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34-013-21365

Well Details

Well ID: 34-013-21365
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Country: United States
State: Ohio
County: Belmont
Municipality: Mead Township
Operator Name: XTO ENERGY INC.
Well Pad ID: US-OH-001341
Farm/Lease Name: KRNYAICH UNIT C
License Status: Producing
License Date: 2018-09-21
Spud Date: 2018-08-11
Spud Drilling Contractor: PATTERSON DRILLING
Final Drill Date: 2018-12-14
Well Total Depth: 22135.00 ft
Configuration: Horizontal
Latitude: 39.960000
Longitude: -80.840000

For data sources see[1]

Well History

Well Status Well Status Date Comment
APP 2018-08-24 Proposed Formations:POINT PLEASANT, Issued Date:8/24/2018, Expired Date:8/23/2020 12:00:00 PM, Drilling unit acres:288.945, Proposed Well Type:OG, Proposed Well Class:POOL
APP 2018-09-21 Proposed Formations:POINT PLEASANT, Issued Date:9/21/2018, Expired Date:9/20/2020 12:00:00 PM, Drilling unit acres:288.945, Proposed Well Type:OG, Proposed Well Class:POOL
Reached Total Depth 2018-12-14
Record Last Modified 2019-01-29
Construction Permit Expires 2020-09-20

For data sources see[2]

Perforation Treatments

Perforation Date Interval Top (ft) Interval Base (ft) Number of Shots
10794 10957 0
21756 21920 0
10794 10957 0

For data sources see[3]

Inspection Data

Inspections Performed

Inspection ID Inspection Date Inspection Type Inspection Result Inspection Comments
-1770185666 2020-4-16 0:00: PL No Violations 0.20
-435986184 2018-11-15 0:00 DD No Violations 1.50
0435986184 2018-11-15 Drill / Deepen / Reopen No Violations On the day of my inspection I witnessed that Patterson UTI 579 had drilled a 12.25-inch diameter section of the well bore to 9000 feet. While running the 9.625-inch diameter casing they became hung in the hole at 8,914 feet and were no longer able to circulate. XTO company man Levi Grover informed me that they plan to bring a wireline service company in and perforate the 9.625-inch diameter casing at 8847 feet which is 22 feet above the float collar and try and re-establish circulation. If they can re-establish circulation they will proceed with cementing the 9.625-inch diameter casing. I informed Levi Grover to keep me informed on all progress forward with the well.
1629311290 2019-8-27 0:00: PW No Violations 0.30

For data sources see[4]

References