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Well ID: 34-009-21988 | Loading map...
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Country: United States | |
State: Ohio | |
County: Athens | |
Municipality: Bern Township | |
Operator Name: OLD SOUTH OIL LLC | |
Well Pad ID: | |
Farm/Lease Name: FEDERAL VALLEY COASL CO / BLACK DIAMOND | |
License Status: Producing | |
License Date: 1979-10-17 | |
Spud Date: 1979-11-07 | |
Spud Drilling Contractor: | |
Final Drill Date: 1979-11-12 | |
Well Total Depth: 4861.00 ft | |
Configuration: Vertical | |
Latitude: 39.390000 | |
Longitude: -81.880000 |
For data sources see[1]
Well Status | Well Status Date | Comment |
---|---|---|
CO | 1979-10-17 | 2861 JOHNSON DWIGHT GeoDate 10/17/79 |
Original Spud | 1979-11-07 | R.L. & R.I. 11-21-79 |
Completed | 1979-11-12 | R.L. & R.I. 11-21-79 |
Reached Total Depth | 1979-11-12 | R.L. & R.I. 11-21-79 |
Construction Permit Expires | 1980-10-16 | R.L. & R.I. 11-21-79 |
CO | 1993-02-04 | 28 CGAS EXPLORATION,INC GeoDate 10/17/79 |
Change of Owner | 1998-02-05 | Operator changed from 28, CGAS EXPLORATION to 5063, BUTCHER ENERGY CORP |
Change of Owner | 2002-10-03 | Operator changed from 5063, BUTCHER ENERGY CORP to 309, CHAMBERLAIN dba/OLD SOUTH OIL |
Change of Owner | 2008-07-17 | Operator changed from 0309, CHAMBERLAIN dba/OLD SOUTH OIL to 8390, OLD SOUTH OIL LLC |
Record Last Modified | 2013-10-03 | R.L. & R.I. 11-21-79 |
For data sources see[2]
Perforation Date | Interval Top (ft) | Interval Base (ft) | Number of Shots |
---|---|---|---|
2006-09-11 | 4646 | 4741 | 1 |
4646 | 4741 | 1 | |
4646 | 4741 | 1 |
For data sources see[3]
Stimulation Date | Chemical Agent | Chemical Agent Concentration (%) | Fracking Fluid Volume | Mass of Proppant Used (lb) | Fracking Company | Comments |
---|---|---|---|---|---|---|
H2O | 0 | 1210 Bbl | 45000 |
For data sources see[4]
Period | Operator Name | Gas Quantity (mcf) | Oil Quantity (bbl) | Production Days |
---|---|---|---|---|
1988 | JOHNSON DWIGHT | 1952.00 | 0.00 | 184 |
1990 | JOHNSON DWIGHT | 222.00 | 0.00 | 84 |
1992 | JOHNSON DWIGHT | 226.00 | 0.00 | 70 |
1993 | CGAS EXPLORATION | 654.00 | 0.00 | 366 |
1994 | CGAS EXPLORATION | 1438.00 | 0.00 | 365 |
1995 | CGAS EXPLORATION | 983.00 | 0.00 | 365 |
1996 | CGAS EXPLORATION | 7.00 | 0.00 | 365 |
1997 | CGAS EXPLORATION | 0.00 | 0.00 | 365 |
1998 | BUTCHER ENERGY CORP | 1023.00 | 0.00 | 365 |
1999 | BUTCHER ENERGY CORP | 942.00 | 0.00 | 365 |
2000 | BUTCHER ENERGY CORP | 952.00 | 0.00 | 365 |
2001 | BUTCHER ENERGY CORP | 744.00 | 0.00 | 365 |
2002 | CHAMBERLAIN dba/OLD SOUTH OIL | 875.00 | 0.00 | 365 |
2003 | CHAMBERLAIN dba/OLD SOUTH OIL | 735.00 | 0.00 | 365 |
2004 | CHAMBERLAIN dba/OLD SOUTH OIL | 920.00 | 0.00 | 365 |
2005 | CHAMBERLAIN dba/OLD SOUTH OIL | 730.00 | 0.00 | 365 |
2006 | CHAMBERLAIN dba/OLD SOUTH OIL | 200.00 | 0.00 | 365 |
2007 | CHAMBERLAIN dba/OLD SOUTH OIL | 260.00 | 0.00 | 365 |
2008 | OLD SOUTH OIL LLC | 18.00 | 0.00 | 183 |
2009 | OLD SOUTH OIL LLC | 80.00 | 0.00 | 365 |
2010 | OLD SOUTH OIL LLC | 12.00 | 0.00 | 365 |
2011 | OLD SOUTH OIL LLC | 14.00 | 0.00 | 0 |
2012 | OLD SOUTH OIL LLC | 5.00 | 0.00 | 366 |
2013 | OLD SOUTH OIL LLC | 0.00 | 0.00 | 0 |
2014 | OLD SOUTH OIL LLC | 87.00 | 0.00 | 365 |
2015 | OLD SOUTH OIL LLC | 0.00 | 0.00 | 0 |
2016 | OLD SOUTH OIL LLC | 298.00 | 0.00 | 365 |
2017 | OLD SOUTH OIL LLC | 377.00 | 0.00 | 365 |
2018 | OLD SOUTH OIL LLC | 62.00 | 0.00 | 365 |
Period | Operator Name | Waste Type | Quantity (bbl) | Production Days |
---|---|---|---|---|
1988 | JOHNSON DWIGHT | Brine | 60 | 184 |
1990 | JOHNSON DWIGHT | Brine | 0 | 84 |
1992 | JOHNSON DWIGHT | Brine | 0 | 70 |
1993 | CGAS EXPLORATION | Brine | 91 | 366 |
1994 | CGAS EXPLORATION | Brine | 72 | 365 |
1995 | CGAS EXPLORATION | Brine | 108 | 365 |
1996 | CGAS EXPLORATION | Brine | 0 | 365 |
1997 | CGAS EXPLORATION | Brine | 0 | 365 |
1998 | BUTCHER ENERGY CORP | Brine | 190 | 365 |
1999 | BUTCHER ENERGY CORP | Brine | 0 | 365 |
2000 | BUTCHER ENERGY CORP | Brine | 155 | 365 |
2001 | BUTCHER ENERGY CORP | Brine | 0 | 365 |
2002 | CHAMBERLAIN dba/OLD SOUTH OIL | Brine | 0 | 365 |
2003 | CHAMBERLAIN dba/OLD SOUTH OIL | Brine | 0 | 365 |
2004 | CHAMBERLAIN dba/OLD SOUTH OIL | Brine | 0 | 365 |
2005 | CHAMBERLAIN dba/OLD SOUTH OIL | Brine | 0 | 365 |
2006 | CHAMBERLAIN dba/OLD SOUTH OIL | Brine | 0 | 365 |
2007 | CHAMBERLAIN dba/OLD SOUTH OIL | Brine | 0 | 365 |
2008 | OLD SOUTH OIL LLC | Brine | 0 | 183 |
2009 | OLD SOUTH OIL LLC | Brine | 0 | 365 |
2010 | OLD SOUTH OIL LLC | Brine | 0 | 365 |
2011 | OLD SOUTH OIL LLC | Brine | 0 | |
2012 | OLD SOUTH OIL LLC | Brine | 0 | 366 |
2013 | OLD SOUTH OIL LLC | Brine | 0 | 0 |
2014 | OLD SOUTH OIL LLC | Brine | 145 | 365 |
2015 | OLD SOUTH OIL LLC | Brine | 0 | 0 |
2016 | OLD SOUTH OIL LLC | Brine | 0 | 365 |
2017 | OLD SOUTH OIL LLC | Brine | 0 | 365 |
2018 | OLD SOUTH OIL LLC | Brine | 0 | 365 |
Inspection ID | Inspection Date | Inspection Type | Inspection Result | Inspection Comments |
---|---|---|---|---|
-1360354152 | 2014-2-12 0:00: | AM | No Violations | 0.40 |
-1940253168 | 2014-2-7 0:00:0 | AM | No Violations | 0.30 |
-480616986 | 2014-3-17 0:00: | AM | No Violations | |
-818604850 | 2014-4-23 0:00: | PW | No Violations | 1.50 |
0158052344 | 2007-03-06 | Production Wells | No Violations | There was no tank. There were no violations at the time of inspection. |
0466060519 | 2014-04-03 | Production Wells | No Violations | Follow up to 1377707393. The plunger lift system has been removed from the wellhead. The lines have been disconnected and all the valves are closed. The chart in the meter box does not show any production. There is gas pressure on the annular spaces between the surface casing and the production casing as well as between the tubing and the production casing. |
0480616986 | 2014-03-17 | Administrative Inspection | No Violations | Spoke with Jack Chamberlin of Old South Oil, explained to Mr. Chambering the extension granted until May 1st has been revoked and work needed to be completed by April 1st, 2014. Well need to be placed into production or plugged. Mr. Chamberlin stated he would try to have a rig out to service well by deadline. |
0818604850 | 2014-04-23 | Production Wells | No Violations | Follow up to 1377707393. Well equipped with a plunger lift system, valves on tubing open. 2 line connected to tank battery. Pictures taken. |
1360354152 | 2014-02-12 | Administrative Inspection | No Violations | I spoke with the landowners legal council, Craig Wilson. I notified Mr. Wilson I was in contact with the producer and he was moving forward with relieving the violation associated with this well. |
1377707393 | 2013-08-27 | Production Wells | Violations Noted | Well equipped with a plunger lift system, the valves on the tubing were closed. Tank battery is 100 barrel steel tank, separator, and a meter box with a new chart. Company has reported less than the minimum production standards for the last two years. Well shall be produced in 60 days or plugged in 120 days. |
1399402338 | 2014-05-06 | Salt Water Injection Well | No Violations | Witnessed a reconditioned T607 Team Oil Tools Patriot Packer set in well on 1782 feet of 2 3/8 upset tubing. Packer set at 2200 lbs and then the tubing was unseated from the packer. 18.06 Barrels of fresh water mixed with roughly 5 gallons of corrosion inhibitor was circulated through the annulus to the surface. Then the tubing was stung into the packer and a pressure test was administered. The annular space held 500 psi for the required 15 minutes with an acceptable decrease in pressure at the well head. |
158052344 | 2007-3-6 0:00:0 | PW | No Violations | |
1886860959 | 2013-11-08 | Production Wells | No Violations | Follow up to 1377707393. Well equipped with rabbit unit with a timer. Valve on tubing closed. |
1940253168 | 2014-02-07 | Administrative Inspection | No Violations | Follow up to 1377707393. I spoke with Jack Chamberlain in the field and we discussed the status of the well. A rig was brought onto site two years ago and the tubing was swabbed. The tubing has since loaded with water. The well is connected and an other service rig will be brought onto site next April to swab the well and bring it back into service. |
466060519 | 2014-4-3 0:00:0 | PW | No Violations | 0.80 |
Inspection ID | Violation ID | Violation Date | Violation Code | Violation Comments |
---|---|---|---|---|
1377707393 | US-OH-111200 | 2015-01-08 | Well shall be plugged | |
1377707393 | US-OH-111201 | 2015-01-08 | Nonproduction; well shall be plugged or placed in temporary inactive status |
For data sources see[9]