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Well ID: 34-029-21046 | Loading map...
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Country: United States | |
State: Ohio | |
County: Columbiana | |
Municipality: West Township | |
Operator Name: DIVERSIFIED PRODUCTION LLC | |
Well Pad ID: | |
Farm/Lease Name: PICKNELL-MILLER UNIT | |
License Status: Producing | |
License Date: 1984-06-28 | |
Spud Date: 1984-09-18 | |
Spud Drilling Contractor: SHERMAN DRLG | |
Final Drill Date: 1984-09-22 | |
Well Total Depth: 5821.00 ft | |
Configuration: Vertical | |
Latitude: 40.770000 | |
Longitude: -81.030000 |
For data sources see[1]
Well Status | Well Status Date | Comment |
---|---|---|
CO | 1984-06-28 | 43 RESOURCE AMERICA INC GeoDate 6/28/84 |
Oil and Gas | 1984-06-28 | Issued Date 6/28/84 Expired Date 12/25/84 Acres 0040000 Tool Type RTAF Proposed Formation CLINTON Proposed Depth 05821 Proposed Drill Depth 05821 |
Original Spud | 1984-09-18 | |
Completed | 1984-09-22 | |
Reached Total Depth | 1984-09-22 | |
Completion Report Received | 1984-10-15 | |
Construction Permit Expires | 1984-12-25 | |
Change of Owner | 2004-03-12 | Operator changed from 43, RESOURCE AMERICA INC to 6867, ATLAS AMERICA INC |
Change of Owner | 2011-01-27 | Operator changed from 6867, ATLAS AMERICA LLC to 6866, ATLAS NOBLE LLC |
Change of Owner | 2011-02-08 | Operator changed from 6867, ATLAS AMERICA LLC to 6866, ATLAS NOBLE LLC |
Change of Owner | 2017-10-17 | Operator changed from 6866, ATLAS NOBLE LLC to 8685, M & R INVESTMENTS OHIO LLC |
Record Last Modified | 2017-10-17 |
For data sources see[2]
Perforation Date | Interval Top (ft) | Interval Base (ft) | Number of Shots |
---|---|---|---|
1997-06-29 | 5588 | 5736 | 0 |
5588 | 5736 | 0 | |
2006-09-11 | 5608 | 5736 | 35 |
5608 | 5736 | 35 | |
5588 | 5736 | 0 |
For data sources see[3]
Stimulation Date | Chemical Agent | Chemical Agent Concentration (%) | Fracking Fluid Volume | Mass of Proppant Used (lb) | Fracking Company | Comments |
---|---|---|---|---|---|---|
H2O | 0 | 120000 Gal | 80000 | FRAC: H2O,SAND |
For data sources see[4]
Period | Operator Name | Gas Quantity (mcf) | Oil Quantity (bbl) | Production Days |
---|---|---|---|---|
1984 | LANGASCO ENERGY CORP | 739.00 | 202.00 | 0 |
1985 | LANGASCO ENERGY CORP | 11436.00 | 2148.00 | 365 |
1986 | LANGASCO ENERGY CORP | 4821.00 | 904.00 | 365 |
1987 | LANGASCO ENERGY CORP | 2717.00 | 702.00 | 365 |
1990 | RESOURCE AMERICA INC | 650.00 | 183.00 | 228 |
1991 | RESOURCE AMERICA INC | 1665.00 | 560.00 | 365 |
1993 | RESOURCE AMERICA INC | 2206.00 | 566.00 | 365 |
1994 | RESOURCE AMERICA INC | 3059.00 | 590.00 | 365 |
1995 | RESOURCE AMERICA INC | 2770.00 | 395.00 | 365 |
1996 | RESOURCE AMERICA INC | 1501.00 | 2420.00 | 265 |
1997 | RESOURCE AMERICA INC | 2209.00 | 395.00 | 365 |
1998 | RESOURCE AMERICA INC | 1633.00 | 254.00 | 365 |
1999 | RESOURCE AMERICA INC | 2353.00 | 399.00 | 365 |
2000 | RESOURCE AMERICA INC | 2164.00 | 342.00 | 365 |
2001 | RESOURCE AMERICA INC | 1886.00 | 112.00 | 365 |
2002 | RESOURCE AMERICA INC | 1734.00 | 497.00 | 365 |
2003 | RESOURCE AMERICA INC | 1927.00 | 283.00 | 365 |
2004 | CHEVRON APPALACHIA LLC | 1179.00 | 228.00 | 365 |
2005 | CHEVRON APPALACHIA LLC | 926.00 | 350.00 | 365 |
2006 | CHEVRON APPALACHIA LLC | 1066.00 | 216.00 | 365 |
2007 | CHEVRON APPALACHIA LLC | 1043.00 | 225.00 | 365 |
2008 | CHEVRON APPALACHIA LLC | 918.00 | 276.00 | 366 |
2009 | CHEVRON APPALACHIA LLC | 925.00 | 233.00 | 365 |
2010 | ATLAS NOBLE LLC | 872.00 | 156.00 | 365 |
2011 | CHEVRON APPALACHIA LLC | 749.00 | 180.00 | 365 |
2012 | ATLAS NOBLE LLC | 733.00 | 154.00 | 366 |
2013 | ATLAS NOBLE LLC | 516.00 | 75.00 | 365 |
2014 | ATLAS NOBLE LLC | 512.00 | 163.00 | 365 |
2015 | ATLAS NOBLE LLC | 562.00 | 211.00 | 365 |
2016 | ATLAS NOBLE LLC | 487.00 | 122.00 | 366 |
2017 | M & R INVESTMENTS OHIO LLC | 158.00 | 0.00 | 182 |
2018 | M & R INVESTMENTS OHIO LLC | 529.00 | 46.00 | 365 |
Period | Operator Name | Waste Type | Quantity (bbl) | Production Days |
---|---|---|---|---|
1984 | LANGASCO ENERGY CORP | Brine | 0 | 0 |
1985 | LANGASCO ENERGY CORP | Brine | 450 | 365 |
1986 | LANGASCO ENERGY CORP | Brine | 100 | 365 |
1987 | LANGASCO ENERGY CORP | Brine | 115 | 365 |
1990 | RESOURCE AMERICA INC | Brine | 29 | 228 |
1991 | RESOURCE AMERICA INC | Brine | 0 | 365 |
1993 | RESOURCE AMERICA INC | Brine | 0 | 365 |
1994 | RESOURCE AMERICA INC | Brine | 0 | 365 |
1995 | RESOURCE AMERICA INC | Brine | 0 | 365 |
1996 | RESOURCE AMERICA INC | Brine | 0 | 265 |
1997 | RESOURCE AMERICA INC | Brine | 0 | 365 |
1998 | RESOURCE AMERICA INC | Brine | 77 | 365 |
1999 | RESOURCE AMERICA INC | Brine | 99 | 365 |
2000 | RESOURCE AMERICA INC | Brine | 0 | 365 |
2001 | RESOURCE AMERICA INC | Brine | 0 | 365 |
2002 | RESOURCE AMERICA INC | Brine | 40 | 365 |
2003 | RESOURCE AMERICA INC | Brine | 0 | 365 |
2004 | CHEVRON APPALACHIA LLC | Brine | 33 | 365 |
2005 | CHEVRON APPALACHIA LLC | Brine | 30 | 365 |
2006 | CHEVRON APPALACHIA LLC | Brine | 42 | 365 |
2007 | CHEVRON APPALACHIA LLC | Brine | 34 | 365 |
2008 | CHEVRON APPALACHIA LLC | Brine | 38 | 366 |
2009 | CHEVRON APPALACHIA LLC | Brine | 20 | 365 |
2010 | ATLAS NOBLE LLC | Brine | 7 | 365 |
2011 | CHEVRON APPALACHIA LLC | Brine | 30 | 365 |
2012 | ATLAS NOBLE LLC | Brine | 8 | 366 |
2013 | ATLAS NOBLE LLC | Brine | 0 | 365 |
2014 | ATLAS NOBLE LLC | Brine | 17 | 365 |
2015 | ATLAS NOBLE LLC | Brine | 0 | 365 |
2016 | ATLAS NOBLE LLC | Brine | 20 | 366 |
2017 | ATLAS NOBLE LLC | Brine | 0 | 182 |
2018 | M & R INVESTMENTS OHIO LLC | Brine | 0 | 365 |
Inspection ID | Inspection Date | Inspection Type | Inspection Result | Inspection Comments |
---|---|---|---|---|
-1603725692 | 2013-4-9 0:00:0 | PW | No Violations | |
-2140563422 | 2017-3-28 0:00: | PW | No Violations | 0.60 |
0074077613 | 2002-08-01 | Production Wells | No Violations | Obtained GPS coordinates. EPE - 12. |
1328880237 | 2012-01-31 | Production Wells | No Violations | On 1/31/2012, I performed a status check on the above well site. No violations were noted at this time. |
1580708818 | 2013-03-18 | Production Wells | No Violations | On 03/17/2013 at approximately 10:05pm, I was left a voicemail message from Rusty Morrison of Atlas regarding a reported tank fire at an Atlas site on Knox-School Road. In a subsequent phone conversation at 10:25pm that evening, I discussed the situation with Rusty Morrison. It was his understanding that a 210 bbl storage tank at the Picknell-Miller Unit #1 had caught fire and exploded, blowing the top of the tank off. The local fire department had been summoned to the location, and had extinguished the fire. No oil escaped the tank. There was no oil in the dike. He indicated that all emergency personnel and company personnel were leaving the site. Mr. Morrison indicated he would be at the site at first light on 03/18/2013. At 11:08am on 03/18/2013, I had a phone conversation with Mr. Morrison. He indicated that he had been to the site. OEPA personnel had been to the site, as well as Columbiana County EMA. The current status was that the well was shut in, the equipment that had been blown off was returned to the tank battery. The tank top was retrieved and brought near the tank battery. A neighboring mobile home had experienced window damage, and Mr. Morrison arranged for repairs. Mr. Morrison indicated confirmed that there was no oil spilled, and that the remaining oil in the tank was to be hauled later in the day on 03/18/2013. A cause for the fire and explosion is still undetermined. I went to the site for a follow-up inspection, arriving at approximately 2:00pm on 03/18/2013. I found the situation at the location as Mr. Morrison had described. I walked around the tank battery and took pictures. Additionally, I went to the well head, and found the well shut in. |
1603725692 | 2013-04-09 | Production Wells | No Violations | I went to the site to follow up on the repairs at the tank battery following the 03/17/2013 tank explosion. I found that the damaged 210 bbl tank had been removed, and was replaced with a new 100 bbl tank. The tank had new identification labeling. The dike was in good repair following the tank replacement work. Equipment at the tank battery now includes: horizontal separator, meter box, drip bottle, concrete vault brine tank, 100 bbl storage tank, and a house gas meter assembly. |
1733121120 | 2003-10-10 | Production Wells | No Violations | The tank battery consists of 1-210 bbl storage tank, 1- buried concrete salt water storage tank, 1-separator and a dike. |
2140563422 | 2017-03-28 | Production Wells | No Violations | The purpose of my inspection was to conduct a status check on well #2-1046. Lease access was through a residential driveway that was stable and drivable. The well location was stable with well-established vegetation. Correct and legible identification was present at the well head. The 8.625 well head was above grade and contained a closed valve in both annular side ports. The 4.5 production casing was equipped with a Concoyle production assembly. Production valves were in the open position. No audible or visual leaks were detected. I observed some minor staining on the ground consistent with legacy operations. There was no fresh or active leaking present. The tank battery consisted of one (1) horizontal separator, one (1) 100 bbl production tank and one (1) buried concrete brine tank. The equipment was contained within an earthen dike that was stable and free of fluid. The horizontal separator was in good repair. No audible or visual leaks were detected. The meter house contained a current production chart. Correct and legible identification was present on the tank body. The load line valve was closed, locked and plugged. The drain line valve was closed, locked and plumbed out to the brine tank. The hatch lid was closed. The brine tank above grade was in good repair with no cracks or evidence of overfilling. The drip tank discharge was plumbed into the brine vault. |
74077613 | 2002-8-1 0:00:0 | PW | No Violations | 0.50 |
For data sources see[9]