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Well ID: 34-009-23545 | Loading map...
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Country: United States | |
State: Ohio | |
County: Athens | |
Municipality: Bern Township | |
Operator Name: ENERVEST OPERATING LLC | |
Well Pad ID: | |
Farm/Lease Name: WOGAN J | |
License Status: Producing | |
License Date: 2018-05-09 | |
Spud Date: 1994-02-03 | |
Spud Drilling Contractor: HIGHLAND DRLG | |
Final Drill Date: 1994-02-08 | |
Well Total Depth: 5045.00 ft | |
Configuration: Vertical | |
Latitude: 39.440000 | |
Longitude: -81.880000 |
For data sources see[1]
Well Status | Well Status Date | Comment |
---|---|---|
CO | 1993-11-24 | 198 VIKING RESOURCES CORP GeoDate 11/24/93 |
Oil and Gas | 1993-11-24 | Issued Date 11/24/93 Expired Date 11/24/94 Acres 0040000 Tool Type RTAF Proposed Formation CLINTON Proposed Depth 05045 Proposed Drill Depth 05045 |
Original Spud | 1994-02-03 | |
Annular Disposal Well | 1994-02-08 | |
Completed | 1994-02-08 | |
Reached Total Depth | 1994-02-08 | |
Completion Report Received | 1994-03-11 | |
Change of Owner | 1998-11-12 | Operator changed from 198, VIKING RESOURCES CORP to 3793, ENERGY SEARCH INC |
Revocation | 1999-03-31 | |
Last Compliance Report | 2005-10-17 | |
Change of Owner | 2008-02-26 | Operator changed from 3793, ENERGY SEARCH INC to 1388, NORTH COAST ENERGY INC |
Change of Owner | 2009-12-14 | Operator changed from 1388, EXCO - NORTH COAST ENERGY INC to 7578, ENERVEST OPERATING LLC |
APP | 2018-05-09 | Proposed Formations:MEDINA SAND, Issued Date:5/9/2018, Expired Date:5/8/2020 12:00:00 PM, Drilling unit acres:40, Proposed Well Type:OG, Proposed Well Class: |
Record Last Modified | 2018-05-16 | |
Construction Permit Expires | 2020-05-08 |
For data sources see[2]
Perforation Date | Interval Top (ft) | Interval Base (ft) | Number of Shots |
---|---|---|---|
1998-01-09 | 4912 | 4918 | 2 |
4912 | 4918 | 2 | |
4912 | 4918 | 2 |
For data sources see[3]
Stimulation Date | Chemical Agent | Chemical Agent Concentration (%) | Fracking Fluid Volume | Mass of Proppant Used (lb) | Fracking Company | Comments |
---|---|---|---|---|---|---|
H2O | 0 | 48460 Gal | 50000 | FRAC W/48,460 GAL H20 & 50M# SAND |
For data sources see[4]
Period | Operator Name | Gas Quantity (mcf) | Oil Quantity (bbl) | Production Days |
---|---|---|---|---|
1994 | VIKING RESOURCES LLC | 34016.00 | 0.00 | 365 |
1995 | VIKING RESOURCES LLC | 35931.00 | 0.00 | 365 |
1996 | VIKING RESOURCES LLC | 29196.00 | 0.00 | 0 |
1997 | VIKING RESOURCES LLC | 14980.00 | 0.00 | 0 |
1998 | VIKING RESOURCES LLC | 3139.00 | 0.00 | 365 |
1999 | ENERGY SEARCH INC | 0.00 | 0.00 | 365 |
2000 | ENERGY SEARCH INC | 0.00 | 0.00 | 365 |
2008 | EXCO - NORTH COAST ENERGY INC | 0.00 | 0.00 | 366 |
2009 | EXCO - NORTH COAST ENERGY INC | 0.00 | 0.00 | 0 |
2010 | ENERVEST OPERATING LLC | 0.00 | 0.00 | 0 |
2011 | ENERVEST OPERATING LLC | 0.00 | 0.00 | 0 |
2012 | ENERVEST OPERATING LLC | 0.00 | 0.00 | 0 |
2013 | ENERVEST OPERATING LLC | 0.00 | 0.00 | 365 |
2014 | ENERVEST OPERATING LLC | 0.00 | 0.00 | 0 |
2015 | ENERVEST OPERATING LLC | 0.00 | 0.00 | 1 |
2016 | ENERVEST OPERATING LLC | 0.00 | 0.00 | 0 |
2017 | ENERVEST OPERATING LLC | 0.00 | 0.00 | 0 |
2018 | ENERVEST OPERATING LLC | 0.00 | 0.00 | 0 |
Period | Operator Name | Waste Type | Quantity (bbl) | Production Days |
---|---|---|---|---|
1994 | VIKING RESOURCES LLC | Brine | 2542 | 365 |
1995 | VIKING RESOURCES LLC | Brine | 633 | 365 |
1996 | VIKING RESOURCES LLC | Brine | 204 | 0 |
1997 | VIKING RESOURCES LLC | Brine | 0 | |
1998 | VIKING RESOURCES LLC | Brine | 0 | 365 |
1999 | ENERGY SEARCH INC | Brine | 0 | 365 |
2000 | ENERGY SEARCH INC | Brine | 365 | |
2008 | EXCO - NORTH COAST ENERGY INC | Brine | 0 | 366 |
2009 | EXCO - NORTH COAST ENERGY INC | Brine | 0 | 0 |
2010 | ENERVEST OPERATING LLC | Brine | 0 | 0 |
2011 | ENERVEST OPERATING LLC | Brine | 0 | |
2012 | ENERVEST OPERATING LLC | Brine | 0 | 0 |
2013 | ENERVEST OPERATING LLC | Brine | 0 | 365 |
2014 | ENERVEST OPERATING LLC | Brine | 0 | 0 |
2015 | ENERVEST OPERATING LLC | Brine | 0 | 1 |
2016 | ENERVEST OPERATING LLC | Brine | 0 | 0 |
2017 | ENERVEST OPERATING LLC | Brine | 0 | 0 |
2018 | ENERVEST OPERATING LLC | Brine | 0 | 0 |
Inspection ID | Inspection Date | Inspection Type | Inspection Result | Inspection Comments |
---|---|---|---|---|
-1087437835 | 2018-1-30 0:00: | PW | No Violations | 1.00 |
-1319452902 | 2018-9-12 0:00: | PW | No Violations | 0.80 |
-1528668751 | 2017-8-11 0:00: | PW | No Violations | 1.50 |
-1554870470 | 2017-8-18 0:00: | PW | No Violations | 2.00 |
-1888134611 | 2005-9-8 0:00:0 | AD | No Violations | |
-1895118757 | 2005-3-1 0:00:0 | PW | No Violations | |
-2075207265 | 2018-3-27 0:00: | PW | No Violations | |
-886618916 | 2020-4-10 0:00: | PW | No Violations | 1.00 |
0000015651 | Preliminary Restoration | No Violations | PASSED Y WITNESSED 11/22/94 INSPECTOR DAN GOINS DATE 11/2219/94 DATA FROM OLD VAX INFO | |
1087437835 | 2018-01-30 | Production Wells | No Violations | Follow-up to inspection 1528668751 on 8/11/17. There were several violations cited in the report. The pollution and contamination has been addressed, the tank was removed so tank spacing and equipment pressure was addressed. The tank was removed and the dike was remediated so the failure to keep dike free and clear of contaminates was addressed. I still have received no plan to plug the well. The tubing was still behind the well and no flow lines were connected. The well is still in violation of 12b however the other violations are as of today cleared. |
1115819277 | Production Wells | No Violations | ||
1142804841 | 2004-01-21 | Annular Disposal | No Violations | Well is not equipped for annular disposal. |
1159238256 | 2017-08-11 | Temporary Abandoned Annular Disposal | No Violations | Annular disposal is not in use. Well is not set up for annular disposal. Well is idle and incapable of production. |
1319452902 | 2018-09-12 | Production Wells | No Violations | I have received a plugging permit in the mail. I emailed Tim McConaha to ask what the plan was for this well. The well was found in the same state as last reported. |
1350554162 | 2018-07-19 | Production Wells | No Violations | I received the permit to plug the well a couple months back. The well is still not capable of production. The well is shut in with a bull plug and the valve is in the closed position. I called Tim McConoughey with Enervest and left a message. The well was originally written up for 12B. |
1528668751 | 2017-08-11 | Production Wells | Violations Noted | Inspection of this well revealed a swage nipple, valve reduced to 2 and a bull plug. A string on 1.5 inch tubing was laid out behind the well. The tank was correctly identified and was leaking. There were several 100 pound propane tanks laying around the dike. The dike was contaminated with an oily substance. The environmental contamination shall be properly remediated. The source of the contamination shall be dealt with in such a way as to prevent further contamination and releases. This well shall be plugged. |
1554870470 | 2017-08-18 | Production Wells | No Violations | Checked on status of cleanup. The dike was filled with rain water today. It did look as if someone had driven a four wheeler back to the location in the last week. It did not appear that clean up had begun. |
15651 | PL | No Violations | ||
1888134611 | 2005-09-08 | Annular Disposal | No Violations | Well is not equipped for annular disposal. |
1895118757 | 2005-03-01 | Production Wells | No Violations | The well was found disconnected and incapable of production. The well was equipped with a 2 to 4 1/2 inch swage and valve. Apparently, a pump jack was removed from the well. |
2075207265 | 2018-03-27 | Production Wells | No Violations | Follow-up to inspection 1528668751 on 8/11/17. There were several violations cited in the report. The pollution and contamination has been addressed, the tank was removed so tank spacing and equipment pressure was addressed. The tank was removed and the dike was remediated so the failure to keep dike free and clear of contaminates was addressed. I still have received no plan to plug the well. The tubing was still behind the well and no flow lines were connected. The well is still in violation of 12b. I contacted the company and they said they would get started on the plugging permit paperwork. |
Inspection ID | Violation ID | Violation Date | Violation Code | Violation Comments |
---|---|---|---|---|
1528668751 | US-OH-114640 | 2017-08-21 | 9-1-07 | Well operation causing pollution and contamination |
1528668751 | US-OH-114641 | 2017-08-21 | 9-9-05(A)2 | Violation of tank spacing requirements |
1528668751 | US-OH-114642 | 2017-08-21 | 9-9-05(A)8 | Equipment pressure rated below operating pressure |
1528668751 | US-OH-114643 | 2017-08-21 | 9-9-05(A)9 | No SPCC dike/or failure to keep dike free of water or oil |
1528668751 | US-OH-114644 | 2017-08-21 | NONE | Well shall be plugged |
For data sources see[9]