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Well ID: 34-019-21848 | Loading map...
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Country: United States | |
State: Ohio | |
County: Carroll | |
Municipality: Union Township | |
Operator Name: 3200 SCIO, LLC | |
Well Pad ID: | |
Farm/Lease Name: LUCE EDWARD & CARMELLA & M J | |
License Status: Domestic Well | |
License Date: 1995-09-22 | |
Spud Date: 1995-11-07 | |
Spud Drilling Contractor: ADVENT DRLG | |
Final Drill Date: 1995-11-12 | |
Well Total Depth: 6084.00 ft | |
Configuration: Vertical | |
Latitude: 40.520000 | |
Longitude: -81.110000 |
For data sources see[1]
Well Status | Well Status Date | Comment |
---|---|---|
CO | 1995-09-22 | 1388 NORTH COAST ENERGY INC GeoDate 9/22/95 |
Oil and Gas | 1995-09-22 | Issued Date 9/22/95 Expired Date 9/21/96 Acres 0040000 Tool Type RTAF Proposed Formation CLINTON Proposed Depth 06084 Proposed Drill Depth 06084 |
Original Spud | 1995-11-07 | CHANGED STATUS OF WELL FROM PR TO DM PER TRANSFER FROM ENERVEST OPERATING LLC #7578 TO OWNER ON 6/16/2016 CM. |
Completed | 1995-11-12 | CHANGED STATUS OF WELL FROM PR TO DM PER TRANSFER FROM ENERVEST OPERATING LLC #7578 TO OWNER ON 6/16/2016 CM. |
Reached Total Depth | 1995-11-12 | CHANGED STATUS OF WELL FROM PR TO DM PER TRANSFER FROM ENERVEST OPERATING LLC #7578 TO OWNER ON 6/16/2016 CM. |
Completion Report Received | 1996-03-22 | CHANGED STATUS OF WELL FROM PR TO DM PER TRANSFER FROM ENERVEST OPERATING LLC #7578 TO OWNER ON 6/16/2016 CM. |
Construction Permit Expires | 1996-09-21 | CHANGED STATUS OF WELL FROM PR TO DM PER TRANSFER FROM ENERVEST OPERATING LLC #7578 TO OWNER ON 6/16/2016 CM. |
Change of Owner | 2009-12-14 | Operator changed from 1388, EXCO - NORTH COAST ENERGY INC to 7578, ENERVEST OPERATING LLC |
Change of Owner | 2016-06-16 | Operator changed from 7578, ENERVEST OPERATING LLC to 9695, 3200SCIO, LLC |
Record Last Modified | 2017-02-15 | CHANGED STATUS OF WELL FROM PR TO DM PER TRANSFER FROM ENERVEST OPERATING LLC #7578 TO OWNER ON 6/16/2016 CM. |
For data sources see[2]
Perforation Date | Interval Top (ft) | Interval Base (ft) | Number of Shots |
---|---|---|---|
1997-06-29 | 5797 | 5890 | 0 |
5797 | 5890 | 0 | |
2006-09-11 | 5821 | 5890 | 33 |
5821 | 5890 | 33 | |
5797 | 5890 | 0 |
For data sources see[3]
Stimulation Date | Chemical Agent | Chemical Agent Concentration (%) | Fracking Fluid Volume | Mass of Proppant Used (lb) | Fracking Company | Comments |
---|---|---|---|---|---|---|
H2O | 0 | 69500 Gal | 120000 | FRAC W/69.5M GAL H20 & 120M# SAND |
For data sources see[4]
Period | Operator Name | Gas Quantity (mcf) | Oil Quantity (bbl) | Production Days |
---|---|---|---|---|
1997 | EXCO - NORTH COAST ENERGY INC | 0.00 | 0.00 | 365 |
2000 | EXCO - NORTH COAST ENERGY INC | 0.00 | 0.00 | 0 |
2001 | EXCO - NORTH COAST ENERGY INC | 0.00 | 0.00 | 0 |
2002 | EXCO - NORTH COAST ENERGY INC | 0.00 | 0.00 | 0 |
2003 | EXCO - NORTH COAST ENERGY INC | 2191.00 | 0.00 | 335 |
2004 | EXCO - NORTH COAST ENERGY INC | 1054.00 | 63.00 | 365 |
2005 | EXCO - NORTH COAST ENERGY INC | 587.00 | 67.00 | 365 |
2006 | EXCO - NORTH COAST ENERGY INC | 563.00 | 0.00 | 365 |
2007 | EXCO - NORTH COAST ENERGY INC | 137.00 | 0.00 | 365 |
2008 | EXCO - NORTH COAST ENERGY INC | 0.00 | 0.00 | 366 |
2009 | EXCO - NORTH COAST ENERGY INC | 41.00 | 0.00 | 365 |
2010 | ENERVEST OPERATING LLC | 348.00 | 0.00 | 365 |
2011 | ENERVEST OPERATING LLC | 312.00 | 39.00 | 0 |
2012 | ENERVEST OPERATING LLC | 404.00 | 0.00 | 366 |
2013 | ENERVEST OPERATING LLC | 255.00 | 0.00 | 365 |
2014 | ENERVEST OPERATING LLC | 402.00 | 0.00 | 365 |
2015 | ENERVEST OPERATING LLC | 1495.00 | 8.00 | 352 |
2016 | ENERVEST OPERATING LLC | 99.00 | 0.00 | 167 |
Period | Operator Name | Waste Type | Quantity (bbl) | Production Days |
---|---|---|---|---|
1997 | EXCO - NORTH COAST ENERGY INC | Brine | 0 | 365 |
2000 | EXCO - NORTH COAST ENERGY INC | Brine | 0 | 0 |
2001 | EXCO - NORTH COAST ENERGY INC | Brine | 0 | 0 |
2002 | EXCO - NORTH COAST ENERGY INC | Brine | 0 | 0 |
2003 | EXCO - NORTH COAST ENERGY INC | Brine | 376 | 335 |
2004 | EXCO - NORTH COAST ENERGY INC | Brine | 97 | 365 |
2005 | EXCO - NORTH COAST ENERGY INC | Brine | 30 | 365 |
2006 | EXCO - NORTH COAST ENERGY INC | Brine | 0 | 365 |
2007 | EXCO - NORTH COAST ENERGY INC | Brine | 0 | 365 |
2008 | EXCO - NORTH COAST ENERGY INC | Brine | 0 | 366 |
2009 | EXCO - NORTH COAST ENERGY INC | Brine | 31 | 365 |
2010 | ENERVEST OPERATING LLC | Brine | 37 | 365 |
2011 | ENERVEST OPERATING LLC | Brine | 41 | |
2012 | ENERVEST OPERATING LLC | Brine | 0 | 366 |
2013 | ENERVEST OPERATING LLC | Brine | 15 | 365 |
2014 | ENERVEST OPERATING LLC | Brine | 0 | 365 |
2015 | ENERVEST OPERATING LLC | Brine | 56 | 352 |
2016 | ENERVEST OPERATING LLC | Brine | 16 | 167 |
Inspection ID | Inspection Date | Inspection Type | Inspection Result | Inspection Comments |
---|---|---|---|---|
-1271522459 | 2016-3-3 0:00:0 | EX | No Violations | 1.00 |
001288i411 | 2002-03-25 | Preliminary Restoration | No Violations | Preliminary restoration approved ; no violations at this time . |
0469372848 | 2016-02-25 | Exempt Well Pre Transfer | No Violations | I conducted an exempt well, pre-transfer inspection with DOGRM District Supervisor Rick Anderson. We were on site with Dennis Kiko, the landowner. The well is equipped with a plunger--up to the well during my inspection, but the landowner informed me that he intends to run a domestic line to heat his barn. The tank battery consists of one 100 bbl production tank, a horizontal separator, and a meter run. There was a gas odor in the air around the separator. We spoke to the landowner, and the well is located on property that is greater than five acres. There are dwellings located on an adjacent parcel of property, and are at a distance of approximately 240 feet to the northeast, 246 feet to the northwest, and approximately 312 feet to the northwest. The operator will be contacted regarding fixing the small leaks, and cleaning up the oil on the wellhead. |
1271522459 | 2016-03-03 | Exempt Well Pre Transfer | No Violations | I conducted a follow-up inspection of the well and tank battery. The operator was contacted on 03/01/2016 in regards to the issues that were found at the well and tank battery during the inspection on 02/25/2016. The leak at the well head has been repaired, and no contaminated soil was visible around the well. No leaks were detected at the well. The apparent gas leak at the separator has been repaired, as no leaks or gas odor were detected around the equipment. No violations were found at the well or tank battery. |
1288i411 | 2002-3-25 0:00: | PL | No Violations | 1.00 |
1462892862 | 2016-05-05 | Exempt Well Pre Transfer | No Violations | I conducted a follow-up to my exempt, pre-transfer inspection conducted on 02/25/2016. The well is equipped with a plunger lift system. A domestic gas connection at the well has been constructed. No leaks were detected at the well or tank battery. No violations were found. |
2135162343 | 2015-03-11 | Exempt Well Pre Transfer | No Violations | I conducted an exempt well, pre-transfer inspection of this Clinton Sandstone well. I attempted to contact the landowner (transferee) and the phone number I was given was disconnected. I inspected the wellhead and found the well equipped with a plunger-lift system. The Logic controls for the plunger system were not functioning at the time of my inspection. Gauges indicated 950psi on the 4.5 production casing and 825psi on the 1.5 tubing. The 8.625 surface casing was above graded and gas was leaking (bubbling) through the packing and slips in the annulus between the surface and production casing strings. There is no gauge on the 8.625 casing and the valve is shut. I inspected the tank battery and found that it was diked and contained one (1) 100 barrel tank, a horizontal separator, and an old line heater that was disconnected. The 100 barrel tank is rusted and was half full of an unknown fluid (oil or brine) and needs to be emptied. There is an odor of methane at the separator that also needs to be addressed. The flow line is open into the separator and the valve on the sales line out of the tank battery is also open. I found no domestic hook-up at the wellhead or tank battery and need to verify the domestic hook-up and that the sales line is not producing into a commercial line. Due to the leaking annulus at the wellhead, issues I found at the tank battery, and the need to verify the domestic gas hook-up, I cannot approve the domestic transfer at this time. I will have Enervest address the issues I found and approve the transfer after the issues are properly addressed. |
469372848 | 2016-2-25 0:00: | EX | No Violations | 1.50 |
For data sources see[9]