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Well ID: 34-013-21179 | Loading map...
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Country: United States | |
State: Ohio | |
County: Belmont | |
Municipality: Washington Township | |
Operator Name: GULFPORT APPALACHIA LLC | |
Well Pad ID: US-OH-001454 | |
Farm/Lease Name: WHITE 210082 | |
License Status: Producing | |
License Date: 2017-06-14 | |
Spud Date: 2017-03-21 | |
Spud Drilling Contractor: NOMAC DRILLING CORP | |
Final Drill Date: 2017-07-14 | |
Well Total Depth: 17640.00 ft | |
Configuration: Horizontal | |
Latitude: 39.940000 | |
Longitude: -81.010000 |
For data sources see[1]
Well Status | Well Status Date | Comment |
---|---|---|
APP | 2017-02-08 | Proposed Formations:TRENTON, Issued Date:2/8/2017, Expired Date:2/8/2019 12:00:00 PM, Drilling unit acres:0, Proposed Well Type:ST, Proposed Well Class:STRT |
APP | 2017-06-14 | Proposed Formations:UTICA/POINT PLEASANT, Issued Date:6/14/2017, Expired Date:6/14/2019 12:00:00 PM, Drilling unit acres:390.554, Proposed Well Type:OG, Proposed Well Class:POOL |
Reached Total Depth | 2017-07-14 | |
Correction to Well | 2017-09-01 | CHANGE TO TARGET AND TAKE-POINT INFORMATION FROM AS DRILLED SURVEY PLAT. |
Completion Report Received | 2018-01-26 | |
Record Last Modified | 2018-02-10 | |
Construction Permit Expires | 2019-06-14 |
For data sources see[2]
Perforation Date | Interval Top (ft) | Interval Base (ft) | Number of Shots |
---|---|---|---|
2018-02-09 | 9650 | 9794 | 40 |
2018-02-09 | 17370 | 17468 | 40 |
17370 | 17468 | 40 | |
9650 | 9794 | 40 | |
9650 | 9794 | 40 |
For data sources see[3]
Job Number | Job Start Date | Job End Date | True Vertical Depth (ft) | Total Water Volume (gal) | Total Non-Water Volume (gal) |
---|---|---|---|---|---|
1 | 09/02/2017 | 09/22/2017 | 9426 | 12,927,900.0 | 0 |
Job Number | Trade Name | Supplier | Purpose | Ingredient Name | CAS Number | Additive Percentage by Mass | Job Percentage by Mass | Mass Used (lb) |
---|---|---|---|---|---|---|---|---|
1 | NEFE-180 | Chemplex | Corrosion Inhibitor/Iron Control | 2-Ethylhexanol | 104-76-7 | 10 | 0.000131145 | 157.3 |
Coconut oil acid diethanolamine | 68603-42-9 | 5 | 0.00006557 | 78.65 | ||||
Fatty acids, tall oil | 61790-12-3 | 5 | 0.00006557 | 78.65 | ||||
Alcohols, C14-15, ethoxylated | 68951-67-7 | 5 | 0.00006557 | 78.65 | ||||
Olefin | Proprietary | 5 | 0.00006557 | 78.65 | ||||
2-Propyn-1-ol | 107-19-7 | 5 | 0.00006557 | 78.65 | ||||
Methanol | 67-56-1 | 35 | 0.000459008 | 550.55 | ||||
Acetic acid | 64-19-7 | 65 | 0.000852444 | 1022.45 | ||||
Other Chemical(s) | Listed Above | See Trade Name(s) List | Alcohols, C12-16, Ethoxylated | 68551-12-2 | 2 | 0.00177631 | 2130.57 | |
Olefin | Proprietary | 5 | 0.00006557 | 78.65 | ||||
Water | 7732-18-5 | 45 | 0.039967 | 47937.8 | ||||
Water | 7732-18-5 | 55 | 0.00769018 | 9223.85 | ||||
Oleic Acid Diethanolamide | 93-83-4 | 2 | 0.00177631 | 2130.57 | ||||
Methanol | 67-56-1 | 35 | 0.000459008 | 550.55 | ||||
Water | 7732-18-5 | 72 | 0.151764 | 182030 | ||||
Fatty acids, tall oil | 61790-12-3 | 5 | 0.00006557 | 78.65 | ||||
Ammonium Chloride ((NH4)Cl) | 12125-02-9 | 1 | 0.000888156 | 1065.28 | ||||
Ethanol | 64-17-5 | 5 | 0.00145712 | 1747.72 | ||||
Water | 7732-18-5 | 60 | 0.0174854 | 20972.6 | ||||
2-Ethylhexanol | 104-76-7 | 10 | 0.000131145 | 157.3 | ||||
Coconut oil acid diethanolamine | 68603-42-9 | 5 | 0.00006557 | 78.65 | ||||
Didecyl dimethyl Ammonium Chloride | 7173-51-5 | 10 | 0.00291424 | 3495.44 | ||||
Alcohols, C14-15, ethoxylated | 68951-67-7 | 5 | 0.00006557 | 78.65 | ||||
copolymer of 2-propenamide | 69418-26-4 | 30 | 0.0266447 | 31958.5 | ||||
Quaternary Ammonium Compounds,
Benzyl-C12-C16-alkyldimethyl, Chlorides |
68424-85-1 | 10 | 0.00291424 | 3495.44 | ||||
2-Propyn-1-ol | 107-19-7 | 5 | 0.00006557 | 78.65 | ||||
Sand (100 Mesh Proppant) | Muskie | Proppant | Silica Substrate | 14808-60-7 | 100 | 1.36453 | 1,636,660.0 | |
Sand (40/70 Proppant) | Muskie | Proppant | Silica Substrate | 14808-60-7 | 100 | 8.27927 | 9,930,430.0 | |
Plexslick 920 | Chemplex SOLVAY | Friction Reducer | Petroleum Distillate | 64742-47-8 | 20 | 0.0177631 | 21305.7 | |
Ammonium Chloride ((NH4)Cl) | 12125-02-9 | 1 | 0.000888156 | 1065.28 | ||||
Water | 7732-18-5 | 45 | 0.039967 | 47937.8 | ||||
Oleic Acid Diethanolamide | 93-83-4 | 2 | 0.00177631 | 2130.57 | ||||
copolymer of 2-propenamide | 69418-26-4 | 30 | 0.0266447 | 31958.5 | ||||
Alcohols, C12-16, Ethoxylated | 68551-12-2 | 2 | 0.00177631 | 2130.57 | ||||
Hydrochloric Acid (28%) | Oxy | Acidizing | Water | 7732-18-5 | 72 | 0.151764 | 182030 | |
Hydrochloric Acid (Hydrogen Chloride) | 7647-01-0 | 28 | 0.0590192 | 70789.6 | ||||
Sand (30/50 Proppant) | Muskie | Proppant | Silica Substrate | 14808-60-7 | 100 | 0.066965 | 80320 | |
Water | Gulfport Energy Corporation | Carrier/Base Fluid | Water | 7732-18-5 | 100 | 89.9452 | 107,883,000.0 | |
SI-20 | Moon | Scale inhibitor | Water | 7732-18-5 | 55 | 0.00769018 | 9223.85 | |
Phosphinocarboxylic Acid | 110224-99-2 | 45 | 0.00629196 | 7546.79 | ||||
B2512 | Aquaserv | Biocide | Quaternary Ammonium Compounds,
Benzyl-C12-C16-alkyldimethyl, Chlorides |
68424-85-1 | 10 | 0.00291424 | 3495.44 | |
Didecyl dimethyl Ammonium Chloride | 7173-51-5 | 10 | 0.00291424 | 3495.44 | ||||
Glutaraldehyde | 111-30-8 | 30 | 0.00874272 | 10486.3 | ||||
Water | 7732-18-5 | 60 | 0.0174854 | 20972.6 | ||||
Ethanol | 64-17-5 | 5 | 0.00145712 | 1747.72 |
For data sources see[4]
Stimulation Date | Chemical Agent | Chemical Agent Concentration (%) | Fracking Fluid Volume | Mass of Proppant Used (lb) | Fracking Company | Comments |
---|---|---|---|---|---|---|
2017-09-22 | H2O | 10 | 6999 Bbl | 273340 | STINGRAY PRESSURE PUMPING LLC | STAGE 44/44
STAGES 2-43 SEE IMAGES |
2017-09-03 | H2O | 15 | 7104 Bbl | 275980 | STINGRAY PRESSURE PUMPING LLC | STAGE 1/44
STAGES 2-43 SEE IMAGES |
For data sources see[5]
Period | Operator Name | Gas Quantity (mcf) | Oil Quantity (bbl) | Production Days |
---|---|---|---|---|
2017 | GULFPORT ENERGY CORPORATION | 630530 | 0 | 46 |
2018 | GULFPORT ENERGY CORPORATION | 3862956 | 0 | 361 |
2019 | GULFPORT ENERGY CORPORATION | 448767 | 0 | 90 |
Period | Operator Name | Waste Type | Quantity (bbl) | Production Days |
---|---|---|---|---|
2017 | GULFPORT ENERGY CORPORATION | Brine | 7124 | 46 |
2018 | GULFPORT ENERGY CORPORATION | Brine | 25422 | 361 |
2019 | GULFPORT ENERGY CORPORATION | Brine | 3015 | 90 |
Inspection ID | Inspection Date | Inspection Type | Inspection Result | Inspection Comments |
---|---|---|---|---|
-1817988927 | 2018-8-21 0:00: | PW | No Violations | 0.50 |
-52259357 | 2018-8-7 0:00:0 | PW | No Violations | 0.30 |
0052259357 | 2018-08-07 | Production Wells | No Violations | Status check inspection found the well pad surface and lease road has a gravel surface and is in good repair. There are 6 wells present on the pad all in production. The said well is equipped with a lower A section and upper B section with 2 diameter riser pipes present at the well head and equipped with valves and manual pressure gauges to monitor annular pressure. The 13.375 x 9.625 diameter casing pressure was 200 pounds per square inch (psi) the 9.625 x 5.5 diameter casing pressure was 500 psi. The 5.5 diameter production casing internal working pressure was 4,100 psi and the production flow line pressure was 1,000 psi. The well is equipped with production tubing and was free flowing above line pressure. There are 6 gas processing units on location. At the right rear corner of the well pad is the production fluid facility consisting of 4 steel construction 400 barrel capacity production tanks located inside a polymer lined steel containment dike area. There is also a midstream station at the right front corner entry point of the well pad. Fire extinguishers and emergency shut down control points are present at all the critical areas of the well pad. The well pad perimeter is protected by an earthen berm. Also on this day I contacted Gulfports Production Superintendent Robert Coots and we discussed the 9.625 annular pressures on several of the wells on the pad along with having the well pad annulis monitored more closely while stimulation operations are going on the neighboring well pad. |
1339688361 | 2018-03-22 | Production Wells | No Violations | The well is equipped with 5.5-inch diameter production casing. The well appears to be free flowing with no artificial lift technology present. The well is piped to a gas processing unit. From there, it is routed to a production area that contains four 400-barrel production fluid holding tanks. There were also three 500-barrrel frac tanks on site. Annular pressures read on the gauges provided appeared to be 150 pounds on between the outside of the 9.625-inch diameter casing and the inside of the 13.375-inch diameter casing and 825 pounds between the outside of the 5.5-inch diameter casing and the inside of the 9.625-inch diameter casing . The production records within RBDMS are currently updated to 2017. |
1494851987 | 2017-05-12 | Casing String Witnessed | No Violations | Purpose of this inspection was to witness the cementing of the surface casing. Accomapnied by Inspector Pat Shrieve, please see his report this date for job details. |
1663890087 | 2018-03-22 | Production Wells | No Violations | Accompanied Belmont County Inspector Andrew Corder, Reference his Report for further details |
1817988927 | 2018-08-21 | Production Wells | No Violations | On the day of my inspection I witnessed that the well was equipped with a 3-string casing design with 5.5-inch diameter production casing that appeared to be open flowing with no artificial lift technology. Annular pressure monitoring was in place for the 9.625-inch diameter intermediate casing gauge read 690 pounds per square inch, and the 13.375-inch diameter casing gauge read 200 pounds per square inch. Production equipment included a Sand Separator, Gas Processing unit and four 400-barrel production fluid tanks, and a 50-barrel produced water tank shared with the other producing wells on the well pad. There were multiple Emergency Shutoff Devices on location, Identification tags were present, and production was up to date. |
926208030 | 2020-7-16 0:00: | PL | No Violations | 0.20 |
957871640 | 2020-3-23 0:00: | PW | No Violations | 0.20 |
For data sources see[10]