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34-019-20438

Well Details

Well ID: 34-019-20438
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Country: United States
State: Ohio
County: Carroll
Municipality: Rose Township
Operator Name: G & O RESOURCES LTD
Well Pad ID:
Farm/Lease Name: GROSENBAUGH WM E ETAL UNIT
License Status: Producing
License Date: 1969-05-20
Spud Date: 1969-08-18
Spud Drilling Contractor:
Final Drill Date: 1969-08-27
Well Total Depth: 5440.00 ft
Configuration: Vertical
Latitude: 40.610000
Longitude: -81.240000

For data sources see[1]

Well History

Well Status Well Status Date Comment
CO 1969-05-20 311 STOCKER & SITLER INC GeoDate 5/20/69
Original Spud 1969-08-18
Completed 1969-08-27
Reached Total Depth 1969-08-27
Change of Owner 1999-07-20 Operator changed from 311, STOCKER & SITLER INC to 5785, M-J OIL COMPANY INC.
Change of Owner 2001-03-13 Operator changed from 5785, M-J OIL COMPANY INC. to 5894, G & O RESOURCES LTD
Record Last Modified 2013-12-31

For data sources see[2]

Perforation Treatments

Perforation Date Interval Top (ft) Interval Base (ft) Number of Shots
2006-09-11 5274 5331 2
5274 5331 2
5274 5331 2

For data sources see[3]

Stimulations Data

Stimulation Date Chemical Agent Chemical Agent Concentration (%) Fracking Fluid Volume Mass of Proppant Used (lb) Fracking Company Comments
H2O 0 1715 Bbl 74000

For data sources see[4]

Production Data

Period Operator Name Gas Quantity (mcf) Oil Quantity (bbl) Production Days
1984 STOCKER & SITLER INC 323.00 373.00 365
1985 STOCKER & SITLER INC 1225.00 481.00 0
1986 STOCKER & SITLER INC 842.00 278.00 365
1987 STOCKER & SITLER INC 647.00 305.00 365
1988 STOCKER & SITLER INC 560.00 323.00 0
1989 STOCKER & SITLER INC 591.00 434.00 365
1990 STOCKER & SITLER INC 1138.00 734.00 365
1991 STOCKER & SITLER INC 600.00 367.00 365
1992 STOCKER & SITLER INC 528.00 263.00 365
1993 STOCKER & SITLER INC 576.00 252.00 365
1994 STOCKER & SITLER INC 654.00 221.00 0
1998 STOCKER & SITLER INC 0.00 43.00 365
1999 M-J OIL COMPANY INC. 0.00 43.00 100
2000 M-J OIL COMPANY INC. 69.00 154.00 365
2001 M-J OIL COMPANY INC. 0.00 43.00 49
2002 G & O RESOURCES LTD 0.00 47.00 365
2003 G & O RESOURCES LTD 0.00 53.00 365
2004 G & O RESOURCES LTD 0.00 34.00 365
2005 G & O RESOURCES LTD 0.00 0.00 0
2006 G & O RESOURCES LTD 0.00 0.00 0
2007 G & O RESOURCES LTD 0.00 0.00 0
2008 G & O RESOURCES LTD 0.00 18.00 366
2009 G & O RESOURCES LTD 0.00 0.00 0
2010 G & O RESOURCES LTD 0.00 11.00 365
2011 G & O RESOURCES LTD 0.00 0.00 0
2012 G & O RESOURCES LTD 0.00 0.00 0
2013 G & O RESOURCES LTD 0.00 0.00 0
2014 G & O RESOURCES LTD 0.00 0.00 0
2015 G & O RESOURCES LTD 0.00 0.00 0
2016 G & O RESOURCES LTD 0.00 0.00 0
2017 G & O RESOURCES LTD 0.00 0.00 0

For data sources see[5] [6]

Waste Data

Period Operator Name Waste Type Quantity (bbl) Production Days
1984 STOCKER & SITLER INC Brine 0 365
1985 STOCKER & SITLER INC Brine 0 0
1986 STOCKER & SITLER INC Brine 0 365
1987 STOCKER & SITLER INC Brine 0 365
1988 STOCKER & SITLER INC Brine 0 0
1989 STOCKER & SITLER INC Brine 0 365
1990 STOCKER & SITLER INC Brine 0 365
1991 STOCKER & SITLER INC Brine 0 365
1992 STOCKER & SITLER INC Brine 0 365
1993 STOCKER & SITLER INC Brine 0 365
1994 STOCKER & SITLER INC Brine 0 0
1998 STOCKER & SITLER INC Brine 25 365
1999 M-J OIL COMPANY INC. Brine 19 100
2000 M-J OIL COMPANY INC. Brine 170 365
2001 M-J OIL COMPANY INC. Brine 17 49
2002 G & O RESOURCES LTD Brine 124 365
2003 G & O RESOURCES LTD Brine 15 365
2004 G & O RESOURCES LTD Brine 9 365
2005 G & O RESOURCES LTD Brine 0 0
2006 G & O RESOURCES LTD Brine 7 0
2007 G & O RESOURCES LTD Brine 0 0
2008 G & O RESOURCES LTD Brine 11 366
2009 G & O RESOURCES LTD Brine 17 0
2010 G & O RESOURCES LTD Brine 0 365
2011 G & O RESOURCES LTD Brine 0 0
2012 G & O RESOURCES LTD Brine 0 0
2013 G & O RESOURCES LTD Brine 0 0
2014 G & O RESOURCES LTD Brine 0 0
2015 G & O RESOURCES LTD Brine 5 0
2016 G & O RESOURCES LTD Brine 0 0
2017 G & O RESOURCES LTD Brine 0 0

For data sources see[7] [8]

Inspection Data

Inspections Performed

Inspection ID Inspection Date Inspection Type Inspection Result Inspection Comments
-1822462555 2013-8-22 0:00: AM No Violations
-550254584 2013-8-23 0:00: PW No Violations
-595081306 2018-9-20 0:00: PW No Violations
0407676743 2017-11-02 Production Wells No Violations I conducted a follow-up inspection to the compliance notice that was issued on 11/10/2015 to plug the well. No changes have been made to the well since my last inspection and the well is not equipped with production equipment. Reported production for the well has been zero since 2010. I contacted G&O Resources on 11/08/2017 and requested a call-back to discuss plugging operations of the well.
0550254584 2013-08-23 Production Wells No Violations The well was surrounded by a small fence and the grass had grown up over top of the well. There was no tank battery visible from the site and the lease road did not continue all the way to the site, which is located in a pasture. There has been no production recorded for this well since 2004, and the last production was only brine.
0595081306 2018-09-20 Production Wells No Violations A compliance notice was issued to plug this well on 10/15/2015. The tank battery consisted of one 100 bbl production tank and was overgrown with vegetation. The well access road was heavily overgrown with vegetation and I was unable to get to the well at the time of inspection. The compliance notice to plug the well remains open. The last reported production was 11 bbls in 2010. I will be meeting with the operator to discuss a plugging schedule.
1093827122 2015-10-15 Production Wells Violations Noted

-11-05(B), and the well plugged within 180 days. The well owner/operator will be notified if the plugging schedule is approved or denied.

1424127746 2017-09-20 Production Wells No Violations I followed up at the tank battery regarding the compliance notice issued on 05/22/2018 for multiple issues at the tank battery. The tank battery was overgrown with vegetation, but the given issues in the compliance notice at the tank battery have been resolved. The tank battery consitsed of one 100 bbl production tank and was surrounded by a dike. This well was properly identified. This compliance notice can be closed.
1429198438 2015-03-30 Production Wells Violations Noted

-210 bbl oil production tank, two-100 bbl. Brine tanks, and a heater treater separator. Inspection of the tank battery revealed a label indicating the production equipment is shared by G & O Resources PN #(438, 436, 438). There was an oil stain measuring 76 inches by 14 inches surrounding one of the tanks, and there was free crude oil pooled at the base of the heater treater. The dike was breached and not sufficient for containment. Tank fluid leakage was evident from significant dead vegetation in the land adjacent to tank battery and in the pasture surrounding the dike. Oil has breached the dike and has pooled in an area measuring 20 feet by 12 feet. There was no bull plug on the valve of the production tank. The gas meter at the tank battery contained no chart. Identification with permit numbers was not present at the tank battery. RBDMS shows there has been no reported production for this well since 2010, which was 11 bbls. Due to well operation causing pollution, failure to have required bull plugs, the dike not able to prevent escape of brine, and proper identification not posted at the tank battery, a Compliance Notice is being issued. The oil and brine and impacted soil around the tank battery must be removed immediately, the leaks at the produc

1453743253 2016-01-25 Production Wells No Violations I conducted a follow-up inspection of this well. There is no change at the well head from my last inspection. The tank battery now consists of one, 100 bbl production tank. The production tank does not appear to be plumbed into the flowline. The dike surrounding the tank battery is in good repair. Proper identification is posted at the tank battery. The compliance notice to plug the well remains open.
1559146840 2019-4-24 0:00: PW No Violations 0.90
1716763375 2015-06-30 Production Wells No Violations I conducted a compliance follow-up inspection of the tank battery. All production equipment expect the meter run, the valve system, and one, 100 barrel production tank had been removed. A new dike had been constructed and housed the valve system. The production tank located outside of the dike, and was not attached to any equipment at the time of inspection. All of the impacted soil had been removed. I spoke to Ron Hammon from Lakeside Excavating, who is a contractor for G&O. He informed me that they will be moving the production tank inside of the dike and hooking up the production equipment. I will follow up during the week of 07/27/2015
1822462555 2013-08-22 Administrative Inspection No Violations Review of the well file shows that last reported production for this well was in 2010. Production that year was 11 barrels. The well has made a total of 29 barrels of oil since 2005. This well either needs to be put back into production or plugged. I will be having a meeting with the operator to discuss the well on 08/30/13.
407676743 2017-11-2 0:00: PW No Violations

Violations Commited

Inspection ID Violation ID Violation Date Violation Code Violation Comments
1093827122 US-OH-102217 2018-11-16 NONE Well shall be plugged
1429198438 US-OH-112547 2018-11-13 9-1-07 Well operation causing pollution and contamination
1429198438 US-OH-112548 2018-11-13 9-9-02 General Safety
1429198438 US-OH-112549 2018-11-13 9-9-05(A)10 Failure to legibly identify well
1429198438 US-OH-112550 2018-11-13 9-9-05(A)9 No SPCC dike/or failure to keep dike free of water or oil
1429198438 US-OH-112551 2018-11-13 9-9-05(D) Failure to have required locks, bull plugs

For data sources see[9]

References