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34-009-21705

Well Details

Well ID: 34-009-21705
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Country: United States
State: Ohio
County: Athens
Municipality: York Township
Operator Name: KILBARGER INVESTMENTS INC
Well Pad ID:
Farm/Lease Name: WHARTON
License Status: Final Restoration
License Date: 2018-09-27
Spud Date: 1971-10-01
Spud Drilling Contractor:
Final Drill Date: 1972-01-01
Well Total Depth: 3236.00 ft
Configuration: Vertical
Latitude: 39.450000
Longitude: -82.250000

For data sources see[1]

Well History

Well Status Well Status Date Comment
CO 1971-10-01 125 ELKHEAD GAS & OIL CO GeoDate 10/1/71
Original Spud 1971-10-01
Completed 1972-01-01
Reached Total Depth 1972-01-01
Change of Owner 1999-12-13 Operator changed from 125, ELKHEAD GAS & OIL CO to 1675, KILBARGER EDWARD OR ANN
APP 2018-09-27 Proposed Formations:CLINTON SAND, Issued Date:9/27/2018, Expired Date:9/26/2020 12:00:00 PM, Drilling unit acres:0, Proposed Well Type:OG, Proposed Well Class:
Plugged/Abandoned 2018-10-04
Record Last Modified 2019-01-30
Construction Permit Expires 2020-09-26

For data sources see[2]

Stimulations Data

Stimulation Date Chemical Agent Chemical Agent Concentration (%) Fracking Fluid Volume Mass of Proppant Used (lb) Fracking Company Comments
0 0 0

For data sources see[3]

Production Data

Period Operator Name Gas Quantity (mcf) Oil Quantity (bbl) Production Days
1985 ELKHEAD GAS & OIL CO 0.00 0.00 0
1988 ELKHEAD GAS & OIL CO 8725.00 0.00 351
1989 ELKHEAD GAS & OIL CO 7721.00 0.00 334
1990 ELKHEAD GAS & OIL CO 4925.00 0.00 360
1991 ELKHEAD GAS & OIL CO 5128.00 0.00 361
1992 ELKHEAD GAS & OIL CO 2611.00 0.00 301
1993 ELKHEAD GAS & OIL CO 2471.00 0.00 211
1994 ELKHEAD GAS & OIL CO 1323.00 0.00 350
1995 ELKHEAD GAS & OIL CO 689.00 0.00 350
2014 KILBARGER INVESTMENTS INC 50.00 0.00 365
2017 KILBARGER INVESTMENTS INC 0.00 0.00 365
2018 KILBARGER INVESTMENTS INC 0.00 0.00 365

For data sources see[4] [5]

Waste Data

Period Operator Name Waste Type Quantity (bbl) Production Days
1985 ELKHEAD GAS & OIL CO Brine 0 0
1988 ELKHEAD GAS & OIL CO Brine 0 351
1989 ELKHEAD GAS & OIL CO Brine 0 334
1990 ELKHEAD GAS & OIL CO Brine 0 360
1991 ELKHEAD GAS & OIL CO Brine 0 361
1992 ELKHEAD GAS & OIL CO Brine 0 301
1993 ELKHEAD GAS & OIL CO Brine 0 211
1994 ELKHEAD GAS & OIL CO Brine 0 350
1995 ELKHEAD GAS & OIL CO Brine 0 350
2014 KILBARGER INVESTMENTS INC Brine 0 365
2017 KILBARGER INVESTMENTS INC Brine 0 365
2018 KILBARGER INVESTMENTS INC Brine 0 365

For data sources see[6] [7]

Inspection Data

Inspections Performed

Inspection ID Inspection Date Inspection Type Inspection Result Inspection Comments
-1012815770 2017-10-17 0:00 PW No Violations 0.50
-1057003201 2016-1-5 0:00:0 PW No Violations 1.00
-1096926030 2016-5-12 0:00: PW No Violations 2.40
-1151581589 2018-8-16 0:00: PW No Violations 0.50
-1160416986 2018-10-2 0:00: PB No Violations
-1299985660 2018-5-25 0:00: PW No Violations 0.40
-1379978637 2018-10-5 0:00: PB No Violations
-1405637122 2018-2-2 0:00:0 PW No Violations 1.50
-1498609745 2018-10-1 0:00: PB No Violations
-1556072327 2015-10-21 0:00 PW No Violations 0.70
-2015352386 2019-11-29 0:00 FR No Violations 0.40
-273731528 2018-10-4 0:00: PB No Violations 4.50
-527666671 2013-8-15 0:00: PW No Violations 0.80
-592581293 2018-10-18 0:00 PB No Violations 0.40
-594441679 2018-10-12 0:00 PB No Violations 0.30
-630612121 2019-7-2 0:00:0 FR No Violations 1.00
-945200148 2018-3-13 0:00: PW No Violations 0.50
0273731528 2018-10-04 Plug / Plug Back No Violations Today the plugging crew shoveled clay for about 3 hours till the hole filled back up. They will need to let the clay slurry settle out. They then started moving out some equipment. The violation to plug the well is closed.
0527666671 2013-08-15 Production Wells No Violations Follow up to 1416250079. Identification on well, 4 1/2 casing equipped with a swedge and a closed 2 ball valve. There is a separator and multiple drips on site. A large oak tree has fallen across the site and landed on top of the 50 barrel steel tank, denting the lid and side of the tank. No production has been reported.
0592581293 2018-10-18 Plug / Plug Back No Violations The clay was still at the surface and the location was drying out. I called Nick with Kilbargers. I let him know the location was drying out and he said he would try to get people in there on Friday if it didnt rain.
0594441679 2018-10-12 Plug / Plug Back No Violations Location was still extremely muddy and water logged. The clay was down about 4 feet. I called Nick Vicerelli and he expressed concern with it being too wet to reclaim the area. I explained that it would be a good thing to leave the hole open and allow me to monitor the level of the clay and finish the reclaim when the location has dried out a little bit.
0725119742 2016-06-08 Production Wells No Violations Met with Nick Valentine on location and walked to the well site. He agreed to have the old 40 barrel tank off the location and start work to lay a line to the horse barn for the land owners until such time as they can figure out a way to get to a sale line.
0841250966 2017-06-26 Production Wells No Violations The well is still idle, except for clearing out the brush last year nothing has been done to bring the well into compliance. The well has no flowline connected to it. I spoke with the land owners who would be thrilled to have access to house gas.
0945200148 2018-03-13 Production Wells No Violations I called Jim Kilbarger today about this well and he said he would have Nick call me back or he himself would. To let me know exactly what is going to happen with the well. I explained that I was putting together a Chiefs Order Request.
1012815770 2017-10-17 Production Wells No Violations Inspection of the well found the well in the exact non-compliance state as previous inspections. I was able to get Jim Kilbargers number from another inspector and left him a message and received no return call.
1057003201 2016-01-05 Production Wells No Violations Follow up to 1416250079. No lines or equipment hooked to wellhead, valves closed at well head.
1096926030 2016-05-12 Production Wells No Violations Could not locate a entry point for this well. No one was home at the time to ask property owner. Will call Kilbargers.
1151581589 2018-08-16 Production Wells No Violations Nothing was completed at the location. Well was found to still be idle. I called Nick Vickerelli who said he had no information about what is going on with the wells. He said he would talk with Jim Kilbarger about it.
1160416986 2018-10-02 Plug / Plug Back No Violations The plugging crew finished placing 3.5 tons of clay slurry into the 4.5 inch casing for the bottom plug. They then went into rip the pipe. They were able to get telegraph at 2424 feet. They ripped the pipe and pulled 7 joints and placed about 4 ton of clay to cover up the top of the lime.
1299985660 2018-05-25 Production Wells No Violations Follow up to Chiefs Order to plug well. The well is still idle pictures were taken. I spoke to Nick Vickerelli a few days ago who stated they plan to appeal the order. There were no flowlines attached to the wellhead. The vertical separator was laying over on its side.
1364521892 2018-05-15 Production Wells No Violations This well was issued a violation for non-production. A subsequent Chiefs Order was issued for the well to be plugged. The well is still idle and not capable of production. Pictures were taken.
1369748643 2013-05-28 Production Wells No Violations Follow up to 1416250079. The producer has placed an identification on the well head. No lines or equipment is hooked up at the well head. The valve at the well head was closed. The corroded tank, lines, and separator was on site.
1379978637 2018-10-05 Plug / Plug Back No Violations Went today to check the level of the clay plug. The clay was down further than I could see I called Nick Vickerelli and shared my findings.
1387205012 2013-12-16 Production Wells No Violations Follow up to 1416250079. Identification on well. No lines or equipment at wellhead. 50 Barrel tank still has holes and a fallen tree branch on top of it.
1392213964 2014-02-12 Production Wells No Violations Follow up to 1416250079. No lines or equipment at well, 2 valve on production closed. 50 Barrel steel tank on site is empty and unable to contain fluids. There is a large tree branch that has fallen on the tank.
1392318813 2014-02-13 Administrative Inspection No Violations Follow up to 1416250079. Supervisor Dan Goins spoke with Jim Kilbarger regarding the timeline of resolving the violation. The company plans to have violations resolved by July 1st of 2014.
1404317326 2014-07-02 Production Wells No Violations Follow up to 1416250079. No lines or production equipment at well head, valve closed. Separator laying on its side and the 30 Bbl tank still has a tree limb on top of it.
1405637122 2018-02-02 Production Wells No Violations Took pictures of the well as it was today, idle, disconnected and not capable of production. I tried to call Jim Kilbarger and got his voicemail.
1416250079 2013-01-24 Production Wells Violations Noted The conductor and surface casing were open at the surface. The 4 1/2 production casing was on hangers and equipped with a swedge and a closed 2 ball valve. The 50 Barrel tanks has corroded away in many places but there is no evidence of contamination. Two drips and a separator are on site but inoperable. The identification on the well is incorrect. No production has been reported since 1991. All producing leases shall be legibly identified in a conspicuous place on or near the well-head or the storage tank as to owner, lease name, well number, permit number where available, county, and an emergency telephone number. The well shall be plugged or produced.
1416409619 2014-11-19 Production Wells No Violations Follow up to 1416250079. Work has been done to clean up brush at well site, but well remains idle.
1498609745 2018-10-01 Plug / Plug Back No Violations When I arrived today they were finishing sitting up the rig and getting the location ready to plug. Once they started shoveling clay the water came out of the 8 inch casing first, showing a hole in the 4.5 inch, somewhere. I asked them to shovel the 3.5 tons of clay in now before the rip to get as much down the 4.5 inch casing as possible. They finished up the day having placed 3 tons of clay in the hole.
1527707716 2018-05-30 Production Wells No Violations This well was originally issued a violation for O.R.C. 1509.12B. Today the wellhead is comprised of 4.5 casing, swage nipple to 2 with a valve in the closed position. The 4.5 casing is hanging on a casing hanger. There are no flowlines connected to the wellhead. The vertical separator is knocked over and laying on its side. This is the same state as I have found the well to be in previous inspections.
1531835806 2018-07-17 Production Wells No Violations The well remains in a state that is not capable of production. There are no flowlines connected to the swage nipple from 4.5 inch to 2 inch. The valve is in the closed position on the top of the swage nipple. I called and left a message with Nick Vickerelly the field supervisor with Kilbargers.
1556072327 2015-10-21 Production Wells No Violations Follow up to 1416250079. The conductor and the surface casing were open at the surface. The production casing was equipped with a reducer swedge and a closed 2 ball valve. There were no lines at the well. The 50 Bbl steel tank was still on site and full of holes, the separator was also on site but was laying on its side.
1935580698 2014-08-18 Production Wells No Violations Follow up to 1416250079. No lines or production equipment at well head, valve closed.
2099104217 2018-10-03 Plug / Plug Back No Violations Today I received a call saying the pipe that was ripped yesterday was stuck in the hole. Nick called me and said they pulled 45000 on it and wouldnt move, that was double the pipe weight. They were leery about pulling anymore than that because the location was very soft. I explained I was close and would be there in a minute. Once on location they let the pipe down and screwed in a short nipple and worked the pipe for about an hour and a half up and down. The pipe started coming and they pulled the 2424 feet of pipe. They then sat the pre-cast 7 inch plug on the 7 inch casing seat. Then they started the clay slurry.
725119742 2016-6-8 0:00:0 PW No Violations 2.30
841250966 2017-6-26 0:00: PW No Violations 2.00
882145465 2019-11-7 0:00: FR No Violations 0.30
9856841 2019-8-20 0:00: FR No Violations 1.00

Violations Commited

Inspection ID Violation ID Violation Date Violation Code Violation Comments
1416250079 US-OH-112215 2013-01-24 Failure to legibly identify well
1416250079 US-OH-112216 2013-01-24 Well shall be plugged
1416250079 US-OH-112217 2013-01-24 Nonproduction; well shall be plugged or placed in temporary inactive status

For data sources see[8]

References