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Well ID: 34-013-21365 | Loading map...
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Country: United States | |
State: Ohio | |
County: Belmont | |
Municipality: Mead Township | |
Operator Name: XTO ENERGY INC. | |
Well Pad ID: US-OH-001341 | |
Farm/Lease Name: KRNYAICH UNIT C | |
License Status: Producing | |
License Date: 2018-09-21 | |
Spud Date: 2018-08-11 | |
Spud Drilling Contractor: PATTERSON DRILLING | |
Final Drill Date: 2018-12-14 | |
Well Total Depth: 22135.00 ft | |
Configuration: Horizontal | |
Latitude: 39.960000 | |
Longitude: -80.840000 |
For data sources see[1]
Well Status | Well Status Date | Comment |
---|---|---|
APP | 2018-08-24 | Proposed Formations:POINT PLEASANT, Issued Date:8/24/2018, Expired Date:8/23/2020 12:00:00 PM, Drilling unit acres:288.945, Proposed Well Type:OG, Proposed Well Class:POOL |
APP | 2018-09-21 | Proposed Formations:POINT PLEASANT, Issued Date:9/21/2018, Expired Date:9/20/2020 12:00:00 PM, Drilling unit acres:288.945, Proposed Well Type:OG, Proposed Well Class:POOL |
Reached Total Depth | 2018-12-14 | |
Record Last Modified | 2019-01-29 | |
Construction Permit Expires | 2020-09-20 |
For data sources see[2]
Perforation Date | Interval Top (ft) | Interval Base (ft) | Number of Shots |
---|---|---|---|
10794 | 10957 | 0 | |
21756 | 21920 | 0 | |
10794 | 10957 | 0 |
For data sources see[3]
Inspection ID | Inspection Date | Inspection Type | Inspection Result | Inspection Comments |
---|---|---|---|---|
-1770185666 | 2020-4-16 0:00: | PL | No Violations | 0.20 |
-435986184 | 2018-11-15 0:00 | DD | No Violations | 1.50 |
0435986184 | 2018-11-15 | Drill / Deepen / Reopen | No Violations | On the day of my inspection I witnessed that Patterson UTI 579 had drilled a 12.25-inch diameter section of the well bore to 9000 feet. While running the 9.625-inch diameter casing they became hung in the hole at 8,914 feet and were no longer able to circulate. XTO company man Levi Grover informed me that they plan to bring a wireline service company in and perforate the 9.625-inch diameter casing at 8847 feet which is 22 feet above the float collar and try and re-establish circulation. If they can re-establish circulation they will proceed with cementing the 9.625-inch diameter casing. I informed Levi Grover to keep me informed on all progress forward with the well. |
1629311290 | 2019-8-27 0:00: | PW | No Violations | 0.30 |
For data sources see[4]