1990 | GLENEAYRE RESOURCES INC | 251.00 | 95.00 | 365 |
1992 | KAPLAN INTERESTS INC | 199.00 | 0.00 | 365 |
1993 | KAPLAN INTERESTS INC | 168.00 | 0.00 | 365 |
1994 | KAPLAN INTERESTS INC | 177.00 | 0.00 | 365 |
1995 | KAPLAN INTERESTS INC | 221.00 | 0.00 | 365 |
1996 | KAPLAN INTERESTS INC | 151.00 | 0.00 | 365 |
1997 | KAPLAN INTERESTS INC | 121.00 | 0.00 | 365 |
1998 | KAPLAN INTERESTS INC | 91.00 | 32.00 | 365 |
1999 | KAPLAN INTERESTS INC | 107.00 | 38.00 | 365 |
2000 | KAPLAN INTERESTS INC | 95.00 | 53.00 | 365 |
2001 | KAPLAN INTERESTS INC | 55.00 | 50.00 | 365 |
2002 | KAPLAN INTERESTS INC | 68.00 | 30.00 | 365 |
2003 | KAPLAN INTERESTS INC | 37.00 | 20.00 | 365 |
2004 | KEITO GAS INC | 4.00 | 18.00 | 180 |
2005 | KEITO GAS INC | 20.00 | 17.00 | 365 |
2006 | KEITO GAS INC | 18.00 | 38.00 | 365 |
2007 | KEITO GAS INC | 18.00 | 21.00 | 365 |
2008 | KEITO GAS INC | 32.00 | 32.00 | 365 |
2009 | KEITO GAS INC | 22.00 | 21.00 | 365 |
2010 | KEITO GAS INC | 36.00 | 51.00 | 365 |
2011 | KEITO GAS INC | 59.00 | 21.00 | 365 |
2012 | KEITO GAS INC | 34.00 | 48.00 | 366 |
2013 | KEITO GAS INC | 35.00 | 40.00 | 365 |
2014 | KEITO GAS INC | 29.00 | 28.00 | 365 |
2015 | KEITO GAS INC | 17.00 | 20.00 | 365 |
2016 | KEITO GAS INC | 1.00 | 24.00 | 270 |
2017 | AM-TEK OIL INC | 13.00 | 0.00 | 365 |
Period | Operator Name | Waste Type | Quantity (bbl) | Production Days |
---|---|---|---|---|
1984 | TRIPLE GAS CO | Brine | 0 | 0 |
1987 | GLENEAYRE RESOURCES INC | Brine | 202 | 365 |
1988 | GLENEAYRE RESOURCES INC | Brine | 213 | 365 |
1989 | GLENEAYRE RESOURCES INC | Brine | 173 | 365 |
1990 | GLENEAYRE RESOURCES INC | Brine | 204 | 365 |
1992 | KAPLAN INTERESTS INC | Brine | 0 | 365 |
1993 | KAPLAN INTERESTS INC | Brine | 0 | 365 |
1994 | KAPLAN INTERESTS INC | Brine | 0 | 365 |
1995 | KAPLAN INTERESTS INC | Brine | 0 | 365 |
1996 | KAPLAN INTERESTS INC | Brine | 0 | 365 |
1997 | KAPLAN INTERESTS INC | Brine | 0 | 365 |
1998 | KAPLAN INTERESTS INC | Brine | 0 | 365 |
1999 | KAPLAN INTERESTS INC | Brine | 0 | 365 |
2000 | KAPLAN INTERESTS INC | Brine | 0 | 365 |
2001 | KAPLAN INTERESTS INC | Brine | 200 | 365 |
2002 | KAPLAN INTERESTS INC | Brine | 83 | 365 |
2003 | KAPLAN INTERESTS INC | Brine | 10 | 365 |
2004 | KEITO GAS INC | Brine | 0 | 180 |
2005 | KEITO GAS INC | Brine | 11 | 365 |
2006 | KEITO GAS INC | Brine | 0 | 365 |
2007 | KEITO GAS INC | Brine | 40 | 365 |
2008 | KEITO GAS INC | Brine | 14 | 365 |
2009 | KEITO GAS INC | Brine | 6 | 365 |
2010 | KEITO GAS INC | Brine | 5 | 365 |
2011 | KEITO GAS INC | Brine | 0 | 365 |
2012 | KEITO GAS INC | Brine | 19 | 366 |
2013 | KEITO GAS INC | Brine | 33 | 365 |
2014 | KEITO GAS INC | Brine | 36 | 365 |
2015 | KEITO GAS INC | Brine | 62 | 365 |
2016 | KEITO GAS INC | Brine | 270 | |
2017 | AM-TEK OIL INC | Brine | 0 | 365 |
Inspection ID | Inspection Date | Inspection Type | Inspection Result | Inspection Comments |
---|---|---|---|---|
-117995395 | 2018-6-7 0:00:0 | PW | No Violations | 0.40 |
-1388729019 | 2018-5-29 0:00: | PW | No Violations | 0.30 |
-1643837146 | 2018-7-11 0:00: | PW | No Violations | 0.30 |
0117995395 | 2018-06-07 | Production Wells | No Violations | I was accompanied to the well by Andrew Ulrich who while on the location made a sign for the well and identified it. Andrew hopes to get a rig on this well by the end of August. |
0236362143 | 2018-08-14 | Production Wells | No Violations | This well is still open to the atmosphere. I called Andrew Ulrich the owner of Am-tek who plans to make this a swab well. He said he will swab it yearly to get the oil and fluid off of it. I contacted Andrew the owner of the company about resolving this violation he said he was waitng to get a rig on it. |
0985291538 | 2018-05-02 | Production Wells | Violations Noted | This well is just 4.5 inch casing sticking out of the ground. The swage nipple is unscrewed off the casing and laying next to it. There were no valves and no flowlines attached. There was also no identification. The well is not currently capable of well control. I spoke with Andrew Ulrich owner of company at 10:15 am on 5/4/18 about this well and others that were issued violations. |
0986569621 | 2018-12-03 | Production Wells | No Violations | This well was originally issued a compliance notice because it was open to atmosphere and to be plugged. Andrew the owner of Am-tek said he was going to make it a swab well. However, nothing has been done to comply with the original violations issued. |
1388729019 | 2018-05-29 | Production Wells | No Violations | The 4.5 casing is still open to the atmosphere and no flowlines attached. The wellhead was not identified either. |
1643837146 | 2018-07-11 | Production Wells | No Violations | This well is still not capable of production in its current state. There is only 4.5 inch diameter casing sticking out of the ground. I sent Andrew the owner an email about this well and the follow-up I conducted today. |
2123822703 | 2020-8-4 0:00:0 | PW | No Violations | 0.20 |
236362143 | 2018-8-14 0:00: | PW | No Violations | 0.40 |
985291538 | 2018-5-2 0:00:0 | PW | No Violations | 0.30 |
986569621 | 2018-12-3 0:00: | PW | No Violations | 0.40 |
Inspection ID | Violation ID | Violation Date | Violation Code | Violation Comments |
---|---|---|---|---|
0985291538 | US-OH-131319 | 2018-05-11 | 9-9-05(A)1 | Well insufficiently equipped to prevent escape of oil and gas |
0985291538 | US-OH-131320 | 2018-05-11 | 9-9-05(A)10 | Failure to legibly identify well |
For data sources see[8]