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Well ID: 34-013-20906 | Loading map...
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Country: United States | |
State: Ohio | |
County: Belmont | |
Municipality: Wheeling Township | |
Operator Name: AMERICAN ENERGY UTICA LLC | |
Well Pad ID: US-OH-001212 | |
Farm/Lease Name: CRAVAT N WHL BL | |
License Status: Final Restoration | |
License Date: 2015-05-01 | |
Spud Date: 2015-06-18 | |
Spud Drilling Contractor: | |
Final Drill Date: | |
Well Total Depth: | |
Configuration: Vertical | |
Latitude: 40.150000 | |
Longitude: -80.910000 |
For data sources see[1]
Well Status | Well Status Date | Comment |
---|---|---|
APP | 2015-01-14 | Proposed Formations:UTICA THRU POINT PLEASANT, Issued Date:1/14/2015, Expired Date:1/13/2017 12:00:00 PM, Drilling unit acres:0, Proposed Well Type:ST, Proposed Well Class:STRT |
Correction to Well | 2015-03-27 | CHANGE IN WELL NUMBER |
APP | 2015-05-01 | Proposed Formations:UTICA THRU POINT PLEASANT, Issued Date:5/1/2015, Expired Date:4/30/2017 12:00:00 PM, Drilling unit acres:453.384, Proposed Well Type:OG, Proposed Well Class:EDPW |
Plugged/Abandoned | 2015-07-08 | |
Construction Permit Expires | 2017-04-30 | |
Record Last Modified | 2018-01-04 |
For data sources see[2]
Inspection ID | Inspection Date | Inspection Type | Inspection Result | Inspection Comments |
---|---|---|---|---|
-1387171067 | 2018-1-2 0:00:0 | FR | No Violations | 0.50 |
-733592749 | 2015-7-8 0:00:0 | PB | No Violations | 3.00 |
-866486712 | 2015-6-29 0:00: | DD | No Violations | 2.00 |
0018075866 | 2015-06-18 | Casing String Witnessed | No Violations | |
0733592749 | 2015-07-08 | Plug / Plug Back | No Violations | This well is a lost hole. Following the 18.625 cement job the operator was tripping back into the hole with the 17.5 hammer bit when they encountered an obstruction @ 135. Upon further investigation it was found that the 18.625 casing had parted. The operator decided to plug this well. Cement was tagged when running tubing @ 155. The cement from the backside had entered the inside of the casing. Cement circulated top of cement to surface. |
0866486712 | 2015-06-29 | Drill / Deepen / Reopen | No Violations | Following the 18.625 casing job Alpha Hunter # 9 attempted to trip into the hole with their 17.5 bit. They hit an obstruction @ 130. Upon further investigation it was found that the 18.625 casing was compromised at that depth. The operator has decided that it is unfeasible to salvage this well and they have chosen to plug and abandon it. They will survey another well within 50 of the original location and permit it as the 3HA well. |
1387171067 | 2018-01-02 | Final Restoration | No Violations | The final restoration for this well is complete as the well has been plugged. The restoration for the well site pad disturbance area is required to be remediated once all other wells on this pad are plugged. Final restoration passed. |
1435502204 | 2015-06-28 | Casing String Witnessed | No Violations | On this day Alpha Rig #9 had reach a total depth of 350. No mine was encountered on this well. Formation was soft around 230-240. The rate of penetration only picked up for about 2 in this section. Hammer hit all the way through the formations. Cuttings revealed approximately 25% coal. The 18.625 casing was ran and cemented into a 24 open hole to a depth of 340. O-Tex Cementing was on site to cement with 680 sacks of Class A cement. Cement to surface established. See cement ticket for details. |
18075866 | 2015-6-18 0:00: | CS | No Violations | 4.00 |
For data sources see[3]