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34-031-20141

Well Details

Well ID: 34-031-20141
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Country: United States
State: Ohio
County: Coshocton
Municipality: Perry Township
Operator Name: ECLIPSE RESOURCES-OHIO LLC
Well Pad ID:
Farm/Lease Name: WILSON J J
License Status: Final Restoration
License Date: 2014-07-15
Spud Date: 1938-06-09
Spud Drilling Contractor:
Final Drill Date: 1938-07-11
Well Total Depth: 3227.00 ft
Configuration: Vertical
Latitude: 40.270000
Longitude: -82.170000

For data sources see[1]

Well History

Well Status Well Status Date Comment
CO 1801-01-02 79 OXFORD OIL CO
Oil and Gas 1802-01-01
Original Spud 1938-06-09 GL=1090.3
Completed 1938-07-11 GL=1090.3
Reached Total Depth 1938-07-11 GL=1090.3
APP 2010-11-10 Proposed Formations:CLINTON, Issued Date:11/10/2010, Expired Date:11/9/2012 12:00:00 PM, Drilling unit acres:0, Proposed Well Type:OG, Proposed Well Class:
APP 2013-02-06 Proposed Formations:CLINTON, Issued Date:2/6/2013, Expired Date:2/6/2015 12:00:00 PM, Drilling unit acres:80, Proposed Well Type:OG, Proposed Well Class:
Change of Owner 2014-02-06 Operator changed from 79, OXFORD OIL to 9216, ECLIPSE RESOURCES-OHIO LLC
APP 2014-07-15 Proposed Formations:CLINTON, Issued Date:7/15/2014, Expired Date:7/14/2016 12:00:00 PM, Drilling unit acres:80, Proposed Well Type:OG, Proposed Well Class:
Plugged/Abandoned 2015-08-13 GL=1090.3
Record Last Modified 2016-06-17 GL=1090.3
Construction Permit Expires 2016-07-14 GL=1090.3

For data sources see[2]

Perforation Treatments

Perforation Date Interval Top (ft) Interval Base (ft) Number of Shots
2006-09-11 3181 3221 0
3181 3221 0
3181 3221 0

For data sources see[3]

Stimulations Data

Stimulation Date Chemical Agent Chemical Agent Concentration (%) Fracking Fluid Volume Mass of Proppant Used (lb) Fracking Company Comments
ACID 0 90 Qts 0

For data sources see[4]

Production Data

Period Operator Name Gas Quantity (mcf) Oil Quantity (bbl) Production Days
1984 OXFORD OIL 0.00 336.00 0
1985 OXFORD OIL 0.00 340.00 365
1986 OXFORD OIL 0.00 236.00 365
1987 OXFORD OIL 0.00 208.00 365
1988 OXFORD OIL 0.00 210.00 365
1989 OXFORD OIL 0.00 199.00 365
1990 OXFORD OIL 0.00 184.00 365
1991 OXFORD OIL 0.00 157.00 365
1992 OXFORD OIL 0.00 147.00 365
1993 OXFORD OIL 0.00 98.00 365
1994 OXFORD OIL 0.00 132.00 365
1995 OXFORD OIL 0.00 85.00 365
1996 OXFORD OIL 0.00 53.00 366
1997 OXFORD OIL 0.00 124.00 365
1998 OXFORD OIL 0.00 129.00 365
1999 OXFORD OIL 0.00 128.00 365
2000 OXFORD OIL 0.00 120.00 0
2001 OXFORD OIL 0.00 126.00 365
2002 OXFORD OIL 0.00 128.00 365
2003 OXFORD OIL 0.00 120.00 365
2004 OXFORD OIL 0.00 68.00 365
2005 OXFORD OIL 0.00 81.00 365
2006 OXFORD OIL 0.00 52.00 365
2007 OXFORD OIL 0.00 38.00 365
2008 OXFORD OIL 0.00 93.00 0
2009 OXFORD OIL 0.00 41.00 0
2010 OXFORD OIL 0.00 128.00 365
2011 OXFORD OIL 0.00 94.00 0
2012 OXFORD OIL 0.00 101.00 0
2013 ECLIPSE RESOURCES-OHIO LLC 0.00 56.00 365
2014 ECLIPSE RESOURCES-OHIO LLC 0.00 93.00 365
2015 ECLIPSE RESOURCES-OHIO LLC 0.00 48.00 365
2016 ECLIPSE RESOURCES-OHIO LLC 0.00 0.00 365

For data sources see[5] [6]

Waste Data

Period Operator Name Waste Type Quantity (bbl) Production Days
1984 OXFORD OIL Brine 0 0
1985 OXFORD OIL Brine 26 365
1986 OXFORD OIL Brine 16 365
1987 OXFORD OIL Brine 25 365
1988 OXFORD OIL Brine 28 365
1989 OXFORD OIL Brine 17 365
1990 OXFORD OIL Brine 17 365
1991 OXFORD OIL Brine 18 365
1992 OXFORD OIL Brine 10 365
1993 OXFORD OIL Brine 23 365
1994 OXFORD OIL Brine 24 365
1995 OXFORD OIL Brine 15 365
1996 OXFORD OIL Brine 15 366
1997 OXFORD OIL Brine 10 365
1998 OXFORD OIL Brine 5 365
1999 OXFORD OIL Brine 10 365
2000 OXFORD OIL Brine 10
2001 OXFORD OIL Brine 15 365
2002 OXFORD OIL Brine 11 365
2003 OXFORD OIL Brine 11 365
2004 OXFORD OIL Brine 15 365
2005 OXFORD OIL Brine 16 365
2006 OXFORD OIL Brine 6 365
2007 OXFORD OIL Brine 22 365
2008 OXFORD OIL Brine 12
2009 OXFORD OIL Brine 25
2010 OXFORD OIL Brine 84 365
2011 OXFORD OIL Brine 26
2012 OXFORD OIL Brine 26
2013 ECLIPSE RESOURCES-OHIO LLC Brine 6 365
2014 ECLIPSE RESOURCES-OHIO LLC Brine 9 365
2015 ECLIPSE RESOURCES-OHIO LLC Brine 0 365
2016 ECLIPSE RESOURCES-OHIO LLC Brine 0 365

For data sources see[7] [8]

Inspection Data

Inspections Performed

Inspection ID Inspection Date Inspection Type Inspection Result Inspection Comments
-1701158897 2015-8-10 0:00: PB No Violations
-2142536612 2016-6-8 0:00:0 FR No Violations 0.70
0242728274 2015-08-12 Plug / Plug Back No Violations Wright had ran 2.375tubing in to depth of 2280. Formation set cement plug from 2280-1980 in 7.875open hole. Thru 10 holes that perforated the 5.5casing that was shot by Appalachian Wireline. They also perforated at 10 shot per foot at the depth of 1014. Set Berea plug with cement at 1014-772. Placed it with 2.375tubing. Then rig pulled tubing up to bottom of 8.25casing. Appalachian used a collar buster and shot 5.5casing off at 650 and pulled all the 5.5casing out. They set 100in and 100out of the 8.25casing. The plug was set at 630-430. Appalachian Wireline shot 5 perfs at 200. Then a plug was placed thru the 2.375tubing and circulated until out of cement. There was no cement returns. There was an old water well that communicated and the oil and water came out and went to pit. Shut down and will run back in on 8-13-15 and tag cement.
0728054644 2015-08-17 Plug / Plug Back No Violations On the day of my inspection I found that Eclipse had a crew on site to close the pit, grade the site and seed it. The well had already been capped and buried. The tank battery and lease road are still in use for permits 0873, 0874 and 1143.
1101076689 2004-12-15 Production Wells No Violations Well in production .
1204080780 2015-08-06 Plug / Plug Back No Violations Wrights well service was at the site getting ready to pull the tubing out and I was there to meet with the Superintendent Elliot Sheely. We met and then Kenny Wright pulled out the 2.375 10 round thread tubing. Company requires a burn permit for welding a 8.625nipple on the casing. Steamers was coming in as I left.
1439172737 2015-08-07 Plug / Plug Back No Violations Wright well service pulled tubing and steamed tubing and ran back to depth of 3170. Formation Cementing was the cementing company. They ran 40 sacks of Regular class A cement. The plug was at 3170-2770. Wrights well service went in after pulling the 2.375tubing out and started ripping pipe. They went in at approximately 2400. Wright was having problems with the old 5.1875casing . They were getting the tools stuck and was pulling them out of the casing. I made a suggestion to run in with a bond log and then perforate. Wrights ran in and got tools stuck and snapped the sand line. This would lead to a fishing job on the first of the week.
1439814503 2015-08-11 Plug / Plug Back No Violations On the day of my inspection I found that Wright Well Services had backed off 430 of 5. They retrieved the tools and were in the process of running back in with newer 5 to screw back onto the original casing. The original casing was badly rusted and pitted.
1503916907 2015-08-13 Plug / Plug Back No Violations Rig tagged the cement top at 100 in the oil well. The rig scratched around and exposed the 8.25casing of the water well. Formation was called out and finish the cementing on both wells. Topped off the 2 tubing and the 8.25casing in water well. Then topped off the oil well. Formation used about 75 sacks at 2%gelled cement.
1701158897 2015-08-10 Plug / Plug Back No Violations On the day of my inspection I found that Wright Well Services was trying to fish ripping tools out of the 5.5 casing. Tim Altier of Eclipse reported that they set a 40 sack cement bottom plug through tubing. They tried to rip the 5.5 at 2450. He felt that they parted that casing, but it would not pull free. Wright went back in with the ripping tools to make a second attempt when his tools got hung at 150. The cable parted when they tried to pull the tools back out of the hole. Wright backed the 5.5 casing off at 200 and retrieved the tools.
2142536612 2016-06-08 Final Restoration No Violations On the day of my inspection I found that the well site was growing with well established tall grasses. I found no oilfield materials or debris left behind. I found no signs of erosion. The access road and tank battery are still in use for permits 0873, 0874 and 1143. This site passes final restoration.
242728274 2015-8-12 0:00: PB No Violations 9.50
728054644 2015-8-17 0:00: PB No Violations

For data sources see[9]

References