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Well ID: 34-013-20350 | Loading map...
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Country: United States | |
State: Ohio | |
County: Belmont | |
Municipality: Somerset Township | |
Operator Name: NORTHWOOD ENERGY CORP | |
Well Pad ID: | |
Farm/Lease Name: DOUDNA | |
License Status: Final Restoration | |
License Date: 2016-02-29 | |
Spud Date: 1981-03-16 | |
Spud Drilling Contractor: | |
Final Drill Date: 1981-03-21 | |
Well Total Depth: 3750.00 ft | |
Configuration: Vertical | |
Latitude: 39.940000 | |
Longitude: -81.150000 |
For data sources see[1]
Well Status | Well Status Date | Comment |
---|---|---|
CO | 1980-09-30 | 1902 DUCK CREEK ENERGY INC GeoDate 9/30/80 |
Oil and Gas | 1980-09-30 | Issued Date 9/30/80 Expired Date Acres 0020000 Tool Type RTA Proposed Formation OHIO SHALE Proposed Depth 03750 Proposed Drill Depth 03750 |
Original Spud | 1981-03-16 | |
Completed | 1981-03-21 | |
Reached Total Depth | 1981-03-21 | |
Completion Report Received | 1981-04-27 | |
CO | 1986-06-09 | 1902 DUCK CREEK ENERGY INC GeoDate 6/9/86 |
Unknown | 1986-06-09 | Issued Date 6/9/86 Expired Date 6/9/87 Proposed Purpose OG Was Plug Supervised Who Superivsed Plug and Abandon Date |
CO | 1997-03-04 | 24 ROCANVILLE CORPORATION GeoDate 6/9/86 |
Change of Owner | 2003-06-24 | Operator changed from 24, ROCANVILLE CORPORATION to 4540, PEOPLES PETROLEUM CORP. |
Change of Owner | 2005-10-05 | Operator changed from 4540, PEOPLES PETROLEUM CORP. to 1634, NORTHWOOD ENERGY CORP |
APP | 2015-12-21 | Proposed Formations:OHIO SHALE, Issued Date:12/21/2015, Expired Date:12/20/2017 12:00:00 PM, Drilling unit acres:129, Proposed Well Type:OG, Proposed Well Class: |
APP | 2016-02-29 | Proposed Formations:OHIO SHALE, Issued Date:2/29/2016, Expired Date:2/28/2018 12:00:00 PM, Drilling unit acres:20, Proposed Well Type:OG, Proposed Well Class: |
Plugged/Abandoned | 2016-04-05 | |
Record Last Modified | 2017-02-10 | |
Construction Permit Expires | 2018-02-28 |
For data sources see[2]
Period | Operator Name | Gas Quantity (mcf) | Oil Quantity (bbl) | Production Days |
---|---|---|---|---|
1984 | OBERLE JAMES LTD | 215.00 | 69.00 | 0 |
2003 | PEOPLES PETROLEUM CORP. | 0.00 | 0.00 | 0 |
2004 | WHITED ROGER | 0.00 | 0.00 | 365 |
2005 | NORTHWOOD ENERGY CORP | 0.00 | 0.00 | 0 |
2006 | NORTHWOOD ENERGY CORP | 0.00 | 0.00 | 0 |
2007 | NORTHWOOD ENERGY CORP | 0.00 | 60.00 | 365 |
2008 | NORTHWOOD ENERGY CORP | 0.00 | 25.00 | 365 |
2009 | NORTHWOOD ENERGY CORP | 258.00 | 0.00 | 365 |
2010 | NORTHWOOD ENERGY CORP | 61.00 | 0.00 | 365 |
2011 | NORTHWOOD ENERGY CORP | 64.00 | 0.00 | 0 |
2012 | NORTHWOOD ENERGY CORP | 78.00 | 40.00 | 366 |
2013 | NORTHWOOD ENERGY CORP | 29.00 | 0.00 | 365 |
2014 | NORTHWOOD ENERGY CORP | 24.00 | 0.00 | 365 |
2015 | NORTHWOOD ENERGY CORP | 0.00 | 5.00 | 365 |
2016 | NORTHWOOD ENERGY CORP | 0.00 | 0.00 | 0 |
Period | Operator Name | Waste Type | Quantity (bbl) | Production Days |
---|---|---|---|---|
1984 | OBERLE JAMES LTD | Brine | 0 | 0 |
2003 | PEOPLES PETROLEUM CORP. | Brine | 0 | 0 |
2004 | PEOPLES PETROLEUM CORP. | Brine | 0 | 0 |
2005 | NORTHWOOD ENERGY CORP | Brine | 0 | 0 |
2006 | NORTHWOOD ENERGY CORP | Brine | 0 | 0 |
2007 | NORTHWOOD ENERGY CORP | Brine | 80 | 365 |
2008 | NORTHWOOD ENERGY CORP | Brine | 100 | 365 |
2009 | NORTHWOOD ENERGY CORP | Brine | 33 | 365 |
2010 | NORTHWOOD ENERGY CORP | Brine | 53 | 365 |
2011 | NORTHWOOD ENERGY CORP | Brine | 70 | |
2012 | NORTHWOOD ENERGY CORP | Brine | 63 | 366 |
2013 | NORTHWOOD ENERGY CORP | Brine | 62 | 365 |
2014 | NORTHWOOD ENERGY CORP | Brine | 0 | 365 |
2015 | NORTHWOOD ENERGY CORP | Brine | 73 | 365 |
2016 | NORTHWOOD ENERGY CORP | Brine | 193 | 0 |
Inspection ID | Inspection Date | Inspection Type | Inspection Result | Inspection Comments |
---|---|---|---|---|
-1157452944 | 2015-7-10 0:00: | PW | No Violations | |
-1182495915 | 2015-4-3 0:00:0 | PW | No Violations | 0.50 |
-1250246777 | 2016-10-11 0:00 | FR | No Violations | 1.00 |
-1341011457 | 2016-3-22 0:00: | PB | No Violations | 5.00 |
-1574259396 | 2015-9-25 0:00: | PW | No Violations | 0.50 |
-1648698382 | 2015-4-24 0:00: | PW | No Violations | 0.50 |
-1683917453 | 2012-12-5 0:00: | PW | No Violations | 0.50 |
-1878362740 | 2016-4-4 0:00:0 | PB | No Violations | 5.00 |
-2089425707 | 2016-3-15 0:00: | PB | No Violations | 5.50 |
-425909267 | 2013-4-4 0:00:0 | PW | No Violations | 0.50 |
-745498766 | 2016-3-16 0:00: | PB | No Violations | 7.00 |
-890439715 | 2016-3-29 0:00: | PB | No Violations | 3.50 |
0005604i55 | 2002-01-29 | Production Wells | No Violations | |
0425909267 | 2013-04-04 | Production Wells | No Violations | On the day of my inspection the well was equipped with a pumping unit and was capable of production. The tank battery contents included: one 100 bbl oil storage tank and one mechanical separator. No violations were noted. |
0446988120 | 2014-09-24 | Production Wells | No Violations | Onsite with Inspector Andrew Corder. Site contents include 100 bbl oil tank, a mechanical seperator, and a pumping unit on the wellhead. Well has all the required equipment to produce. |
0563640861 | 2014-09-24 | Production Wells | No Violations | On the day of my inspection the well had a pumping unit and all equipment to be capable of production. The tank battery contents included a 100 bbl oil storage tank and a separator. No violations noted. |
0577237614 | 2016-03-17 | Plug / Plug Back | No Violations | On site along with county inspector to discuss options concerning plugging of said well, Davis Well Service currently is washing 2.875 tubing over 1.5 tubing it was stuck in hole and they are currently at 3200 and they are having trouble with power swivel and they hope to be back in operation tomorrow. |
0626917790 | 2016-03-28 | Plug / Plug Back | No Violations | I attemped to contact Glen Davis and Earl Barnes with no success. I visited the site to get updated on the progress of this plugging operation and there was no activity taking place. |
0685957219 | 2015-02-11 | Production Wells | Violations Noted | I received an email from Gene Chini of the Orphan Well Program. He had received a call from Greg Martin alleging that the well does not produce enough products to meet the requirements of the Ohio Revised Code. The well is equipped with the necessary equipment to be capable of production. The tank battery contents include: one 100 bbl oil storage tank and one mechanical separator. This well has produced domestic gas in the past but the landowner claims it is not currently supplying gas. RBDMS records of production demonstrate that this well does not produce enough oil, gas, or combination thereof to meet the State regulation. Company shall plug this well within 180 days. |
0745498766 | 2016-03-16 | Plug / Plug Back | No Violations | On this day the operator had tripped back to bottom with the 2.875 tubing. They have lost ground and tagged up above the point they had washed to the previous day. This indicates the possibility of a hole in the 4.5 casing up hole casing debris to fall onto the backside of the 1.5 tubing. Washing operators continued today with about 8 of progress. Operator will continue washing operations tomorrow. |
0890439715 | 2016-03-29 | Plug / Plug Back | No Violations | On this day the operator tripped 2.875 tubing back into the hole with an overshot tool. Once on the 1.5 tubing the operator pulled to try and recover the tubing. After several attempts the 1.5 parted. The operator pulled 3 joints and tripping operations will continue tomorrow. |
0913814174 | 2016-03-11 | Plug / Plug Back | No Violations | On this day the company was attempting to wash 2.875 tubing down to free the 1.5 tubing so that it may be recovered prior to plugging operations commencing. |
0934355334 | 2016-03-08 | Plug / Plug Back | No Violations | |
0989530891 | 2016-03-17 | Plug / Plug Back | No Violations | On this day the operator had tripped back to bottom with the 2.875 tubing. They tagged up at approximately the same depth they had reached in the previous day. Washing operations had success today and they were making progress. Toward the end of the day the swivel had broken down. The operator is working to remedy the mechanical issues. Once they the swivel is fixed the washing operations will resume. |
1060555939 | 2016-03-23 | Plug / Plug Back | No Violations | On site with county inspector to discuss upcoming plugging operation. |
1126724469 | 2005-09-14 | Production Wells | No Violations | C/O TO ROGER WHITED. NO PRODUCTION FILED SINCE 2003. CAPABLE OF PRODUCTION. |
1157452944 | 2015-07-10 | Production Wells | No Violations | Email sent to Bill Arnholt. This is a reminder of the Compliance Notice that I issued. This issue needs to be addressed. I will not grant an extension on this Notice. |
1182495915 | 2015-04-03 | Production Wells | No Violations | An email was sent to Bill Arnholt of Northwood Energy. The email was to address questions that Bill had asked. I informed him that he needed to address the issue of insufficient production and he questioned if the oil in the tank was shipped and met State requirements would the Compliance be cleared. I told him to submit the documentation to me and I would clear the notice. I also reminded him this action needed to take place by 08/11/2015 |
1250246777 | 2016-10-11 | Final Restoration | No Violations | This site has been restored and has passed final restoration. |
1341011457 | 2016-03-22 | Plug / Plug Back | No Violations | The operator has repaired the swivel and washing operators have commenced again. |
1452608765 | 2016-03-10 | Plug / Plug Back | No Violations | |
1457953271 | 2016-03-09 | Plug / Plug Back | No Violations | On this day the Davis Wells service rig was moved onto location. The planned operations were to pull the rods from the well and determine how to proceed with plugging operations. Rod retrieval operations were unsuccessful and it was determined that a stripping job would have to be performed. |
1458588170 | 2016-03-21 | Plug / Plug Back | No Violations | On this day the operator was attempting to fix the swivel unit. It was determined that bearings were needed and the unit was taken to the shop for repairs. |
1459257536 | 2016-03-29 | Plug / Plug Back | No Violations | The operator had to get new slips because the ones they had were non operational. Fishing operations for the 1.5 tubing are to start back up today. |
1459775311 | 2016-03-31 | Plug / Plug Back | No Violations | On this day the operator attemped to drill and wash around the 1.5 tubing to free it from the hole. Operations were not successful and it was determined that the bottom hole plug will be set from 3150 to 2400. |
1459950999 | 2016-04-01 | Plug / Plug Back | No Violations | On this day the cementing process of the plugging operations commenced. Cemenco was on site and set the bottom hole plug from 3150-2305 using Class A cement. The cement was set through the 2.875 tubing. Cement procedures utilized 65 sacks of Class A cement and 13.4 barrels of water to displace the cement plug to the proper depth. |
1574259396 | 2015-09-25 | Production Wells | No Violations | On the day of my inspection the well was equipped with a pumping unit and appeared to have all equipment to be considered capable of production. The valves coming from the well head were in the off position. The tank battery contents include: one 100 bbl oil storage tank and one mechanical separator. Due to the proper equipment and reported production this well will not be required to be plugged. The Compliance Notice for this well is now resolved. See inspection 685957219 for resolved notice. |
1576277387 | 2015-05-22 | Production Wells | No Violations | Email sent to Bill Arnholt. Just another reminder of this Compliance Notice. This notice must be addressed before 08/11/2015. No extension will be granted. |
1584558493 | 2016-04-05 | Plug / Plug Back | No Violations
--550-- | |
1628245077 | 2015-08-11 | Production Wells | No Violations | On the day of my inspection the well was equipped to be capable of production. The valve off of the well head leading to the tank battery appeared to be in the closed position. The valves in the tank battery leading to the sales and separation tank appeared to be closed as well. The chart on the metering system appeared to represent no activity. I have made attempts to contact the operator to remedy this compliance notice for the last 6 months with no progress. Photos were taken on the day of the inspection. The landowner, Greg Martin, was present and he inquired about further actions. |
1648698382 | 2015-04-24 | Production Wells | No Violations | Email sent to Bill Arnholt of Northwood Energy. Just another reminder of this Compliance Notice. |
1683917453 | 2012-12-05 | Production Wells | No Violations | On the day of my inspection the well was equipped with a pumping unit and was capable of production. The tank battery contents included: one 100 bbl oil storage tank and one mechanical separator. No violations were noted. |
1731149004 | 2016-03-30 | Plug / Plug Back | No Violations | On this day the 2.875 tubing was tripped from the hole to see if any 1.5 tubing was retrieved. The 1.5 tubing was tallied and the operator was able to recover 1.5 down to 3150. Planned operations are to try and wash down over the 1.5 tubing again to free it from the hole. |
1878362740 | 2016-04-04 | Plug / Plug Back | No Violations
- | |
2089425707 | 2016-03-15 | Plug / Plug Back | No Violations | On this day the operator was attempting to use a tooth bit and fluid to wash down around the 1.5 tubing to free it from the hole. The operator is having little success in washing the debris out from the hole around the 1.5 tubing. The operator will continue to wash in attempt to free the tubing. |
446988120 | 2014-9-24 0:00: | PW | No Violations | 1.00 |
5604i55 | 2002-1-29 0:00: | PW | No Violations | |
563640861 | 2014-9-24 0:00: | PW | No Violations | 1.00 |
577237614 | 2016-3-17 0:00: | PB | No Violations | |
626917790 | 2016-3-28 0:00: | PB | No Violations | 1.50 |
685957219 | 2015-2-11 0:00: | PW | No Violations | 0.50 |
913814174 | 2016-3-11 0:00: | PB | No Violations | 2.00 |
934355334 | 2016-3-8 0:00:0 | PB | No Violations | 0.50 |
989530891 | 2016-3-17 0:00: | PB | No Violations | 8.00 |
Inspection ID | Violation ID | Violation Date | Violation Code | Violation Comments |
---|---|---|---|---|
0685957219 | US-OH-127759 | 2015-11-10 | Well shall be plugged |
For data sources see[7]