X

Track changes made to this page

If you find this page useful and would like to be notified of changes made to this page, start by inputting your email below.



Privacy policy
Close this window

powered by ChangeDetection

34-019-20437

Well Details

Well ID: 34-019-20437
Loading map...
Country: United States
State: Ohio
County: Carroll
Municipality: Rose Township
Operator Name: WILLIAM S MILLER INC
Well Pad ID:
Farm/Lease Name: GROSENBAUGH
License Status: Producing
License Date: 2018-07-30
Spud Date: 1969-11-25
Spud Drilling Contractor:
Final Drill Date: 1970-03-19
Well Total Depth: 5450.00 ft
Configuration: Vertical
Latitude: 40.610000
Longitude: -81.250000

For data sources see[1]

Well History

Well Status Well Status Date Comment
CO 1969-05-20 311 STOCKER & SITLER INC GeoDate 5/20/69
Original Spud 1969-11-25 UPDATED LOCATION PER DOGRM SURVEYOR 10/15/18 ALE.
Completed 1970-03-19 UPDATED LOCATION PER DOGRM SURVEYOR 10/15/18 ALE.
Reached Total Depth 1970-03-19 UPDATED LOCATION PER DOGRM SURVEYOR 10/15/18 ALE.
Change of Owner 1999-07-20 Operator changed from 311, STOCKER & SITLER INC to 5785, M-J OIL COMPANY INC.
Change of Owner 2001-03-13 Operator changed from 5785, M-J OIL COMPANY INC. to 5894, G & O RESOURCES LTD
Change of Owner 2012-04-10 Operator changed from 5894, G & O RESOURCES LTD to 2512, MILLER WILLIAM S INC
APP 2018-07-30 Proposed Formations:CLINTON, Issued Date:7/30/2018, Expired Date:7/29/2020 12:00:00 PM, Drilling unit acres:160.98, Proposed Well Type:OG, Proposed Well Class:
Record Last Modified 2018-10-15 UPDATED LOCATION PER DOGRM SURVEYOR 10/15/18 ALE.
Construction Permit Expires 2020-07-29 UPDATED LOCATION PER DOGRM SURVEYOR 10/15/18 ALE.

For data sources see[2]

Stimulations Data

Stimulation Date Chemical Agent Chemical Agent Concentration (%) Fracking Fluid Volume Mass of Proppant Used (lb) Fracking Company Comments
H2O 0 1525 Bbl 62500

For data sources see[3]

Production Data

Period Operator Name Gas Quantity (mcf) Oil Quantity (bbl) Production Days
1984 STOCKER & SITLER INC 322.00 373.00 365
1985 STOCKER & SITLER INC 1224.00 481.00 0
1986 STOCKER & SITLER INC 842.00 278.00 365
1987 STOCKER & SITLER INC 647.00 305.00 365
1988 STOCKER & SITLER INC 559.00 323.00 0
1989 STOCKER & SITLER INC 423.00 256.00 365
1990 STOCKER & SITLER INC 969.00 556.00 365
1991 STOCKER & SITLER INC 600.00 367.00 365
1992 STOCKER & SITLER INC 527.00 263.00 365
1993 STOCKER & SITLER INC 576.00 252.00 365
1994 STOCKER & SITLER INC 839.00 279.00 0
1995 STOCKER & SITLER INC 13.00 229.00 0
1996 STOCKER & SITLER INC 0.00 0.00 0
1997 STOCKER & SITLER INC 0.00 0.00 365
1998 STOCKER & SITLER INC 179.00 159.00 365
1999 M-J OIL COMPANY INC. 62.00 43.00 100
2000 M-J OIL COMPANY INC. 69.00 154.00 365
2001 M-J OIL COMPANY INC. 0.00 43.00 49
2002 G & O RESOURCES LTD 0.00 47.00 365
2003 G & O RESOURCES LTD 0.00 53.00 365
2004 G & O RESOURCES LTD 0.00 34.00 365
2005 G & O RESOURCES LTD 0.00 0.00 0
2006 G & O RESOURCES LTD 0.00 0.00 0
2007 G & O RESOURCES LTD 0.00 0.00 0
2008 G & O RESOURCES LTD 0.00 18.00 366
2009 G & O RESOURCES LTD 0.00 0.00 0
2010 G & O RESOURCES LTD 0.00 11.00 365
2012 WILLIAM S MILLER INC 0.00 0.00 0
2013 WILLIAM S MILLER INC 0.00 0.00 0
2014 WILLIAM S MILLER INC 0.00 0.00 0
2015 G & O RESOURCES LTD 0.00 0.00 0
2016 WILLIAM S MILLER INC 0.00 0.00 0
2017 WILLIAM S MILLER INC 0.00 0.00 0
2018 WILLIAM S MILLER INC 0.00 0.00 0

For data sources see[4] [5]

Waste Data

Period Operator Name Waste Type Quantity (bbl) Production Days
1984 STOCKER & SITLER INC Brine 0 365
1985 STOCKER & SITLER INC Brine 0 0
1986 STOCKER & SITLER INC Brine 0 365
1987 STOCKER & SITLER INC Brine 0 365
1988 STOCKER & SITLER INC Brine 0 0
1989 STOCKER & SITLER INC Brine 0 365
1990 STOCKER & SITLER INC Brine 0 365
1991 STOCKER & SITLER INC Brine 0 365
1992 STOCKER & SITLER INC Brine 0 365
1993 STOCKER & SITLER INC Brine 0 365
1994 STOCKER & SITLER INC Brine 0 0
1995 STOCKER & SITLER INC Brine 0 0
1996 STOCKER & SITLER INC Brine 0 0
1997 STOCKER & SITLER INC Brine 162 365
1998 STOCKER & SITLER INC Brine 59 365
1999 STOCKER & SITLER INC Brine 0 365
2000 M-J OIL COMPANY INC. Brine 170 365
2001 M-J OIL COMPANY INC. Brine 17 49
2002 G & O RESOURCES LTD Brine 124 365
2003 G & O RESOURCES LTD Brine 15 365
2004 G & O RESOURCES LTD Brine 9 365
2005 G & O RESOURCES LTD Brine 0 0
2006 G & O RESOURCES LTD Brine 7 0
2007 G & O RESOURCES LTD Brine 0 0
2008 G & O RESOURCES LTD Brine 11 366
2009 G & O RESOURCES LTD Brine 17 0
2010 G & O RESOURCES LTD Brine 0 365
2012 WILLIAM S MILLER INC Brine 0 0
2013 WILLIAM S MILLER INC Brine 0 0
2014 WILLIAM S MILLER INC Brine 0 0
2015 WILLIAM S MILLER INC Brine 0 0
2016 WILLIAM S MILLER INC Brine 0 0
2017 WILLIAM S MILLER INC Brine 0 0
2018 WILLIAM S MILLER INC Brine 0 0

For data sources see[6] [7]

Inspection Data

Inspections Performed

Inspection ID Inspection Date Inspection Type Inspection Result Inspection Comments
0957939803 2013-08-22 Production Wells No Violations My inspection of the tank battery associated with this well found the following: Brine scalding on the west side of the tank battery outside of the dike. It appears the dump line has come free from the top of the brine tank and is dumping onto the ground. There was free crude oil and brine inside the dike. The valve tree were the four wells come into the tank battery is leaking. The soil around the valves is saturated with oil and brine. The west side of the dike, inside of the battery is stained with oil and brine. The following needs completed by 09/03/2013. All oil contaminated soil needs removed from in and around the tank battery. All necessary repairs to the battery need to be made to prevent the release of oil and brine. Identification for all wells produced into the battery needs to be posted with updated contact information.
1378403123 2013-09-05 UrbanProduction Wells No Violations Follow up to inspection on 08/22/13: Tank battery in question with oil staining and free crude oil is not the tank battery for this well. This well used to be produced into this tank battery. The tank battery is believed to belong to the Grosenbaugh #1 and #4. If this is the case the tank battery belongs to G & O Resources. G & O Resources has been contacted.
1432822534 2015-05-19 Production Wells Violations Noted Inspection shows the well is equipped with a electrical pump jack. The tubing valve is fully open and the production casing valve is partially open. The pressure gauge on the tubing reads 0. The pressure gauge on the production casing is broken. There is not a line for domestic gas. The identification sign on the electric box shows G & O as the owner and is faded. The electric timer is not operating. Division of Oil and Gas records show William Miller as the owner. Division of Oil and Gas records show 0 production from 2012 through 2014. 2011 production records are missing from the Divisions records. Division records show 0 barrels of oil and 0 mcf gas produced between 2005 and 2007, 18 bbls. of oil and 0 mcf of gas in 2008 and 11 barrels of oil and 0 mcf gas in 2010. This well shared a tank battery with P. 435, 436 and 438 between 2005 and 2010.These wells reported the same production. Dave Wittuck w/ G & O thinks this may still be owned by G & O and may be plugged in the near future. William Miller and G & O will need to determine ownership. The tank battery that this well produced into is dismantled due to a recent clean up of oil inside the dike.
1461534907 2018-11-7 0:00: PW No Violations
1559137392 2019-05-07 Production Wells No Violations I conducted a compliance-notice follow-up on the well which was issued for non-production. Identification was posted. The production valve appeared to be in the closed position. I did not locate a tank battery associated with this well. No production has been reported and the compliance notice remains open. I spoke to the operator regarding the plugging status of the well, and was informed that the well is on the list to plug.
1582649927 2020-2-24 0:00: PW No Violations 0.50
1902514079 2017-03-08 Production Wells No Violations I spoke to David Miller of William S. Miller Inc. on 03/08/2017 regarding the plugging status of the well. He informed me that this well is on the list to be plugged and is hoping to start plugging operations in 2017.
957939803 2013-8-22 0:00: PW No Violations

Violations Commited

Inspection ID Violation ID Violation Date Violation Code Violation Comments
1432822534 US-OH-112660 2015-08-03 Failure to legibly identify well
1432822534 US-OH-112661 2015-08-03 Well shall be plugged

For data sources see[8]

References