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Well ID: 34-009-22123 | Loading map...
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Country: United States | |
State: Ohio | |
County: Athens | |
Municipality: Rome Township | |
Operator Name: ODOT-PR | |
Well Pad ID: | |
Farm/Lease Name: HUBBARD JEAN S | |
License Status: Final Restoration | |
License Date: 2016-04-22 | |
Spud Date: 1981-02-12 | |
Spud Drilling Contractor: | |
Final Drill Date: 1981-02-15 | |
Well Total Depth: 1582.00 ft | |
Configuration: Vertical | |
Latitude: 39.290000 | |
Longitude: -81.930000 |
For data sources see[1]
Well Status | Well Status Date | Comment |
---|---|---|
CO | 1980-12-01 | 45 G W F CORPORATION GeoDate 12/1/80 |
Oil and Gas | 1980-12-01 | Issued Date 12/1/80 Expired Date Acres 0010000 Tool Type RTF Proposed Formation BEREA Proposed Depth 00000 Proposed Drill Depth 00000 |
Original Spud | 1981-02-12 | ODOT acquired this well as well as 2338,3347,2512,2146, during the widening of SR 50. Wells transferred to ODOT 2-14-05.See ODOT file for documentation. UPDATED SURFACE LOCATION PER SURVEYORS COORDINATES 11/9/16 ALE. |
Completed | 1981-02-15 | ODOT acquired this well as well as 2338,3347,2512,2146, during the widening of SR 50. Wells transferred to ODOT 2-14-05.See ODOT file for documentation. UPDATED SURFACE LOCATION PER SURVEYORS COORDINATES 11/9/16 ALE. |
Reached Total Depth | 1981-02-15 | ODOT acquired this well as well as 2338,3347,2512,2146, during the widening of SR 50. Wells transferred to ODOT 2-14-05.See ODOT file for documentation. UPDATED SURFACE LOCATION PER SURVEYORS COORDINATES 11/9/16 ALE. |
CO | 1994-08-17 | 4350 CENTURY WELL SERVICE GeoDate 12/1/80 ODOT acquired this well as well as 2338,3347,2512,2146, during the widening of SR 50. Wells transferred to ODOT 2-14-05.See ODOT file for documentation. |
Change of Owner | 2005-02-14 | Operator changed from 4350, CENTURY WELL SERVICE to 2472, ODOT DISTRICT 5/HITCHENS |
APP | 2016-04-22 | Proposed Formations: BEREA, Issued Date:4/22/2016, Expired Date:4/22/2018 12:00:00 PM, Drilling unit acres:74.67, Proposed Well Type:HAD, Proposed Well Class: |
Plugged/Abandoned | 2016-05-26 | ODOT acquired this well as well as 2338,3347,2512,2146, during the widening of SR 50. Wells transferred to ODOT 2-14-05.See ODOT file for documentation. UPDATED SURFACE LOCATION PER SURVEYORS COORDINATES 11/9/16 ALE. |
Record Last Modified | 2017-06-20 | ODOT acquired this well as well as 2338,3347,2512,2146, during the widening of SR 50. Wells transferred to ODOT 2-14-05.See ODOT file for documentation. UPDATED SURFACE LOCATION PER SURVEYORS COORDINATES 11/9/16 ALE. |
Construction Permit Expires | 2018-04-22 | ODOT acquired this well as well as 2338,3347,2512,2146, during the widening of SR 50. Wells transferred to ODOT 2-14-05.See ODOT file for documentation. UPDATED SURFACE LOCATION PER SURVEYORS COORDINATES 11/9/16 ALE. |
For data sources see[2]
Perforation Date | Interval Top (ft) | Interval Base (ft) | Number of Shots |
---|---|---|---|
2006-09-11 | 1446 | 1456 | 0 |
1446 | 1456 | 0 | |
1446 | 1456 | 0 |
For data sources see[3]
Stimulation Date | Chemical Agent | Chemical Agent Concentration (%) | Fracking Fluid Volume | Mass of Proppant Used (lb) | Fracking Company | Comments |
---|---|---|---|---|---|---|
H2O | 0 | 36000 Gal | 30000 |
For data sources see[4]
Period | Operator Name | Gas Quantity (mcf) | Oil Quantity (bbl) | Production Days |
---|---|---|---|---|
1986 | G W F CORPORATION | 3939.00 | 0.00 | 350 |
1987 | G W F CORPORATION | 4230.00 | 0.00 | 350 |
1988 | G W F CORPORATION | 2882.00 | 0.00 | 365 |
1989 | G W F CORPORATION | 6711.00 | 0.00 | 365 |
1990 | G W F CORPORATION | 3402.00 | 0.00 | 365 |
1994 | CENTURY WELL SERVICE | 2013.00 | 0.00 | 365 |
1995 | CENTURY WELL SERVICE | 4601.00 | 0.00 | 365 |
1996 | CENTURY WELL SERVICE | 4094.00 | 0.00 | 365 |
1997 | CENTURY WELL SERVICE | 2074.00 | 0.00 | 365 |
Period | Operator Name | Waste Type | Quantity (bbl) | Production Days |
---|---|---|---|---|
1986 | G W F CORPORATION | Brine | 862 | 350 |
1987 | G W F CORPORATION | Brine | 873 | 350 |
1988 | G W F CORPORATION | Brine | 805 | 365 |
1989 | G W F CORPORATION | Brine | 600 | 365 |
1990 | G W F CORPORATION | Brine | 610 | 365 |
1994 | CENTURY WELL SERVICE | Brine | 0 | 365 |
1995 | CENTURY WELL SERVICE | Brine | 40 | 365 |
1996 | CENTURY WELL SERVICE | Brine | 0 | 365 |
1997 | CENTURY WELL SERVICE | Brine | 220 | 365 |
Inspection ID | Inspection Date | Inspection Type | Inspection Result | Inspection Comments |
---|---|---|---|---|
-1270272622 | 2015-9-11 0:00: | PW | No Violations | 0.50 |
-1332773201 | 2016-1-21 0:00: | PW | No Violations | 0.20 |
-1343105690 | 2016-5-26 0:00: | PB | No Violations | 10.50 |
-1832165456 | 2015-7-8 0:00:0 | PW | No Violations | 1.00 |
-1942163273 | 2016-11-7 0:00: | FR | No Violations | 1.00 |
-2116719125 | 2013-3-19 0:00: | PW | No Violations | 0.20 |
-441701570 | 2003-3-17 0:00: | PW | No Violations | |
001269i421 | 2001-10-04 | Annular Disposal | No Violations | Follow - up on NOV , Non - Complaiance. Well is idle and not producing. |
0022372602 | 2001-06-06 | Production Wells | No Violations | An inspection of the well revealed that the well is still incapable of producing, no action has been taken to plug or produce this well. |
0099230451 | 2016-03-07 | Production Wells | No Violations | Found this well since Todd altier would accompany me to well tomorrow. This well is very hard to find it is in the middle of a group of trees. Well is just 4 with swedge and valve. Well is idle. |
0441701570 | 2003-03-17 | Production Wells | No Violations | Follow-up on NOV, Non-Compliance, well still idle, company has not plugged or produced well. |
0454800888 | 2013-10-25 | Production Wells | No Violations | Asked to take photos by Supervisor. |
1065134382 | 2015-02-18 | Production Wells | No Violations | Follow up to 1334260042. Well appears idle. |
1263400487 | 2010-01-12 | Production Wells | No Violations | Inspection with Supervisor Stonerock this day found casing with 4 x 2 swedge, shut in - not tied to any sales line. Well needs plugged. |
1269i421 | 2001-10-4 0:00: | AD | No Violations | |
1270272622 | 2015-09-11 | Production Wells | No Violations | Met with operator to discuss plugging well for the Department of Transportation. |
1332773201 | 2016-01-21 | Production Wells | No Violations | Review of well with Matt Fulk. |
1334260042 | 2012-04-12 | Production Wells | Violations Noted | Well was not equipped with an identification tag. All producing leases shall be legibly identified in a conspicuous place on or near the well-head or the storage tank as to owner, lease name, well number, permit number where available, county, and an emergency telephone number. The production string was on hangers and the surface casing was not visible. Well equipped with a 4 to 2 reducer and a closed 2 ball valve. There were no lines at the well. No production has been reported since 1997. Well shall be plugged, or placed in temporary inactive status. |
1343105690 | 2016-05-26 | Plug / Plug Back | No Violations | Witnessed the pipe ran into the hole to 1585. Set bottom plug then pulled tubing to 900 and set another 300 plug that would be about the top of the cement on the back side of the 4.5 casing. Bond log showed the casing was bonded at 195 and below. There was a collar at 200 pipe was shot off. The plug was set through the 4.5 inch casing. Pipe was pulled and hole was topped off with 25 sacks of cement. |
1832165456 | 2015-07-08 | Production Wells | No Violations | I met with a potential contractor for ODOT to discuss plugging regulations and state requirements as they apply to site construction. |
1935568050 | 2016-12-12 | Administrative Inspection | No Violations | This well was plugged and final restoration was passed, clearing all previous violations. |
1942163273 | 2016-11-07 | Final Restoration | No Violations | Met Rob Lowe with the surveyors and went to the ODOT wells that were plugged. We found the casing and Rob took coordinates of the well. Grass was established and location meet 1509.72. |
2116719125 | 2013-03-19 | Production Wells | No Violations | Follow up to 1334260042. 4 1/2 production casing on hangers and equipped with a swedge fitting that reduces to a 2 closed ball valve. There is a bull plug in the valve. A small amount of gas was leaking from the threads around the swedge on the production casing. No identification, no lines, no tanks. |
22372602 | 2001-6-6 0:00:0 | PW | No Violations | |
454800888 | 2013-10-25 0:00 | PW | No Violations | 0.20 |
99230451 | 2016-3-7 0:00:0 | PW | No Violations | 2.00 |
Inspection ID | Violation ID | Violation Date | Violation Code | Violation Comments |
---|---|---|---|---|
1334260042 | US-OH-109609 | 2012-08-24 | Failure to legibly identify well | |
1334260042 | US-OH-109610 | 2012-08-24 | Nonproduction; well shall be plugged or placed in temporary inactive status | |
1334260042 | US-OH-109611 | 2012-08-24 | Statement of annual production not filed |
For data sources see[9]