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34-009-23034

Well Details

Well ID: 34-009-23034
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Country: United States
State: Ohio
County: Athens
Municipality: Trimble Township
Operator Name: LUOIL INC
Well Pad ID:
Farm/Lease Name: DRYDOCK COAL CO
License Status: Producing
License Date: 1984-03-14
Spud Date: 1984-04-09
Spud Drilling Contractor: CO TOOLS
Final Drill Date: 1984-04-12
Well Total Depth: 1175.00 ft
Configuration: Vertical
Latitude: 39.540000
Longitude: -82.100000

For data sources see[1]

Well History

Well Status Well Status Date Comment
Oil and Gas 1984-03-14 Issued Date 3/14/84 Expired Date 9/10/84 Acres 0330980 Tool Type RTA Proposed Formation BEREA Proposed Depth 01175 Proposed Drill Depth 01175
Original Spud 1984-04-09
Completed 1984-04-12
Reached Total Depth 1984-04-12
CO 1984-05-07 50 SWINGLE DRILLING INC GeoDate 3/14/84
Completion Report Received 1984-07-03
Construction Permit Expires 1984-09-10
Change of Owner 2006-07-31 Operator changed from 50, SWINGLE DRILLING INC to 8073, LUOIL INC
Last Compliance Report 2015-12-10
Record Last Modified 2017-02-15

For data sources see[2]

Perforation Treatments

Perforation Date Interval Top (ft) Interval Base (ft) Number of Shots
1997-06-29 1088 1106 0
1088 1106 0
2006-09-11 1098 1104 1
1098 1104 1
1088 1106 0

For data sources see[3]

Stimulations Data

Stimulation Date Chemical Agent Chemical Agent Concentration (%) Fracking Fluid Volume Mass of Proppant Used (lb) Fracking Company Comments
H2O 0 44000 Gal 25000 FRAC;H2O,SAND

For data sources see[4]

Production Data

Period Operator Name Gas Quantity (mcf) Oil Quantity (bbl) Production Days
1984 PETROCON INC 0.00 1067.00 365
1985 SWINGLE DRILLING INC 0.00 1222.00 0
1986 SWINGLE DRILLING INC 0.00 828.00 365
1993 SWINGLE DRILLING INC 0.00 226.00 365
1995 SWINGLE DRILLING INC 0.00 228.00 365
2000 SWINGLE DRILLING INC 0.00 67.00 365
2001 SWINGLE DRILLING INC 0.00 157.00 365
2002 SWINGLE DRILLING INC 0.00 226.00 365
2003 SWINGLE DRILLING INC 0.00 76.00 365
2004 SWINGLE DRILLING INC 0.00 84.00 365
2005 SWINGLE DRILLING INC 0.00 77.00 365
2006 SWINGLE DRILLING INC 0.00 0.00 0
2008 LUOIL INC 62.00 60.00 365
2009 LUOIL INC 0.00 41.00 365
2010 LUOIL INC 0.00 51.00 365
2011 LUOIL INC 0.00 50.00 156
2012 LUOIL INC 0.00 244.00 366
2013 LUOIL INC 0.00 133.00 260
2014 LUOIL INC 0.00 115.00 260
2015 LUOIL INC 0.00 80.00 156
2016 LUOIL INC 0.00 45.00 156
2017 LUOIL INC 0.00 70.00 365
2018 LUOIL INC 0.00 69.00 365

For data sources see[5] [6]

Waste Data

Period Operator Name Waste Type Quantity (bbl) Production Days
1984 PETROCON INC Brine 200 365
1985 SWINGLE DRILLING INC Brine 40 0
1986 SWINGLE DRILLING INC Brine 30 365
1993 SWINGLE DRILLING INC Brine 0 365
1995 SWINGLE DRILLING INC Brine 0 365
2000 SWINGLE DRILLING INC Brine 0 365
2001 SWINGLE DRILLING INC Brine 0 365
2002 SWINGLE DRILLING INC Brine 0 365
2003 SWINGLE DRILLING INC Brine 0 365
2004 SWINGLE DRILLING INC Brine 0 365
2005 SWINGLE DRILLING INC Brine 0 365
2006 SWINGLE DRILLING INC Brine 0 0
2008 LUOIL INC Brine 0 365
2009 LUOIL INC Brine 0 365
2010 LUOIL INC Brine 0 365
2011 LUOIL INC Brine 0 156
2012 LUOIL INC Brine 0 366
2013 LUOIL INC Brine 0 260
2014 LUOIL INC Brine 0 260
2015 LUOIL INC Brine 0 156
2016 LUOIL INC Brine 0 156
2017 LUOIL INC Brine 0 365
2018 LUOIL INC Brine 0 365

For data sources see[7] [8]

Inspection Data

Inspections Performed

Inspection ID Inspection Date Inspection Type Inspection Result Inspection Comments
-1198476179 2018-1-31 0:00: PW No Violations 1.50
-1256792074 2018-4-12 0:00: PW No Violations 1.00
-1410372809 2008-12-22 0:00 AD No Violations
-2074925894 2015-12-4 0:00: PW No Violations 1.50
-437284889 2018-1-25 0:00: PW No Violations 2.00
-563720748 2018-8-16 0:00: PW No Violations 0.30
-648581798 2001-5-1 0:00:0 AD No Violations
-873789219 2018-5-11 0:00: PW No Violations 0.30
-920595833 2004-4-6 0:00:0 PW No Violations
0036613366 2003-10-16 Production Wells No Violations FOLLOW UP TO NOV. Well is in compliance.
005609i177 2001-05-01 Annular Disposal Violations Noted An inspection of the well revealed there is No ID at the well head, and ID needs to be placed at well head.
0437284889 2018-01-25 Production Wells Violations Noted Went to the location of a release self-reported by the company. They reported that they lost the bottom of the Drydock tank battery and lost approximately 40 barrels of oil and 3-4 barrels outside the dike. The release happened the afternoon before on the 24th of January. I arrived early on the 25th before the crews were on site. I was accompanied by Inspector Brandon Mitchell. I found the site to be like it was reported the previous evening. The location was left in such a way that the oil was contained and left for cleanup during daylight hours. I spoke to Benny Altier, Todd Altier and met with Bruce Fouts on location. We went over the general plan to achieve the best possible results with the clean-up.
0563720748 2018-08-16 Production Wells No Violations The tank was properly identified. Violation is resolved.
0648581798 2001-05-01 Annular Disposal Violations Noted FOLLOW UP TO NOV # 5609i177 An inspection of the well revealed there is No ID at the well head, and ID needs to be placed at well head.
0873789219 2018-05-11 Production Wells No Violations The pollution and contamination has been cleaned up. I am just waiting for the dike to be built.
0920595833 2004-04-06 Production Wells No Violations No violations at the time of inspection.

Updated well latitude and longitude. Recorded coordinates of the tank battery location.

1198476179 2018-01-31 Production Wells No Violations I went to Altiers shop today and spoke with Todd about the next steps. I explained that if his choice was to bioremediate the soil it would need to be lined and a berm around the outside. I also explained that I would need to know the location and that I would inspect it to make sure it was lined and bermed. I then explained that they would need to try to achieve the 50 foot setback requirements for the new tank they set. If they could only get 45 feet I would approve it if they would set a few more posts parallel with the road. They explained that their goals for today was to get the tank set and the wells back into production today since they have houses connected to the wells for heat.
1256792074 2018-04-12 Production Wells No Violations The dike is still not completely rebuilt. I called Benny Altier who stated, the dike should be completed at the beginning of next week.
1410372809 2008-12-22 Annular Disposal No Violations The well was not equipped for annular disposal.
1532540160 2018-07-25 Production Wells No Violations The dike drain has been installed. The dirt at the location still needs to be brought to a height capable of holding the contents of the tank. There is also no identification posted at the wellhead.
1562760604 2018-01-31 Production Wells No Violations I returned later that day and found that the affected soil was piled into the dike ready for disposal and the free oil outside of the dike was reduced to approximately 30 gallons that was contained with a small earthen dike.
1648544420 2015-10-19 Production Wells Violations Noted No ID was found at the well head or on the old production or drop tank. The lead line going to that tank has the valve closed so it is not currently being used. It appears the well has been serviced within the last few years. An oily mess was found at the well head covering a 5x20 area. There is also a kill zone associated with the referenced oily mess indicative of brine. The mess needs cleaned up around the well and some stone would suffice to cover the area next to the well head. However the area down hill toward the orange pipe and hay bales would need seeded and mulched. ID needs posted at the well head in a manner that is consistent with Ohio Oil and Gas laws and rules. The area at the back of the tank where the lead line, that is not currently being used, was leaking needs cleaned up and contaminated soil removed. Fresh oil was noted on the casing head, the source of the leak, adding to the oily mess around the well head needs corrected.
2074925894 2015-12-04 Production Wells No Violations All NOVs from inspection 1648544420 have been corrected. The tank is still present and will eventually need to be moved. However no other violations noted at the time of this inspection.
36613366 2003-10-16 0:00 PW No Violations
5609i177 2001-5-1 0:00:0 AD No Violations

Violations Commited

Inspection ID Violation ID Violation Date Violation Code Violation Comments
005609i177 US-OH-126211 2001-05-08 Failure to legibly identify well
0437284889 US-OH-124708 2018-08-30 9-1-07 Well operation causing pollution and contamination
0437284889 US-OH-124709 2018-08-30 9-9-05(A)8 Equipment pressure rated below operating pressure
0437284889 US-OH-124710 2018-08-30 9-9-05(A)9 No SPCC dike/or failure to keep dike free of water or oil
0648581798 US-OH-127358 2001-05-08 Failure to legibly identify well
1648544420 US-OH-116256 2016-01-04 Well operation causing pollution and contamination
1648544420 US-OH-116257 2016-01-04 Well insufficiently equipped to prevent escape of oil and gas
1648544420 US-OH-116258 2016-01-04 Failure to legibly identify well

For data sources see[9]

References