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Well ID: 34-013-20609 | Loading map...
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Country: United States | |
State: Ohio | |
County: Belmont | |
Municipality: Warren Township | |
Operator Name: FORCE ENVIRONMENTAL SOLUTIONS | |
Well Pad ID: | |
Farm/Lease Name: BUCKEYE UIC BARNESVILLE(SWIW #2) | |
License Status: Active Injection | |
License Date: 2011-12-01 | |
Spud Date: 2010-07-13 | |
Spud Drilling Contractor: L WILSON DRLG | |
Final Drill Date: 2010-09-02 | |
Well Total Depth: 10394.00 ft | |
Configuration: Vertical | |
Latitude: 40.020000 | |
Longitude: -81.150000 |
For data sources see[1]
Well Status | Well Status Date | Comment |
---|---|---|
APP | 2010-02-26 | Proposed Formations:TRENTON THRU CONASAUGA, Issued Date:2/26/2010, Expired Date:2/26/2011 6:00:00 AM, Drilling unit acres:40.48, Proposed Well Type:OG, Proposed Well Class:EDPW |
APP | 2010-05-28 | Proposed Formations:TRENTON THRU CONASAUGA, Issued Date:5/28/2010, Expired Date:5/28/2011 6:00:00 AM, Drilling unit acres:40.48, Proposed Well Type:OG, Proposed Well Class:EDPW |
Correction to Well | 2010-07-16 | CORRECTION TO PROPOSED TOTAL DEPTH AND CASING PROGRAM |
Reached Total Depth | 2010-09-02 | |
Completion Report Received | 2011-07-25 | |
Last Compliance Report | 2011-10-25 | |
APP | 2011-12-01 | Proposed Formations:COPPER RIDGE "B" ZONE, Issued Date:12/1/2011, Expired Date:11/30/2013 12:00:00 PM, Drilling unit acres:55.43, Proposed Well Type:SWD, Proposed Well Class:SWIW |
First Injection | 2012-06-11 | |
Construction Permit Expires | 2013-11-30 | |
Change of Owner | 2016-07-22 | Operator changed from 8441, CNX GAS COMPANY LLC to 9676, CNX WATER ASSETS LLC |
Record Last Modified | 2017-02-15 |
For data sources see[2]
Perforation Date | Interval Top (ft) | Interval Base (ft) | Number of Shots |
---|---|---|---|
2011-10-03 | 10394 | 10491 | 0 |
10394 | 10491 | 0 | |
10394 | 10491 | 0 |
For data sources see[3]
Stimulation Date | Chemical Agent | Chemical Agent Concentration (%) | Fracking Fluid Volume | Mass of Proppant Used (lb) | Fracking Company | Comments |
---|---|---|---|---|---|---|
ACID | 15 | 4500 Gal | 0 | BD PRESSURE: PUMP 800-1900 |
For data sources see[4]
Inspection ID | Inspection Date | Inspection Type | Inspection Result | Inspection Comments |
---|---|---|---|---|
-1029416995 | 2017-8-22 0:00: | SW | No Violations | 3.50 |
-1080824226 | 2012-3-5 0:00:0 | SW | No Violations | |
-1133218044 | 2014-3-20 0:00: | SW | No Violations | |
-1153772189 | 2017-6-26 0:00: | SW | No Violations | |
-1162343719 | 2013-1-16 0:00: | SW | No Violations | |
-1178263128 | 2014-8-19 0:00: | SW | No Violations | |
-1182533367 | 2011-3-28 0:00: | DD | No Violations | 1.00 |
-1236205293 | 2010-8-12 0:00: | DD | No Violations | 8.00 |
-12674869 | 2010-8-2 0:00:0 | DD | No Violations | 4.00 |
-1275814882 | 2014-3-6 0:00:0 | SW | No Violations | |
-1290935470 | 2016-3-2 0:00:0 | SW | No Violations | |
-1303445723 | 2010-8-19 0:00: | DD | No Violations | 2.00 |
-132218032 | 2010-9-30 0:00: | DD | No Violations | 2.00 |
-133499260 | 2010-8-12 0:00: | DD | No Violations | 3.00 |
-1337069427 | 2012-10-11 0:00 | SW | No Violations | 0.50 |
-136307755 | 2014-5-16 0:00: | SW | No Violations | |
-1368363680 | 2012-8-29 0:00: | SW | No Violations | |
-138643577 | 2015-7-23 0:00: | SW | No Violations | |
-1515817249 | 2013-3-21 0:00: | SW | No Violations | |
-1531334974 | 2012-12-13 0:00 | SW | No Violations | |
-1535072050 | 2010-7-13 0:00: | DD | No Violations | 4.00 |
-153742220 | 2014-10-14 0:00 | SW | No Violations | |
-1553022298 | 2013-9-26 0:00: | SW | No Violations | |
-1581721333 | 2010-8-16 0:00: | DD | No Violations | 4.00 |
-15954706 | 2013-6-13 0:00: | SW | No Violations | 2.00 |
-1688990262 | 2018-6-7 0:00:0 | SW | No Violations | 3.00 |
-1761133136 | 2010-8-13 0:00: | AM | No Violations | |
-1810384094 | 2016-1-14 0:00: | SW | No Violations | |
-1849759703 | 2014-2-19 0:00: | SW | No Violations | |
-1889192932 | 2014-6-17 0:00: | SW | No Violations | |
-1950042564 | 2012-10-11 0:00 | PL | No Violations | 0.50 |
-195503247 | 2013-12-16 0:00 | SW | No Violations | |
-2052380716 | 2013-2-1 0:00:0 | SW | No Violations | |
-209788825 | 2013-8-14 0:00: | SW | No Violations | 2.00 |
-2098124996 | 2015-4-8 0:00:0 | SW | No Violations | |
-2117209081 | 2017-1-4 0:00:0 | SW | No Violations | |
-2144557314 | 2010-8-9 0:00:0 | DD | No Violations | 14.50 |
-310723082 | 2014-4-11 0:00: | SW | No Violations | |
-403427 | 2013-5-1 0:00:0 | PL | No Violations | |
-434066317 | 2013-2-14 0:00: | SW | No Violations | |
-524076082 | 2012-9-19 0:00: | SW | No Violations | |
-53197767 | 2010-6-10 0:00: | SC | No Violations | 1.00 |
-532124869 | 2010-8-30 0:00: | DD | No Violations | 3.00 |
-533661460 | 2015-5-28 0:00: | SW | No Violations | |
-666122243 | 2010-9-2 0:00:0 | DD | No Violations | 4.00 |
-672627116 | 2011-3-28 0:00: | CT | No Violations | 1.00 |
-677648927 | 2019-2-11 0:00: | SW | No Violations | |
-717476768 | 2010-7-15 0:00: | DD | No Violations | 2.50 |
-77662028 | 2018-11-14 0:00 | SW | No Violations | |
-83753873 | 2020-1-30 0:00: | SW | No Violations | |
-84525282 | 2013-7-22 0:00: | SW | No Violations | |
-874108247 | 2016-3-3 0:00:0 | SW | No Violations | |
-938662457 | 2012-7-24 0:00: | SW | No Violations | |
-949230984 | 2012-6-8 0:00:0 | SW | No Violations | |
-95165232 | 2020-1-7 0:00:0 | SW | No Violations | |
-954871804 | 2014-2-19 0:00: | SW | No Violations | 1.50 |
-967784789 | 2020-5-6 0:00:0 | SW | No Violations | 8.00 |
0000403427 | 2013-05-01 | Preliminary Restoration | No Violations | Inspection revealed that injection pump was not in operation during my inspection. |
0012674869 | 2010-08-02 | Drill / Deepen / Reopen | No Violations | On day of inspection well was showing large flares at 8464and at 8474.They were at 1575 units on air.Haliburton Engineer is showing up. They will go to fluid. They plan to mix up 9.1weight and not go over 9.3ppg. |
0015954706 | 2013-06-13 | Salt Water Injection Well | No Violations | Inspected site along with local inspector Andrew Corder to go over guidelines for UIC inspection at SWIW facilities.
Note: Injection pump was not in operation during our inspection and it was noted that annulus pressure on tubing has risen a little since my last inspection. |
0053197767 | 2010-06-10 | Surface Facility Construction | No Violations | Per my conversation with Kevin Smith I stopped to look at the site of the proposed well. The conductor hole will be drilled in a smaller rig at the end of the week. |
0077662028 | 2018-11-14 | Salt Water Injection Well | No Violations | On site today to witness CJ Services perform 4000 gallon acid treatment on well.
28% HCL |
0084525282 | 2013-07-22 | Salt Water Injection Well | No Violations | Injection pump was not operating during my inspection and it was noted that one Force Energy vacuum truck was unloading during my inspection.
Note: Discussed with operator that lease road to well head needs to be maintained so inspector can get to well head to check pressures. |
0098998103 | 2014-04-23 | Salt Water Injection Well | No Violations | Inspection revealed that well is still down waiting on storage tanks to be cleaned out before placing well back into operation. |
0132218032 | 2010-09-30 | Drill / Deepen / Reopen | No Violations | On day of inspection met with OEPA and USEPA on the site. There was a complaint about soap suds down hillside from site. It was biodegradable rig soap. The company provided a set of MSDS sheets for us. Looked at the pit and the problems that were at the site. They were satisfied that the issues were being rectified. |
0133499260 | 2010-08-12 | Drill / Deepen / Reopen | No Violations | Logging truck showed up to log hole. Bond log revealed that cement top is at 2040.We had had sufficient bond. |
0135535475 | 2012-05-24 | Salt Water Injection Well | No Violations | Inspection revealed that facility is nearly complete and within the next couple weeks they should be ready to pressure test lines and plumbing before putting well into operation.
Note: Liner in tank area needs to be covered with stone too help prevent it from deteriorating due to exposure to sunlight. |
0136307755 | 2014-05-16 | Salt Water Injection Well | No Violations | Inspection revealed that injection pump was in operation today and it was noted that one Force Trucking vacuum truck was unloading at facility during my inspection. |
0138643577 | 2015-07-23 | Salt Water Injection Well | No Violations | Inspection revealed that injection pump was not in operation on the day of my inspection and it was noted that rain water has built up in dike area and I told operator to pump water into storage tanks and properly dispose of it downhole/ |
0153742220 | 2014-10-14 | Salt Water Injection Well | No Violations | Inspection revealed that injection pump was not in operation during my inspection.
Note: 500 bbl storage tanks are still up on location waiting on operator to truck material down to storage tanks and then inject it into well. |
0173415178 | 2010-07-09 | Drill / Deepen / Reopen | No Violations | On day of inspection the Les Wilson co. is moving large rig in on location. |
0195503247 | 2013-12-16 | Salt Water Injection Well | No Violations | Inspection revealed that injection pump was in operation today and it was noted that annulus pressure has come up since my last inspection and I discussed this with company rep and he decided they would perform MIT test within the next couple weeks. |
0209788825 | 2013-08-14 | Salt Water Injection Well | No Violations | Inspection revealed that injection pump was in operation during my inspection and it was noted that one Force Energy vacuum truck was unloading at facility during my inspection. |
0310723082 | 2014-04-11 | Salt Water Injection Well | No Violations | Inspection revealed that well is still down waiting on tank cleaning crew to finish cleaning tanks before placing well into operation. |
0346839070 | 2015-05-18 | Salt Water Injection Well | No Violations | On site to witness Basic Well Service set wireline plug inside of packer and pressure test tubing it checked out OK and it was determined that they have packer leakage and decision was made to release packer and pull from well. |
0382928994 | 2017-03-28 | Salt Water Injection Well | No Violations | On site to witness pressure testing of 3flowline we tested it at 3750 psi with no decline in test pressure and while testers were on site applied 250 psi to annulus of injection string. |
0408655377 | 2010-07-26 | Drill / Deepen / Reopen | No Violations | On day of inspection talked with drilling consultant.tri cone bit was installed at 4935. Rig is at 6206.AT 6120switched to soap. The Heidelberg showed 440 units. |
0434066317 | 2013-02-14 | Salt Water Injection Well | No Violations | Inspection revealed that injection pump was in operation and dike area was clear of fresh water build up and unloading pad was clean and pump house was neat and clean. |
0524076082 | 2012-09-19 | Salt Water Injection Well | No Violations | On site to gather water sample to take to lab to be analyzed, inspection revealed that injection pump was not in operation during my inspection and it was noted that three vacuum trucks were unloading at facility during my inspection. |
0532124869 | 2010-08-30 | Drill / Deepen / Reopen | No Violations | On day of inspection stopped in to look at rig. Rig was drilling at depth of 10,318.Checked chlorides at place north and below drill pit. They were at 2700ppm.I also met with mud logger Scott Tyrell. I also met with Chris Miller CNX. |
0533661460 | 2015-05-28 | Salt Water Injection Well | No Violations | Producers Services on site to perform 2000 gallon acid treatment on said well they pumped 2000 gal of 28% acid and displaced it into the formation and they will resume operations on Monday June 1,2015. |
0545529800 | 2015-06-03 | Salt Water Injection Well | No Violations | Inspection revealed that injection pump was in operation and BBU is in the process of cleaning out 500 barrel storage tanks that were used during recent work over project on said well. |
0666122243 | 2010-09-02 | Drill / Deepen / Reopen | No Violations | On day of inspection per phone call from Jay Hewitt of CNX well has been TD at 10,490.They will probably set 26lb/ft 7on formation packer to depth of 10,375.At depth of 10,433there was zone that took fluid at a rate of 100bbl -200bbl/hr.The fluid was at a weight of 10.5-10.7 and at 41visc.The drill pipe was being sucked over to the well bore. They set a gel pill with lcm and pulled drill pipe into the 9 5/8 casing. Topping off as needed. I talked with mud engineer and company man. I talked with TOOL pusher on Les Wilson rig 30. |
0672627116 | 2011-03-28 | Completion Testing | No Violations | On day of inspection pit at bottom is needing sucked down.There is a 10,000psi frac valve installed.Will call company. |
0677648927 | 2019-02-11 | Salt Water Injection Well | No Violations | Inspection today revealed that injection pump was in operation and it was noted that one Force truck was offloading at the facility during my inspection.
|
0707980751 | 2016-11-02 | Salt Water Injection Well | No Violations | On site to witness acid treatment on said well. |
0717476768 | 2010-07-15 | Drill / Deepen / Reopen | No Violations | On day of inspection I stopped in to check the status on the rig. They were drilling on 17.5air hammer. They were at a depth of 1031. They were going to 1800.There will be at every 1000a deviation survey ran to check the drift. The drift can only be 1%.After 4000 there will be a company come in and ran deviation tools. There was a Tim Rinehart with CNX that I spoke with. |
0839215518 | 2011-10-26 | Salt Water Injection Well | No Violations | Inspected site at request of UIC Director, company is applying for conversion of said well to SWIW well walked parameter of lease to check for water wells and waterways there were none found in area of wellhead, company has started construction of tank facility but it is not completed as of this date.
Note: Called and talked to company rep Kevin Smith concerning placing stone in ditch beside of lease road to help prevent erosion that might occur during heavy rainfall. |
0842983716 | 2018-10-24 | Salt Water Injection Well | No Violations | On site today to witness 4000 gallon acid treatment on said well,CJ Services performed treatment |
0874108247 | 2016-03-03 | Salt Water Injection Well | No Violations | Injection pump has been changed out and operator is performing mainietence work at the facility today. |
0885733160 | 2017-07-20 | Salt Water Injection Well | No Violations | Inspection today indicated that injection pump was in operation today and it was noted that slip repair still continues. |
0921717884 | 2016-04-20 | Salt Water Injection Well | No Violations | On site along with UIC Program Administrator to meet with company reps to discuss potential for additional SWIW well and the possibility to use existing pump house for the additional well if drilled. |
0938662457 | 2012-07-24 | Salt Water Injection Well | No Violations | Inspection on this day revealed that well is in operation and several company personnel were on site doing a walk through inspection.
Note: Exposed liner needs to be covered with stone to help prevent decay due from exposure to sunlight. |
0949230984 | 2012-06-08 | Salt Water Injection Well | No Violations | Stopped by site they were paving entire parking area and area around pump house and electrical room ,Mike Jenkins site foreman stated that well should be ready to go online by the end of the month. |
0954871804 | 2014-02-19 | Salt Water Injection Well | No Violations | On the day of my inspection I accompanied Dave Ball and CNX was preparing to run tests to determine cause of well issues. No violations noted. |
0966651421 | 2018-06-07 | Salt Water Injection Well | No Violations | Inspection revealed that CJ Services was on site to perform 2000 gallon 28% acid treatment job on said well and we performed mini pressure test on annulus of injection string today. |
0976701831 | 2015-05-11 | Salt Water Injection Well | No Violations | On site along with company rep to witness annulus testing of tubing Producers Services pressured up too 2450 psi and we monitored pressure for 15 minutes and they loss 200 psi indicating that they have possible tubing leak or packer leakage instructed owner to cease operation and perform further testing on tubing before they get service rig on site to possibly pull packer and tubing from well bore. |
1029416995 | 2017-08-22 | Salt Water Injection Well | No Violations | On site to check on the restoration of the slip that had occurred on this location. The company was taking the dirt that had been stock piled on the location and moving it back to the hill side. The tubing in the well on this day had 1400 pounds of pressure. The annulus contained 5 pounds and the pump was running. |
1066084435 | 2019-02-26 | Salt Water Injection Well | No Violations | Inspection revealed that injection pump was in operation today. |
1080824226 | 2012-03-05 | Salt Water Injection Well | No Violations | Inspection revealed that owner is still working on unloading pad and new building constructed art site they are still waiting on installing flow line too well head instructed them we would need to pressure test line once installed. |
1104872061 | 2010-12-09 | Drill / Deepen / Reopen | No Violations | On day of inspection drill pit has been covered. Pit liner and French drain has been removed. There is no more seepage out of the bank. Compliance Notice has been resolved. |
1133218044 | 2014-03-20 | Salt Water Injection Well | No Violations | Team Service rig on site to release packer and pull tubing, it was noted that packer has been released and they were placing 10# brine in well so it would not flow during packer removal. |
1153772189 | 2017-06-26 | Salt Water Injection Well | No Violations | Inspection today indicated that injection pump was not in operation and slip repair in area below well site has begun they expect to be done within the next thirty days. |
1162343719 | 2013-01-16 | Salt Water Injection Well | No Violations | Inspection revealed that operator was waiting on enough water to be received so he could start injection pump it was noted that Force Well Service had one vacuum truck unloading at facility during my inspection.
Note: Operator stated that well was taking approximately 1400 bbl of brine per day. |
1167795196 | 2017-12-29 | Salt Water Injection Well | No Violations | Inspection revealed that injection pump was in operation during my inspection and it was noted that one 25-675 tanker as unloading at the facility during my inspection. |
1178263128 | 2014-08-19 | Salt Water Injection Well | No Violations | Inspection revealed that injection pump was in operation during my inspection and it was noted that the cage for the wellhead has been put back in place. |
1182533367 | 2011-03-28 | Drill / Deepen / Reopen | No Violations | This well has been drilled and is currently shut in and awaiting completion work. There is 10,000 PSI frac valve on the well head. The earthing pits were found to be in good condition. |
1211769218 | 2012-02-16 | Salt Water Injection Well | No Violations | Inspection revealed that 8-300 bbl tanks and 2-400 bbl tanks and 1-100 bbl tank were set within dike area and pump house and electrical building is under construction will monitor site too make sure contractor follows site plans established for said well. |
1236205293 | 2010-08-12 | Drill / Deepen / Reopen | No Violations | FOLLOW UP TO NOV # 1282048725 On day of inspection I was in on site for a BOP Test. The BOP test could not be completed at present time because of wrong rubber size for the job. The CNX engineer Jay Hewitt notified me on a situation with water leaking out of hill. There were four places. There was a 4flow and two 2flows.There was also a 8plastic corrugated pipe that was used for a french drain between the pit and the west wall of the location. I contacted Supervisor Simmers and Inspector Moravy. They told me to notify Inspector Farnsworth to assist me with this situation. I contacted Inspector Farnsworth and he would be in route ASAP.I started taking samples of the water.WS-1 was taken at the 4stream down over the north end of the pit.WS-2 was taken at the sediment trap.WS-3 was taken at the center of the pit.Quantab readings revealed that the chlorides were 10,000-13,000ppm at WS-1 and WS-2.WS-3 and at site behind rig indicated that the chlorides were higher than that.Baroid employee Titus Robinson took samples also. He indicated that the ground water sample was at a chloride level at 13,000ppm.The pit sample was at a 28,000ppm in chlorides. Jay Hewitt contacted the construction team and advised them that he needed them on site to construct the containment pit down over hill. At this point in time, the source of water is yet to be determined. I contacted Tom Tomastik in Columbus and he advised that there were no wells in area near the CNX site.Delrick construction showed up and started to get prepared to construct the containment pit. Approximately 6:00pm Inspector Farnsworth arrived and Hewitt and I briefed him about the situation. We assessed the pit and the water flowing out of the hillside. There was no visible indication on the pit liner that there was a fluid loss from the drilling pit at this time. Inspection of the drilling pit revealed that pit liner was scorched and melted during the flaring of the Utica gas. We observed that the fluid level was at the l |
1275814882 | 2014-03-06 | Salt Water Injection Well | No Violations | Fishing for lost tools within tubing string. |
1280930825 | 2010-08-04 | Drill / Deepen / Reopen | No Violations | On day of inspection Les Wilson rig running in with pipe and overshot and jars to retrieve the fish. The Total depth is at is at 8474.At 8425 is where the bit is at.1200 bbl was what it should have took to load hole.1500bbl is what was actual. Lost circulation and started pulling drillpipe. Will trip out all pipe out of hole and mud up. |
1281878267 | 2010-08-15 | Drill / Deepen / Reopen | No Violations | At about 9:00am Chris Miller the drilling consultant with CNX called and stated that the water quit running out of hill. Water trucks are not available today but water is contained. Chris stated that he has pictures. The trap/impoundment has been pulled down and they will line with a pit liner. I stated that we will continually monitor the chlorides. |
1282048725 | 2010-08-12 | Drill / Deepen / Reopen | Violations Noted | On day of inspection I was in on site for a BOP Test. The BOP test could not be completed at present time because of wrong rubber size for the job. The CNX engineer Jay Hewitt notified me on a situation with water leaking out of hill. There were four places. There was a 4flow and two 2flows.There was also a 8plastic corrugated pipe that was used for a French drain between the pit and the west wall of the location. I contacted Supervisor Simmers and Inspector Moravy. They told me to notify Inspector Farnsworth to assist me with this situation. I contacted Inspector Farnsworth and he would be in route ASAP.I started taking samples of the water.WS-1 was taken at the 4stream down over the north end of the pit.WS-2 was taken at the sediment trap.WS-3 was taken at the center of the pit. Quantab readings revealed that the chlorides were 10,000-13,000ppm at WS-1 and WS-2.WS-3 and at site behind rig indicated that the chlorides were higher than that.The Baroid employee Titus Robinson took samples also. He indicated that the ground water sample was at a chloride level at 13,000ppm.The pit sample was at a 28,000ppm in chlorides. Jay Hewitt contacted the construction team and advised them that he needed them on site to construct the containment pit down over hill. At this point in time, the source of water is yet to be determined. I contacted Tom Tomastik in Columbus and he advised that there were no wells in area near the CNX site. Delrick construction showed up and started to get prepared to construct the containment pit. Approximately 6:00pm Inspector Farnsworth arrived and Hewitt and I briefed him about the situation. We assessed the pit and the water flowing out of the hillside. There was no visible indication on the pit liner that there was a fluid loss from the drilling pit at this time. Inspection of the drilling pit revealed that pit liner was scorched and melted during the flaring of the Utica gas. We observed that the fluid level was at the lowest visible hole at thi |
1282131430 | 2010-08-12 | Drill / Deepen / Reopen | No Violations | On day of inspection Jay Hewitt called stated that there be a BOP Test at 8:00am.The test would consist of testing pipe rams,choke,kill line,annular,sheer rams. The test would be later today because of well head rubber size is 9 5/8 and Green energy group brought 11well head rubber. The test revealed that we tested pipe rams, shear rams,annular,kill line to 250psi for 10min on low and 4500psi for 15min on high side. We tested choke to 4000psi on high and 250psi on low side. BOP test passed. |
1282237901 | 2010-08-18 | Drill / Deepen / Reopen | No Violations | On day of inspection went in to site and took a chloride reading on a quantab and it revealed that the water has dropped back to 2400ppm on chlorides. It is all being contained and monitored. Still extracting from the drill pit. Rig drilled into Utica shale and drilled through and hit a good flare on 10.2ppg on drill mud and showed 350units.Met with Jim Black and Jay Hewitt and Chris Miller. At 4:30 was at 8528.Just getting into the Trenton. The will take samples every 10 for mud logger. |
1282921047 | 2010-08-23 | Drill / Deepen / Reopen | No Violations | On day of inspection rig was at depth of 9818.They tripped drill pipe out and removed PDC bit and installed tricone bit. They were at 10.7 ppg mud and 41 viscosity. |
1283340614 | 2010-08-25 | Drill / Deepen / Reopen | No Violations | On day of inspection stopped in to check status and tricone bit went down. They were tripping pipe out of hole and going in with a magnet and junk basket. Depth was at 10,134.Checked the chlorides and they were at 3500ppm. |
1284510624 | 2010-09-07 | Drill / Deepen / Reopen | No Violations | On day of inspection checked status on how the production job went and picked up samples for geological survey. No water running out of bank anywhere. |
1287083224 | 2010-10-06 | Drill / Deepen / Reopen | No Violations | On day of inspection it was raining I had met with Jim Black on the site. It was causing soap suds on hillside and I told Black to get some environmental friendly de foamer sent to site. I was told that a tote of biodegradable soap was opened up and causing the problem. Up on inspection found that there was 25 roll offs on site and the company was loading them with pit cuttings. They will remove the pit liner and install fire clay in the bottom of the pit. All cuttings are hauled to an approved landfill. |
1289239465 | 2010-11-08 | Drill / Deepen / Reopen | No Violations | On day of inspection a company called McCutcheon was in sucking sludge out of tanks. Cleaning two fishburn tanks. |
1290935470 | 2016-03-02 | Salt Water Injection Well | No Violations | Well not in operation today due to owner having injection pump replaced they hope to be back in operation by Friday March 4,2016. |
1293129805 | 2014-07-24 | Salt Water Injection Well | No Violations | Inspection revealed that injection pump was in operation during my inspection and it was noted that one Force vacuum truck was unloading at facility during my inspection. |
1303445723 | 2010-08-19 | Drill / Deepen / Reopen | No Violations | On day of inspection Bret Farnsworth and I inspected well and found that chlorides were at 4360ppm.Wait on rain to purge. All water will be contained. Rig is at depth of 8995.No major gas just slow drilling. |
1315376791 | 2018-03-30 | Salt Water Injection Well | No Violations | Inspection revealed that injection pump was not in operation during my inspection. |
1329303680 | 2012-02-14 | Salt Water Injection Well | No Violations | On site to witness setting of storage tanks and building construction of pump house and electrical building they will start plumbing tanks together tomorrow and possibly start on construction of unloading pad. |
1332586665 | 2012-03-22 | Salt Water Injection Well | No Violations | Stopped by site to check on progress of building construction and placing of flow line to wellhead the line was installed to well it will need to be tested before well goes into operation and building for the injection pump is nearly complete and tanks are plumbed up and ready to be put into service. |
1335394377 | 2012-04-25 | Salt Water Injection Well | No Violations | Facility under construction nearly complete with electrical work once done they will be ready to go into operation once pressure testing is complete. |
1337069427 | 2012-10-11 | Salt Water Injection Well | No Violations | This inspection was due to a Compliance Notice that had not been resolved. The leaking pit was fixed and has since been closed. Compliance notice RESOLVED. |
1340316894 | 2012-06-21 | Salt Water Injection Well | No Violations | On site to witness testing of flow line to well head and also witness pressure testing of injection pumps, we tested flow line @2500 psi and monitored pressure for 15 minutes with no decline in pressure and we tested plumbing and injection pumps at 2400 psi and monitored for leaks for 30 minutes with no leaks detected.
Note: Facility is fully automated and there will be company personell on site while vaccum trucks unload at facility. |
1345588529 | 2012-08-21 | Salt Water Injection Well | No Violations | Inspection revealed that injection pump was not in operation today.
Note: Onsite to witness MIT testing along with UIC Director and group from Central Office to witness testing preformed by Producers Services they pressured up on annulus to 2540 psi and we monitored pressure for 15 minutes with a 5 lb pressure loss(TEST PASSED). |
1352939225 | 2012-11-14 | Salt Water Injection Well | No Violations | Inspection revealed that injection pump was in operation and it was noted that two Force water trucks were unloading at facility during my inspection.
Note: Personnel was on site applying protective winter cover on all exposed plumbing at facility. |
135535475 | 2012-5-24 0:00: | SW | No Violations | |
1363708567 | 2013-03-19 | Salt Water Injection Well | No Violations | Notice of Compliance is resolved on 3-19-13 by Patrick Shreve. |
1366639728 | 2017-05-11 | Salt Water Injection Well | No Violations | Inspection revealed that injection pump was in operation today and we are still waiting on slip repair too begin. |
1368363680 | 2012-08-29 | Salt Water Injection Well | No Violations | Inspection revealed that injection pump was not in operation today they were changing out injection pump during my inspection and were planning on starting pump if they got it hooked up and plumbed in. |
1368735629 | 2013-05-16 | Salt Water Injection Well | No Violations | Inspection revealed that injection pump was not in operation during my inspection and it was noted that annulus pressure is building up due to thermal expansion and I called company and requested that they bring out small tank so we can bleed down annular pressure.
Note: Annulus pressure was recorded from there monitor due to bad valve on annulus and I contacted company and requested that they replace valve so I can place my gauge on and record pressure with state gauge. |
1371173235 | 2013-06-13 | Salt Water Injection Well | No Violations | On the day of my inspection I accompanied Dave Ball who took pressure readings and conducted a full site inspection. No violations noted. |
1377879682 | 2013-08-29 | Salt Water Injection Well | No Violations | Inspection revealed that injection pump was in operation today and contractor was working on concrete containment area for small storage tank up at the wellhead. |
1380056586 | 2013-09-24 | Salt Water Injection Well | No Violations | Inspection revealed that injection pump was not in operation today and it was noted that plumbing on well head will need to be replaced due to seals leaking on seal ring on flanges leaking when valves are in open position. |
1381999290 | 2012-02-21 | Salt Water Injection Well | No Violations | Inspection revealed that unloading pad is under construction and pump house and electrical facility also will monitor site as time permits. |
1382225740 | 2013-10-18 | Salt Water Injection Well | No Violations | Inspection revealed that injection pump was not in operation during my inspection and it was noted that more plumbing work is needed at wellhead.
Note: Valve needs to be placed on line to tank so inspector can isolate pressure coming from annulus of tubing and pressure check down hole tubing pressure. |
1385744448 | 2013-11-27 | Salt Water Injection Well | No Violations | Inspection revealed that injection pump was not in operation during my inspection and it was noted that wellhead has been winterized by applying insulation to all fittings. |
1390867327 | 2014-01-27 | Salt Water Injection Well | No Violations | Inspection revealed that injection pump was in operation during my inspection and it was noted that there was a small leak in one of the flange connections and I informed operator that it would need to be repaired before injecting any more fluid into well.
Note: Well was shut down after discovering leak until repairs to faulty flange connection were made. |
1393968083 | 2014-03-04 | Salt Water Injection Well | No Violations | On site to test tubing for possible leakage Continental Wire line ran slick line unit to 10,500 and then they set plug inside of tubing and Producers Services pressured up on tubing to check for possible leakage if no leaks are found they will bring in service rig to release packer and replace packer and tubing string.
It was determined that tubing has leak and while testing the plug they set inside of packer with wire line got stuck they will attempt to free it up tomorrow and retrieve is they are unsuccessful they will pull packer and tubing. |
1394138763 | 2014-03-05 | Salt Water Injection Well | No Violations | Wire line retrieved from inside of tubing they will try and fish remaining articles out of tubing tomorrow. |
1394224007 | 2014-03-07 | Salt Water Injection Well | No Violations | Still fishing for lost tools within tubing string. |
1395090801 | 2014-03-17 | Salt Water Injection Well | No Violations | Inspection revealed that service rig has arrived on site waiting on orders from company, once they receive the go ahead they will rig up and release packer and pull from well and once removed they will install a new packer and tubing and flush annulus with fresh water laden with inhibitor and perform required pressure test. |
1395746231 | 2014-03-24 | Salt Water Injection Well | No Violations | On site to witness rebuilt Baker Hornet packer started in hole they ran 107 joints of tubing today and will resume running tubing in well tomorrow. |
1395959677 | 2014-03-25 | Salt Water Injection Well | No Violations | On site to witness tubing and packer run into well and pressure test annulus of tubing once packer gets set in place.
Note: Packer was set@10,305 and set in compression35K and we tested annulus pressure@2480 psi for 15 minutes with no decline in pressure. |
1396650864 | 2014-04-04 | Salt Water Injection Well | No Violations | On site to witness 1200 gallon acid job performed on said well Producers Services pumped acid and displaced it into formation and we monitored pressures throughout entire job. |
1416070640 | 2014-11-14 | Salt Water Injection Well | No Violations | Inspection revealed that injection pump was in operation today and it was noted that two HWR vacuum trucks were unloading at the facility during my inspection. |
1432386355 | 2015-05-20 | Salt Water Injection Well | No Violations | Inspection revealed that Basic Well Service was pulling tubing from well today. |
1432464053 | 2015-05-23 | Salt Water Injection Well | No Violations | On site to witness tubing and packer run into well Basic Well Services ran 10,369 of 3.5 tubing and Baker Hornet packer and set it and Producers Services pumped fresh water and inhibitor and we pressured tested annulus at 2460 psi for 15 minutes with no decline in pressure
Note: 35 gallon of inhibitor and 272 bbl fresh water and packer is set in 51K compression. |
1439642550 | 2015-08-11 | Salt Water Injection Well | No Violations | Inspection on this day indicated that injection pump was not in operation during my inspection but it was noted that one 100 bbl. vacuum truck was unloading at the site.
Note: UIC# 25--396 |
1446059227 | 2015-10-27 | Salt Water Injection Well | No Violations | On site to witness Producers Services perform 2000 gallon acid treatment 28% on said well.
|
1464722636 | 2016-05-31 | Salt Water Injection Well | No Violations | Schlumbger on site to perform acid treatment on said well, prior to doing acid job company wanted to pressure test tubing and now test plug is stuck in profile nipple above packer they have coil tubing unit enroute to site too try and retrieve plug so we can move forward with treatment plan. |
1480364249 | 2016-11-25 | Salt Water Injection Well | No Violations | Inspection today indicated that injection pump was not in operation during my inspection. |
1484414063 | 2015-05-21 | Salt Water Injection Well | No Violations | Basic Well Service running casing scrapper in well and they plan on cleaning out well bore to total depth of 10,394 and then they will prepare to run packer back into well on 5/23/15. |
1485278735 | 2017-01-24 | Salt Water Injection Well | No Violations | Inspection today revealed well is down due to large slip area on the north side of wellsite CEC engineering is on site with core hole rig to determine slope stability and come up with plan on repairing slip and placing well back into injection operations. |
1487282112 | 2017-02-16 | Salt Water Injection Well | No Violations | Inspection today revealed that well is down to a slip developed in the area of flowline and decision was made to have company come to site and access site and formulate repair plan.
Note: Wellhead is in stable area and currently poses no risk of danger, spoke with company rep Brian Randells inquiring if company has repair plan back from contractors for review he stated they are still working on repair plan. |
1492871365 | 2017-04-21 | Salt Water Injection Well | No Violations | Inspection revealed that injection pump was in operation and it was noted that one Force Trucking tanker was unloading at the facility during my inspection.
Note: They are still waiting on slip repair to begin and it was noted that slip area has not changed since my last inspection. |
1503763302 | 2017-08-22 | Salt Water Injection Well | No Violations | Inspection today revealed that injection pump was in operation and work on slip area still continues they are currently moving dirt back into place and compacting it as they put it into place.
Note:Sent photos to central office to be placed into well file. |
1508874451 | 2017-10-23 | Salt Water Injection Well | No Violations | On site along with county inspector to witness 4000 gallon acid treatment job on said well.
CJ services pumped 4000 gallon of 28% HCL acid and displaced it into formation and let it soak for 2 hours prior to resuming injection operations.
|
1509550855 | 2017-10-31 | Salt Water Injection Well | No Violations | Inspection today revealed that injection pumps were not in operation during my inspection and it was noted that electrical workers were on site preforming upgrades on the system. |
1515817249 | 2013-03-21 | Salt Water Injection Well | No Violations | Injection pump not operating today and unloading pad was clean and neat and no evidence of any spillage with in dike area. |
1518727624 | 2018-02-15 | Salt Water Injection Well | No Violations | Inspection today indicated that injection pump was in operation and in good repair and it was noted that in area of old slip area vegetation has began to grow and looks real good at present time. |
1525812954 | 2018-05-07 | Salt Water Injection Well | No Violations | Inspection today indicated that injection pump was in operation during my inspection and it was noted that one Force Trucking tanker was on site offloading during my inspection. |
1531334974 | 2012-12-13 | Salt Water Injection Well | No Violations | Inspection revealed that injection pump was in operation today and there was two Force Trucking vacuum trucks unloading at facility during my inspection. |
1535072050 | 2010-07-13 | Drill / Deepen / Reopen | No Violations | On day of inspection met with CNX man Clint Kelly. We took a tour of the rig and the site. We went over safety and the summary of the job. The rig started to drill mouse hole. |
1553022298 | 2013-09-26 | Salt Water Injection Well | No Violations | On site with company rep to discuss plumbing issues at well head he stated that corrections will be made within the next week and once they are completed he will call and request inspection on the repairs that were made. |
1556360953 | 2018-08-24 | Salt Water Injection Well | No Violations | Inspection today indicated that injection pump was in operation, and it was noted that contractor was on site repaving parking lot today. |
1556663677 | 2019-04-30 | Salt Water Injection Well | No Violations | Inspection today revealed that injection pump was in operation during my inspection and it was noted that one Force Trucking vacuum truck was on site offloading during my inspection. |
1563637943 | 2019-7-15 0:00: | SW | No Violations | |
1573313231 | 2019-11-6 0:00: | SW | No Violations | |
1581721333 | 2010-08-16 | Drill / Deepen / Reopen | No Violations | On day of Inspection Inspector Farnsworth and I met with CNX Compliance man Jim Black and Jay Hewitt and Chris Miller. Water has stopped coming out of bank and sediment trap is lined and containing water and all chloride water is contained in containment pit at bottom. Water still seeping out around french drain. Chlorides are 5800ppm.All fluid is contained. |
1682254422 | 2020-7-27 0:00: | SW | No Violations | |
1688990262 | 2018-06-07 | Salt Water Injection Well | No Violations | CNX gas company had C&J pressure pumping on location to perform an acid job. C&J pumped 2000 gallons of 28 percent HCL acid. They pressured up for 15 minutes on the backside with 500 pounds per square inch with no pressure decline noted. The acid job and testing was successful. Also present on the day of my inspection was Inspector David Ball. |
173415178 | 2010-7-9 0:00:0 | DD | No Violations | 1.00 |
1761133136 | 2010-08-13 | Administrative Inspection | No Violations | On this day received phone call from Jim Black and Kevin Smith on water issue at site. |
1779679926 | 2012-04-09 | Salt Water Injection Well | No Violations | Inspection revealed that facility is still under construction but is nearly complete we will test flow line and plumbing at pump house before putting well into operation. |
1810384094 | 2016-01-14 | Salt Water Injection Well | No Violations | Inspection revealed that injection pump was in operation during my inspection and it was noted that one Force Trucking vacuum truck was unloading at the facility today. |
1820614002 | 2010-08-13 | Drill / Deepen / Reopen | No Violations | On day of inspection I checked the drill pit and the area on hillside where water was coming out. Water was at a small tricle. Water trucks were hauling out of the pit. I took Quantab samples from the holes on the hill down to where there is a lined containment pit and down to culvert at St.Rt.800.The chlorides were at 5800 ppm. From the culvert to creek that runs parallel with State Route 800 The Chlorides were at .01 Parts Per Million. I told Chris Miller the CNX Consultant to haul out of the pit and the trap. Line the trap and from now on haul the fluids. I will be stopping in to Quantab the site and check chlorides. |
1849759703 | 2014-02-19 | Salt Water Injection Well | No Violations | On site to witness testing on annulus of tubing, Producers Services pumped 450 gallon of fresh water and reached pressure of 2150# then ran out of water they shut one side of well head off and we monitored pressure with state gauge and pressure declined too 500# within four minutes which indicated that they have tubing leak or packer failure.
Note: Well was shut down until repairs can be made !!. |
1879793305 | 2017-09-27 | Salt Water Injection Well | No Violations | Restoration work in slip area still continues contractor stated that they should be finished with work area within the next couple of weeks. |
1887229527 | 2013-06-27 | Salt Water Injection Well | No Violations | Inspection revealed that injection pump was not in operation during my inspection. |
1889192932 | 2014-06-17 | Salt Water Injection Well | No Violations | Inspection revealed that injection pump was in operation during my inspection and it was noted that three 500 barrel storage tanks still remained on site and I called company rep and requested that they be emptied and removed from site. |
1894153468 | 2019-03-15 | Salt Water Injection Well | No Violations | Inspection today revealed that injection pump was in operation during my inspection and it was noted that one high pressure valve on wellhead has been replaced since my last inspection. |
1923626777 | 2016-06-15 | Salt Water Injection Well | No Violations | Inspection today revealed that injection pump was in operation and it was noted that one Force trucking was unloading at the facility during my inspection. |
1928693159 | 2015-06-18 | Salt Water Injection Well | No Violations | Inspection revealed that injection pump was in operation today and in conversation with well tender stating that injection pressures have been good since they worked over well recently. |
1950042564 | 2012-10-11 | Preliminary Restoration | No Violations | On the day of my inspection the well site was restored in accordance with the ORC and preliminary restoration is now passed. PASSED |
2052380716 | 2013-02-01 | Salt Water Injection Well | No Violations | Inspection revealed that injection pump was not in operation during my inspection and well tender stated that they had brine trucks coming later today weather permitting. |
2098124996 | 2015-04-08 | Salt Water Injection Well | No Violations | Injection pump was in operation today and it was noted that owner has recently replaced filer pod in the pump house. |
2117209081 | 2017-01-04 | Salt Water Injection Well | No Violations | Received call from Brian Randell company water foreman stating that they have a slip up on wellsite that needs to be addressed so they have decided to shut well down until slip can be repaired. |
2144557314 | 2010-08-09 | Drill / Deepen / Reopen | No Violations | On day of inspection rig was getting stuck in the Utica shale. From 8190 -7600 set kick plug through drill pipe. Schlumberger set a 500 kick plug. Ran 40%excess and which is 569 sks. Then reversed circulated after a 500 ft pull. |
346839070 | 2015-5-18 0:00: | SW | No Violations | |
376924956 | 2019-10-7 0:00: | SW | No Violations | |
382928994 | 2017-3-28 0:00: | SW | No Violations | |
408655377 | 2010-7-26 0:00: | DD | No Violations | 1.00 |
545529800 | 2015-6-3 0:00:0 | SW | No Violations | |
707980751 | 2016-11-2 0:00: | SW | No Violations | |
798722601 | 2020-5-1 0:00:0 | SW | No Violations | |
839215518 | 2011-10-26 0:00 | SW | No Violations | |
842983716 | 2018-10-24 0:00 | SW | No Violations | |
854905002 | 2020-4-2 0:00:0 | SW | No Violations | |
885733160 | 2017-7-20 0:00: | SW | No Violations | |
921717884 | 2016-4-20 0:00: | SW | No Violations | |
966651421 | 2018-6-7 0:00:0 | SW | No Violations | |
976701831 | 2015-5-11 0:00: | SW | No Violations | 6.00 |
98998103 | 2014-4-23 0:00: | SW | No Violations | |
994061021 | 2019-8-28 0:00: | SW | No Violations |
Inspection ID | Violation ID | Violation Date | Violation Code | Violation Comments |
---|---|---|---|---|
1282048725 | US-OH-107837 | 2013-04-09 | Drilling operation causing pollution and contamination | |
1282048725 | US-OH-107838 | 2013-04-09 | Dike or pit not able to prevent escape of Brine or other wastes |
For data sources see[5]