X

Track changes made to this page

If you find this page useful and would like to be notified of changes made to this page, start by inputting your email below.



Privacy policy
Close this window

powered by ChangeDetection

34-013-21250

Well Details

Well ID: 34-013-21250
Loading map...
Country: United States
State: Ohio
County: Belmont
Municipality: Washington Township
Operator Name: GULFPORT APPALACHIA LLC
Well Pad ID: US-OH-001520
Farm/Lease Name: HORSESHOE 210088
License Status: Producing
License Date: 2017-11-27
Spud Date: 2017-12-19
Spud Drilling Contractor: PIONEER DRILLING
Final Drill Date: 2018-04-03
Well Total Depth: 23807.00 ft
Configuration: Horizontal
Latitude: 39.900000
Longitude: -80.930000

For data sources see[1]

Well History

Well Status Well Status Date Comment
APP 2017-05-25 Proposed Formations:TRENTON, Issued Date:5/25/2017, Expired Date:5/25/2019 12:00:00 PM, Drilling unit acres:0, Proposed Well Type:ST, Proposed Well Class:STRT
APP 2017-11-27 Proposed Formations:UTICA/POINT PLEASANT, Issued Date:11/27/2017, Expired Date:11/27/2019 12:00:00 PM, Drilling unit acres:663.085, Proposed Well Type:OG, Proposed Well Class:POOL
Reached Total Depth 2018-04-03
Record Last Modified 2018-08-09
Correction to Well 2018-08-31 TAKE TARGET AS-DRILLED
Construction Permit Expires 2019-11-27

For data sources see[2]

Perforation Treatments

Perforation Date Interval Top (ft) Interval Base (ft) Number of Shots
23647 10507 0
23647 10507 0

For data sources see[3]

Inspection Data

Inspections Performed

Inspection ID Inspection Date Inspection Type Inspection Result Inspection Comments
-2096865217 2018-7-31 0:00: CT No Violations 0.10
-899267340 2020-10-20 0:00 PW No Violations 0.20
-920934483 2019-7-30 0:00: PW No Violations 0.40
0176231226 2018-03-23 Drill / Deepen / Reopen No Violations Pioneer Rig 71 had reached total depth in the 12.25-inch diameter open hole section of the well bore. They were currently performing a reamer run. Following the reamer run they will run their 9.625-inch diameter casing string to approximately 9261 feet. Stingray Cementing Services will provide the cementing procedure for this section of the well bore.
1103688779 2020-2-25 0:00: PW No Violations 0.20
1533062474 2018-07-31 Completion Testing No Violations Status check inspection found the well drilling process is complete and there is a night cap on the well head B section. Crews are on site installing the subsurface production equipment such as flowlines etc. 6 wells have been drilled on the well pad.
1534063899 2019-04-11 Completion Testing No Violations
1560431186 2019-6-13 0:00: CT No Violations 0.20
1728462370 2017-12-20 Casing String Witnessed No Violations Location address: 55950 Goddard Rd, Beallsville. On the day of my inspection I witnessed Lightning had augured a 36 inch diameter hole to 110 feet. 110 feet of 26 inch diameter conductor casing was run. Stingray was onsite with 430 sacks of class A cement. Additives include 2% CaCl and .25 lb./sack cello-flake. Cement weighed with mudscale at 15.6 ppg and yield of 1.21. 30 percent excess ran. 15 barrels of gel ahead of cement. Cement was displaced with 55 barrels of fresh water. 15 barrels of cement returned to surface.
176231226 2018-3-23 0:00: DD No Violations 1.00
2096865217 2018-07-31 Completion Testing No Violations Status check inspection found the well drilling process is complete and there is a night cap on the well head B section. Crews are on site installing the subsurface production equipment such as flowlines etc. 6 wells have been drilled on the well pad. The drilling rig mouse hole has been filled with cement.
417983113 2020-4-29 0:00: PW No Violations 0.20

For data sources see[4]

References