If you find this page useful and would like to be notified of changes made to this page, start by inputting your email below.
powered by ChangeDetection
Well ID: 34-013-20657 | Loading map...
{"type":"SATELLITE","minzoom":false,"maxzoom":false,"types":["ROADMAP","SATELLITE","HYBRID","TERRAIN"],"mappingservice":"googlemaps3","width":"100%","height":"350px","centre":false,"title":"","label":"","icon":"","visitedicon":"","lines":[],"polygons":[],"circles":[],"rectangles":[],"wmsoverlay":false,"copycoords":false,"static":false,"zoom":14,"layers":[],"controls":["pan","zoom","type","scale","streetview","rotate"],"zoomstyle":"DEFAULT","typestyle":"DEFAULT","autoinfowindows":false,"resizable":false,"kmlrezoom":false,"poi":true,"markercluster":false,"clustergridsize":60,"clustermaxzoom":20,"clusterzoomonclick":true,"clusteraveragecenter":true,"clusterminsize":2,"imageoverlays":[],"kml":[],"gkml":[],"searchmarkers":"","enablefullscreen":false,"scrollwheelzoom":false,"locations":[{"text":"","title":"","link":"","lat":40.04,"lon":-81.12,"icon":""}]} |
Country: United States | |
State: Ohio | |
County: Belmont | |
Municipality: Kirkwood Township | |
Operator Name: GULFPORT APPALACHIA LLC | |
Well Pad ID: US-OH-000530 | |
Farm/Lease Name: SHUGERT | |
License Status: Producing | |
License Date: 2012-06-15 | |
Spud Date: 2012-05-25 | |
Spud Drilling Contractor: UNION DRLG | |
Final Drill Date: 2012-06-29 | |
Well Total Depth: 14225.00 ft | |
Configuration: Vertical | |
Latitude: 40.040000 | |
Longitude: -81.120000 |
For data sources see[1]
Well Status | Well Status Date | Comment |
---|---|---|
APP | 2012-02-16 | Proposed Formations:UTICA, Issued Date:2/16/2012, Expired Date:2/15/2014 12:00:00 PM, Drilling unit acres:0, Proposed Well Type:ST, Proposed Well Class:STRT |
APP | 2012-05-24 | Proposed Formations:TRENTON, Issued Date:5/24/2012, Expired Date:5/24/2014 12:00:00 PM, Drilling unit acres:0, Proposed Well Type:ST, Proposed Well Class:STRT |
Plugged Back | 2012-06-22 | |
Reached Total Depth | 2012-06-29 | |
Construction Permit Expires | 2014-05-24 | |
Record Last Modified | 2015-03-18 |
For data sources see[2]
Job Number | Job Start Date | Job End Date | True Vertical Depth (ft) | Total Water Volume (gal) | Total Non-Water Volume (gal) |
---|---|---|---|---|---|
1 | 07/16/2012 | 07/27/2012 | 8671.14 | 6,578,150.0 | 0 |
Job Number | Trade Name | Supplier | Purpose | Ingredient Name | CAS Number | Additive Percentage by Mass | Job Percentage by Mass | Mass Used (lb) |
---|---|---|---|---|---|---|---|---|
1 | Slickwater, WF115, YF115ST, 7.5% acid | Schlumberger | Corrosion Inhibitor, Bactericide (Myacide GA25), Scale Inhibitor, AntiFoam Agent, Surfactant , Acid, Breaker, Crosslinker, Gelling Agent, Friction Reducer, Iron Control Agent, Propping Agent, Fluid Loss Additive | Water (Including Mix Water Supplied by Client)* | NA | 0 | 85.8154 | 0 |
Dicoco dimethyl quaternary ammonium chloride | 61789-77-3 | 0.00153 | 0.00022 | 0 | ||||
Acrylamide, 2-acrylamido-2-methylpropanesulfonic
acid, sodium salt polymer |
38193-60-1 | 0.06474 | 0.00918 | 0 | ||||
Magnesium silicate hydrate (talc) | 14807-96-6 | 0.00007000 | 0.00001000 | 0 | ||||
Octamethylcyclotetrasiloxane | 556-67-2 | 0.00001000 | 0 | 0 | ||||
Thiourea, polymer with formaldehyde and 1-phenylethanone | 68527-49-1 | 0.00086 | 0.00012 | 0 | ||||
Dodecamethylcyclohexasiloxane | 540-97-6 | 0.00001000 | 0 | 0 | ||||
Alkenes, C>10 a- | 64743-02-8 | 0.00018 | 0.00003000 | 0 | ||||
Sodium tetraborate decahydrate | 1303-96-4 | 0.01408 | 0.002 | 0 | ||||
Urea | 57-13-6 | 0.00426 | 0.0006 | 0 | ||||
Siloxanes and Silicones, di-Me,
reaction products with silica |
67762-90-7 | 0.00001000 | 0 | 0 | ||||
Decamethyl cyclopentasiloxane | 541-02-6 | 0.00001000 | 0 | 0 | ||||
Ammonium sulfate | 7783-20-2 | 0.06119 | 0.00868 | 0 | ||||
Glutaraldehyde | 111-30-8 | 0.04374 | 0.0062 | 0 | ||||
Trisodium ortho phosphate | 7601-54-9 | 0.00861 | 0.00122 | 0 | ||||
Alcohols, C14-15, ethoxylated (7EO) | 68951-67-7 | 0.0004 | 0.00006000 | 0 | ||||
Diammonium peroxidisulphate | 7727-54-0 | 0.01487 | 0.00211 | 0 | ||||
Ethane-1,2-diol | 107-21-1 | 0.00245 | 0.00035 | 0 | ||||
Non-crystalline silica | 7631-86-9 | 0.00151 | 0.00021 | 0 | ||||
Fatty acids, tall-oil | 61790-12-3 | 0.00105 | 0.00015 | 0 | ||||
Polypropylene glycol | 25322-69-4 | 0.00028 | 0.00004000 | 0 | ||||
Polyethylene glycol monohexyl ether | 31726-34-8 | 0.03494 | 0.00496 | 0 | ||||
Methanol | 67-56-1 | 0.00142 | 0.0002 | 0 | ||||
Hydrogen chloride | 7647-01-0 | 0.35241 | 0.04999 | 0 | ||||
Dimethyl siloxanes and silicones | 63148-62-9 | 0.00006000 | 0.00001000 | 0 | ||||
Prop-2-yn-1-ol | 107-19-7 | 0.00027 | 0.00004000 | 0 | ||||
Potassium hydroxide | 1310-58-3 | 0.00007000 | 0.00001000 | 0 | ||||
Sodium erythorbate | 6381-77-7 | 0.00253 | 0.00036 | 0 | ||||
Crystalline silica | 14808-60-7 | 98.9818 | 14.0402 | 0 | ||||
1, 2, 3 - Propanetriol | 56-81-5 | 0.02346 | 0.00333 | 0 | ||||
Guar gum | 9000-30-0 | 0.32816 | 0.04655 | 0 | ||||
Sodium sulfate | 7757-82-6 | 0.02645 | 0.00375 | 0 | ||||
Polymer of 2-acrylamido-2-methylpropanesulfonic
acid sodium salt and methyl acrylate |
136793-29-8 | 0.00694 | 0.00098 | 0 | ||||
Tetrasodium ethylenediaminetetraacetate | 64-02-8 | 0.00013 | 0.00002000 | 0 | ||||
Vinylidene chloride/methylacrylate copolymer | 25038-72-6 | 0.00127 | 0.00018 | 0 | ||||
Propan-2-ol | 67-63-0 | 0.00031 | 0.00004000 | 0 | ||||
Sodium hydroxide | 1310-73-2 | 0.00001000 | 0 | 0 |
For data sources see[3]
Period | Operator Name | Waste Type | Quantity (bbl) | Production Days |
---|---|---|---|---|
2012 | GULFPORT ENERGY CORPORATION | Brine | 2343 | 5 |
2013 | GULFPORT ENERGY CORPORATION | Brine | 23908 | 200 |
2014 | GULFPORT ENERGY CORPORATION | Brine | 20123 | 339 |
2015 | GULFPORT ENERGY CORPORATION | Brine | 2102 | 329 |
2016 | GULFPORT ENERGY CORPORATION | Brine | 2979 | 360 |
2017 | GULFPORT ENERGY CORPORATION | Brine | 1667 | 363 |
2018 | GULFPORT ENERGY CORPORATION | Brine | 1323 | 363 |
2019 | GULFPORT ENERGY CORPORATION | Brine | 251 | 90 |
Inspection ID | Inspection Date | Inspection Type | Inspection Result | Inspection Comments |
---|---|---|---|---|
-1024873253 | 2013-1-2 0:00:0 | PW | No Violations | 0.50 |
-1440531795 | 2015-1-21 0:00: | PW | No Violations | 2.00 |
-1743522845 | 2019-1-10 0:00: | PB | No Violations | 0.10 |
-1887447996 | 2017-8-10 0:00: | PW | No Violations | 0.50 |
-1946402956 | 2013-3-6 0:00:0 | PL | No Violations | 0.50 |
-369235296 | 2020-11-3 0:00: | PW | No Violations | 0.30 |
-469161073 | 2013-1-24 0:00: | PW | No Violations | 0.50 |
-494393143 | 2019-1-10 0:00: | PW | No Violations | 0.20 |
0201537417 | 2012-11-21 | Production Wells | No Violations | On the day of my inspection Deepwell was running tubing. Company man Chad Cavelle present. No violations noted. |
0369837083 | 2015-01-12 | Production Wells | No Violations | On the date of inspection I met with Brad Burwell with Gulfport Energy and Jermey Kinney with Hull and Associates. I was on site to collect information from Brad Burwell who had reported a spill at the Shugert 1 pad beneath a scrubbing unit. Brad informed me that a pressure test was done on a buried 4 inch PVC line that was attached to a scrubbing unit. The line was pressure tested with water and failed to test. A leak was found at the connection of the 4 inch line to the scrubbing unit that was buried. According ot Brad the pressure testing was overseen by Royce Bagwell with Gulfport and was performed by ROC Oilfield Services. Brad was informed that approximately 2bbl of water was lost during the testing but it is unclear how much contaminant was released. Brad was informed by Royce Bagwell that the scrubbing unit and 2 separators adjacent to it were not currently in use. At the time of my inspection the excavation was approximately 10 feet by 12 feet wide and 2 feet in depth. On top was approximately 18 inches of limestone aggregate with silty clay underlying it. Jeremy was on site field screening samples using a MineRAE 3000 Photo Ionization Detector (PID). The PID was calibrated using Span gas once each morning. I was informed that the 4 inch line that leaked was primarily a gas carrying line when it was in use. The highest PID readings came from the porous gravel and the contamination appeared to travel in the direction that the 4 inch line had been previously buried. Gulfport will continue to excavate until they can no longer find elevated PID readings. According to Brad, the highest reading they had found as of today was 300ppm. After speaking with Rick Trippel with ODNR, I requested that they send a few samples to the lab to confirm the PID readings and determine if they had excavated to clean soil/gravel. I requested that they include one sample with an elevated reading to obtain a fingerprint of what was released as well as sidewall samples and at least o |
0469161073 | 2013-01-24 | Production Wells | No Violations | On the day of my inspection company was working on the tank battery. No violations noted. |
0494393143 | 2019-01-10 | Production Wells | No Violations | On site inspection found the well equipped with a lower A and upper B section with 2 diameter riser pipes attached to both sections, both riser pipes have valves but only one has a gauge. The riser pipes are not identified as to which well head section they are associated. The well is producing through 3 primary master gate valves and one hydraulic valve present on the production tree with artificial lift technologies present. There is an emergency shut down control button at the well head along with at the production fluid storage area and at the well pad entry along with the gas processing units. The production facility consists of (6) steel construction tanks situated inside a polymer lined steel containment dike area. The well pad perimeter does not have a complete earthen berm surrounding it. The well pad surface and lease road is stone construction and in good repair. There is well identification on each of the (4) wells present on the pad along with at the well pad entry point. The tank battery has hazard warning labels. |
0599988550 | 2012-06-29 | Drill / Deepen / Reopen | No Violations | Stopped by drill rig for update they were at T.D.@14,225 cleaning well bore in preparation to run 5.5 casing . |
1010657344 | 2014-01-09 | Production Wells | No Violations | Responded to a call from Chris Anderson of ALL consulting. A line from the production equipment had failed causing .34 of a barrel of production fluid to spill on pad. Site was remediated. No evident environmental impact. |
1024873253 | 2013-01-02 | Production Wells | No Violations | On the day of my inspection there was no activity on the site. Well is capable of production. No violations noted. |
1348872964 | 2012-09-25 | Completion Testing | No Violations | Inspection revealed that crew was rigging up flow back iron from wellhead to tanks they plan on flowing well back in the next couple of weeks. |
1440531795 | 2015-01-21 | Production Wells | No Violations | On the date of inspection I was on site to check the status of the condensate spill cleanup on the well pad. When I arrived only a water truck operator and his truck were on site sucking fluid from the excavation. I took several pictures which are accessible on the shared drive. I spoke with Brad Burwell later that day on the phone and he stated that the cleanup was complete, samples had been collected (flags in pictures), and that Gulfport was waiting for the laboratory analysis of samples before moving forward. Since my last inspection, the excavation had been extended to the north and northwest (in the opposite direction of the tanks). The entire excavation is approximately 100 feet in length, 10 to 20 feet in width and 1.5 to 4 feet in depth. The excavation extended to expose 4 buried lines. |
1543140993 | 2018-05-15 | Production Wells | No Violations | On the day of my inspection I witnessed that the well was equipped with 5.5 inch diameter production casing with a plunger lift system, all valves were open at the time of my inspection. Annular pressure monitoring was in place for the 9.625 inch diameter casing gauge read 0 pounds per square inch, the 13.375 inch diameter casing gauge read 0 pounds per square inch. Production equipment included a Sand Trap, Separator, Gas Processing unit and line heater. There are 6- 400 barrel purge tanks shared with 3401320706, 3401320689, 3401320688. Identification tags were present, and production was up to date. |
1730062219 | 2014-10-23 | Preliminary Restoration | No Violations | This site has proper erosion and sediment controls preliminary restoration on this site is complete. |
1743522845 | 2019-01-10 | Plug / Plug Back | No Violations | Inspection report to document the well was drilled as a strata graphical test and was plugged back then drilled horizontally and is in production as 3401320657-0100. |
1853036947 | 2012-11-21 | Completion Testing | No Violations | Deep well well services are running 2.875upset tubing in well. There are about 250 joints. String weight will be about 45,000psi. Rig will move snubbing unit and pumping unit in to break pressure disc and get well in line. |
1887447996 | 2017-08-10 | Production Wells | No Violations | This well is equipped with 5.5-inch diameter production casing. The well appears to be free flowing without any artificial lift technology present at this time. The well is piped to a gas processing unit and then to six 400 barrel production fluid holding tanks. Production records in RBDMS are current to 2017. |
1946402956 | 2013-03-06 | Preliminary Restoration | No Violations | On the day of my inspection site was satisfactory. Preliminary restoration cannot be completed because the well site is still being developed. No violations noted. |
201537417 | 2012-11-21 0:00 | PW | No Violations | 2.00 |
369837083 | 2015-1-12 0:00: | PW | No Violations | 4.50 |
599988550 | 2012-6-29 0:00: | DD | No Violations |
For data sources see[6]