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Well ID: 34-013-21081 | Loading map...
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Country: United States | |
State: Ohio | |
County: Belmont | |
Municipality: Colerain Township | |
Operator Name: ASCENT RESOURCES UTICA LLC | |
Well Pad ID: US-OH-001392 | |
Farm/Lease Name: SEABRIGHT CLR BL | |
License Status: Final Restoration | |
License Date: 2016-07-14 | |
Spud Date: 2016-10-28 | |
Spud Drilling Contractor: FALCON DRLG | |
Final Drill Date: | |
Well Total Depth: 1769.00 ft | |
Configuration: Horizontal | |
Latitude: 40.100000 | |
Longitude: -80.800000 |
For data sources see[1]
Well Status | Well Status Date | Comment |
---|---|---|
APP | 2016-07-14 | Proposed Formations:UTICA THRU POINT PLEASANT, Issued Date:7/14/2016, Expired Date:7/14/2018 12:00:00 PM, Drilling unit acres:604.313, Proposed Well Type:OG, Proposed Well Class:FWC |
Plugged/Abandoned | 2016-11-12 | |
Completion Report Received | 2017-03-28 | |
Construction Permit Expires | 2018-07-14 | |
Record Last Modified | 2018-07-24 |
For data sources see[2]
Inspection ID | Inspection Date | Inspection Type | Inspection Result | Inspection Comments |
---|---|---|---|---|
-489058202 | 2016-11-8 0:00: | DD | No Violations | 3.00 |
-496960189 | 2017-5-4 0:00:0 | FR | No Violations | 1.00 |
-704501536 | 2016-11-9 0:00: | DD | No Violations | 2.00 |
0489058202 | 2016-11-08 | Drill / Deepen / Reopen | No Violations | The casing run was unsuccessful and the company had elected to remove the casing from the well bore and attempt a ream and clean out cycle to begin attempts to run the 13.375 casing again. |
0496960189 | 2017-05-04 | Final Restoration | No Violations | The final restoration for this well is complete as the well has been plugged. The restoration for the well site pad disturbance area is required to be remediated once all other wells on this pad are plugged. Final restoration passed. |
0704501536 | 2016-11-09 | Drill / Deepen / Reopen | No Violations | Falcon Rig 26 has pulled that casing and begun drilling again to condition the hole and attempt to run the 13.375 casing string again. |
1146871483 | 2016-11-09 | Drill / Deepen / Reopen | No Violations | Falcon Rig 26 is attempting to run the 13.375 casing with little success. They will continue their attempt. I will check back in the later today. |
1281565814 | 2016-11-03 | Drill / Deepen / Reopen | No Violations | Falcon Rig 26 was drilling the 17.5 open hole section of the well bore. The 13.375 casing is anticipated to be set tomorrow. |
1472480317 | 2016-08-26 | Casing String Witnessed | No Violations | |
1478700569 | 2016-11-08 | Drill / Deepen / Reopen | No Violations | Falcon 26 was on attempting to run the 13.375 surface casing to total depth and O-Tex was on site to cement the casing. |
1479132936 | 2016-11-12 | Plug / Plug Back | No Violations | |
1729785697 | 2016-11-10 | Plug / Plug Back | No Violations | The operator has decided to deem this well a lost hole and begin plugging operations. They will attempt to go into the hole with open ended drill string and cement through the same. If that does not work they will put a bit on, drill back to total depth and cement through the bit. |
For data sources see[3]