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Well ID: 34-009-21705 | Loading map...
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Country: United States | |
State: Ohio | |
County: Athens | |
Municipality: York Township | |
Operator Name: KILBARGER INVESTMENTS INC | |
Well Pad ID: | |
Farm/Lease Name: WHARTON | |
License Status: Final Restoration | |
License Date: 2018-09-27 | |
Spud Date: 1971-10-01 | |
Spud Drilling Contractor: | |
Final Drill Date: 1972-01-01 | |
Well Total Depth: 3236.00 ft | |
Configuration: Vertical | |
Latitude: 39.450000 | |
Longitude: -82.250000 |
For data sources see[1]
Well Status | Well Status Date | Comment |
---|---|---|
CO | 1971-10-01 | 125 ELKHEAD GAS & OIL CO GeoDate 10/1/71 |
Original Spud | 1971-10-01 | |
Completed | 1972-01-01 | |
Reached Total Depth | 1972-01-01 | |
Change of Owner | 1999-12-13 | Operator changed from 125, ELKHEAD GAS & OIL CO to 1675, KILBARGER EDWARD OR ANN |
APP | 2018-09-27 | Proposed Formations:CLINTON SAND, Issued Date:9/27/2018, Expired Date:9/26/2020 12:00:00 PM, Drilling unit acres:0, Proposed Well Type:OG, Proposed Well Class: |
Plugged/Abandoned | 2018-10-04 | |
Record Last Modified | 2019-01-30 | |
Construction Permit Expires | 2020-09-26 |
For data sources see[2]
Stimulation Date | Chemical Agent | Chemical Agent Concentration (%) | Fracking Fluid Volume | Mass of Proppant Used (lb) | Fracking Company | Comments |
---|---|---|---|---|---|---|
0 | 0 | 0 |
For data sources see[3]
Period | Operator Name | Gas Quantity (mcf) | Oil Quantity (bbl) | Production Days |
---|---|---|---|---|
1985 | ELKHEAD GAS & OIL CO | 0.00 | 0.00 | 0 |
1988 | ELKHEAD GAS & OIL CO | 8725.00 | 0.00 | 351 |
1989 | ELKHEAD GAS & OIL CO | 7721.00 | 0.00 | 334 |
1990 | ELKHEAD GAS & OIL CO | 4925.00 | 0.00 | 360 |
1991 | ELKHEAD GAS & OIL CO | 5128.00 | 0.00 | 361 |
1992 | ELKHEAD GAS & OIL CO | 2611.00 | 0.00 | 301 |
1993 | ELKHEAD GAS & OIL CO | 2471.00 | 0.00 | 211 |
1994 | ELKHEAD GAS & OIL CO | 1323.00 | 0.00 | 350 |
1995 | ELKHEAD GAS & OIL CO | 689.00 | 0.00 | 350 |
2014 | KILBARGER INVESTMENTS INC | 50.00 | 0.00 | 365 |
2017 | KILBARGER INVESTMENTS INC | 0.00 | 0.00 | 365 |
2018 | KILBARGER INVESTMENTS INC | 0.00 | 0.00 | 365 |
Period | Operator Name | Waste Type | Quantity (bbl) | Production Days |
---|---|---|---|---|
1985 | ELKHEAD GAS & OIL CO | Brine | 0 | 0 |
1988 | ELKHEAD GAS & OIL CO | Brine | 0 | 351 |
1989 | ELKHEAD GAS & OIL CO | Brine | 0 | 334 |
1990 | ELKHEAD GAS & OIL CO | Brine | 0 | 360 |
1991 | ELKHEAD GAS & OIL CO | Brine | 0 | 361 |
1992 | ELKHEAD GAS & OIL CO | Brine | 0 | 301 |
1993 | ELKHEAD GAS & OIL CO | Brine | 0 | 211 |
1994 | ELKHEAD GAS & OIL CO | Brine | 0 | 350 |
1995 | ELKHEAD GAS & OIL CO | Brine | 0 | 350 |
2014 | KILBARGER INVESTMENTS INC | Brine | 0 | 365 |
2017 | KILBARGER INVESTMENTS INC | Brine | 0 | 365 |
2018 | KILBARGER INVESTMENTS INC | Brine | 0 | 365 |
Inspection ID | Inspection Date | Inspection Type | Inspection Result | Inspection Comments |
---|---|---|---|---|
-1012815770 | 2017-10-17 0:00 | PW | No Violations | 0.50 |
-1057003201 | 2016-1-5 0:00:0 | PW | No Violations | 1.00 |
-1096926030 | 2016-5-12 0:00: | PW | No Violations | 2.40 |
-1151581589 | 2018-8-16 0:00: | PW | No Violations | 0.50 |
-1160416986 | 2018-10-2 0:00: | PB | No Violations | |
-1299985660 | 2018-5-25 0:00: | PW | No Violations | 0.40 |
-1379978637 | 2018-10-5 0:00: | PB | No Violations | |
-1405637122 | 2018-2-2 0:00:0 | PW | No Violations | 1.50 |
-1498609745 | 2018-10-1 0:00: | PB | No Violations | |
-1556072327 | 2015-10-21 0:00 | PW | No Violations | 0.70 |
-2015352386 | 2019-11-29 0:00 | FR | No Violations | 0.40 |
-273731528 | 2018-10-4 0:00: | PB | No Violations | 4.50 |
-527666671 | 2013-8-15 0:00: | PW | No Violations | 0.80 |
-592581293 | 2018-10-18 0:00 | PB | No Violations | 0.40 |
-594441679 | 2018-10-12 0:00 | PB | No Violations | 0.30 |
-630612121 | 2019-7-2 0:00:0 | FR | No Violations | 1.00 |
-945200148 | 2018-3-13 0:00: | PW | No Violations | 0.50 |
0273731528 | 2018-10-04 | Plug / Plug Back | No Violations | Today the plugging crew shoveled clay for about 3 hours till the hole filled back up. They will need to let the clay slurry settle out. They then started moving out some equipment. The violation to plug the well is closed. |
0527666671 | 2013-08-15 | Production Wells | No Violations | Follow up to 1416250079. Identification on well, 4 1/2 casing equipped with a swedge and a closed 2 ball valve. There is a separator and multiple drips on site. A large oak tree has fallen across the site and landed on top of the 50 barrel steel tank, denting the lid and side of the tank. No production has been reported. |
0592581293 | 2018-10-18 | Plug / Plug Back | No Violations | The clay was still at the surface and the location was drying out. I called Nick with Kilbargers. I let him know the location was drying out and he said he would try to get people in there on Friday if it didnt rain. |
0594441679 | 2018-10-12 | Plug / Plug Back | No Violations | Location was still extremely muddy and water logged. The clay was down about 4 feet. I called Nick Vicerelli and he expressed concern with it being too wet to reclaim the area. I explained that it would be a good thing to leave the hole open and allow me to monitor the level of the clay and finish the reclaim when the location has dried out a little bit. |
0725119742 | 2016-06-08 | Production Wells | No Violations | Met with Nick Valentine on location and walked to the well site. He agreed to have the old 40 barrel tank off the location and start work to lay a line to the horse barn for the land owners until such time as they can figure out a way to get to a sale line. |
0841250966 | 2017-06-26 | Production Wells | No Violations | The well is still idle, except for clearing out the brush last year nothing has been done to bring the well into compliance. The well has no flowline connected to it. I spoke with the land owners who would be thrilled to have access to house gas. |
0945200148 | 2018-03-13 | Production Wells | No Violations | I called Jim Kilbarger today about this well and he said he would have Nick call me back or he himself would. To let me know exactly what is going to happen with the well. I explained that I was putting together a Chiefs Order Request. |
1012815770 | 2017-10-17 | Production Wells | No Violations | Inspection of the well found the well in the exact non-compliance state as previous inspections. I was able to get Jim Kilbargers number from another inspector and left him a message and received no return call. |
1057003201 | 2016-01-05 | Production Wells | No Violations | Follow up to 1416250079. No lines or equipment hooked to wellhead, valves closed at well head. |
1096926030 | 2016-05-12 | Production Wells | No Violations | Could not locate a entry point for this well. No one was home at the time to ask property owner. Will call Kilbargers. |
1151581589 | 2018-08-16 | Production Wells | No Violations | Nothing was completed at the location. Well was found to still be idle. I called Nick Vickerelli who said he had no information about what is going on with the wells. He said he would talk with Jim Kilbarger about it. |
1160416986 | 2018-10-02 | Plug / Plug Back | No Violations | The plugging crew finished placing 3.5 tons of clay slurry into the 4.5 inch casing for the bottom plug. They then went into rip the pipe. They were able to get telegraph at 2424 feet. They ripped the pipe and pulled 7 joints and placed about 4 ton of clay to cover up the top of the lime. |
1299985660 | 2018-05-25 | Production Wells | No Violations | Follow up to Chiefs Order to plug well. The well is still idle pictures were taken. I spoke to Nick Vickerelli a few days ago who stated they plan to appeal the order. There were no flowlines attached to the wellhead. The vertical separator was laying over on its side. |
1364521892 | 2018-05-15 | Production Wells | No Violations | This well was issued a violation for non-production. A subsequent Chiefs Order was issued for the well to be plugged. The well is still idle and not capable of production. Pictures were taken. |
1369748643 | 2013-05-28 | Production Wells | No Violations | Follow up to 1416250079. The producer has placed an identification on the well head. No lines or equipment is hooked up at the well head. The valve at the well head was closed. The corroded tank, lines, and separator was on site. |
1379978637 | 2018-10-05 | Plug / Plug Back | No Violations | Went today to check the level of the clay plug. The clay was down further than I could see I called Nick Vickerelli and shared my findings. |
1387205012 | 2013-12-16 | Production Wells | No Violations | Follow up to 1416250079. Identification on well. No lines or equipment at wellhead. 50 Barrel tank still has holes and a fallen tree branch on top of it. |
1392213964 | 2014-02-12 | Production Wells | No Violations | Follow up to 1416250079. No lines or equipment at well, 2 valve on production closed. 50 Barrel steel tank on site is empty and unable to contain fluids. There is a large tree branch that has fallen on the tank. |
1392318813 | 2014-02-13 | Administrative Inspection | No Violations | Follow up to 1416250079. Supervisor Dan Goins spoke with Jim Kilbarger regarding the timeline of resolving the violation. The company plans to have violations resolved by July 1st of 2014. |
1404317326 | 2014-07-02 | Production Wells | No Violations | Follow up to 1416250079. No lines or production equipment at well head, valve closed. Separator laying on its side and the 30 Bbl tank still has a tree limb on top of it. |
1405637122 | 2018-02-02 | Production Wells | No Violations | Took pictures of the well as it was today, idle, disconnected and not capable of production. I tried to call Jim Kilbarger and got his voicemail. |
1416250079 | 2013-01-24 | Production Wells | Violations Noted | The conductor and surface casing were open at the surface. The 4 1/2 production casing was on hangers and equipped with a swedge and a closed 2 ball valve. The 50 Barrel tanks has corroded away in many places but there is no evidence of contamination. Two drips and a separator are on site but inoperable. The identification on the well is incorrect. No production has been reported since 1991. All producing leases shall be legibly identified in a conspicuous place on or near the well-head or the storage tank as to owner, lease name, well number, permit number where available, county, and an emergency telephone number. The well shall be plugged or produced. |
1416409619 | 2014-11-19 | Production Wells | No Violations | Follow up to 1416250079. Work has been done to clean up brush at well site, but well remains idle. |
1498609745 | 2018-10-01 | Plug / Plug Back | No Violations | When I arrived today they were finishing sitting up the rig and getting the location ready to plug. Once they started shoveling clay the water came out of the 8 inch casing first, showing a hole in the 4.5 inch, somewhere. I asked them to shovel the 3.5 tons of clay in now before the rip to get as much down the 4.5 inch casing as possible. They finished up the day having placed 3 tons of clay in the hole. |
1527707716 | 2018-05-30 | Production Wells | No Violations | This well was originally issued a violation for O.R.C. 1509.12B. Today the wellhead is comprised of 4.5 casing, swage nipple to 2 with a valve in the closed position. The 4.5 casing is hanging on a casing hanger. There are no flowlines connected to the wellhead. The vertical separator is knocked over and laying on its side. This is the same state as I have found the well to be in previous inspections. |
1531835806 | 2018-07-17 | Production Wells | No Violations | The well remains in a state that is not capable of production. There are no flowlines connected to the swage nipple from 4.5 inch to 2 inch. The valve is in the closed position on the top of the swage nipple. I called and left a message with Nick Vickerelly the field supervisor with Kilbargers. |
1556072327 | 2015-10-21 | Production Wells | No Violations | Follow up to 1416250079. The conductor and the surface casing were open at the surface. The production casing was equipped with a reducer swedge and a closed 2 ball valve. There were no lines at the well. The 50 Bbl steel tank was still on site and full of holes, the separator was also on site but was laying on its side. |
1935580698 | 2014-08-18 | Production Wells | No Violations | Follow up to 1416250079. No lines or production equipment at well head, valve closed. |
2099104217 | 2018-10-03 | Plug / Plug Back | No Violations | Today I received a call saying the pipe that was ripped yesterday was stuck in the hole. Nick called me and said they pulled 45000 on it and wouldnt move, that was double the pipe weight. They were leery about pulling anymore than that because the location was very soft. I explained I was close and would be there in a minute. Once on location they let the pipe down and screwed in a short nipple and worked the pipe for about an hour and a half up and down. The pipe started coming and they pulled the 2424 feet of pipe. They then sat the pre-cast 7 inch plug on the 7 inch casing seat. Then they started the clay slurry. |
725119742 | 2016-6-8 0:00:0 | PW | No Violations | 2.30 |
841250966 | 2017-6-26 0:00: | PW | No Violations | 2.00 |
882145465 | 2019-11-7 0:00: | FR | No Violations | 0.30 |
9856841 | 2019-8-20 0:00: | FR | No Violations | 1.00 |
Inspection ID | Violation ID | Violation Date | Violation Code | Violation Comments |
---|---|---|---|---|
1416250079 | US-OH-112215 | 2013-01-24 | Failure to legibly identify well | |
1416250079 | US-OH-112216 | 2013-01-24 | Well shall be plugged | |
1416250079 | US-OH-112217 | 2013-01-24 | Nonproduction; well shall be plugged or placed in temporary inactive status |
For data sources see[8]