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Well ID: 34-031-20601 | Loading map...
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Country: United States | |
State: Ohio | |
County: Coshocton | |
Municipality: Bethlehem Township | |
Operator Name: G & S OIL & GAS INC | |
Well Pad ID: | |
Farm/Lease Name: MILLER BETTY M | |
License Status: Final Restoration | |
License Date: 1978-07-03 | |
Spud Date: 1953-12-25 | |
Spud Drilling Contractor: | |
Final Drill Date: 1954-03-18 | |
Well Total Depth: 3504.00 ft | |
Configuration: Vertical | |
Latitude: 40.370000 | |
Longitude: -81.980000 |
For data sources see[1]
Well Status | Well Status Date | Comment |
---|---|---|
Original Spud | 1953-12-25 | REOPEN & R.L. 7-5-79. PER WELL INSPECTION BY CHRIS GRIMM AND PLUGGING INFORMATION ON FILE, WELL NO LONGER EXISTS AND WAS PLUGGED ON 5/1/1979 AFTER AN ATTEMPT TO REPOPEN. WELL AKA FOX #5, B.M. LADD 1A. PREVIOUS STATUS DATE 07/03/1978-ALE 09/29/2016 |
Completed | 1954-03-18 | REOPEN & R.L. 7-5-79. PER WELL INSPECTION BY CHRIS GRIMM AND PLUGGING INFORMATION ON FILE, WELL NO LONGER EXISTS AND WAS PLUGGED ON 5/1/1979 AFTER AN ATTEMPT TO REPOPEN. WELL AKA FOX #5, B.M. LADD 1A. PREVIOUS STATUS DATE 07/03/1978-ALE 09/29/2016 |
Reached Total Depth | 1954-03-18 | REOPEN & R.L. 7-5-79. PER WELL INSPECTION BY CHRIS GRIMM AND PLUGGING INFORMATION ON FILE, WELL NO LONGER EXISTS AND WAS PLUGGED ON 5/1/1979 AFTER AN ATTEMPT TO REPOPEN. WELL AKA FOX #5, B.M. LADD 1A. PREVIOUS STATUS DATE 07/03/1978-ALE 09/29/2016 |
CO | 1978-07-03 | 745 G & S DRILLING GeoDate 7/3/78 |
Unknown | 1978-07-03 | Issued Date 7/3/78 Expired Date 7/3/79 Acres 0000000 Tool Type Proposed Formation Proposed Depth 00000 Proposed Drill Depth 00000 |
Plugged/Abandoned | 1979-05-01 | REOPEN & R.L. 7-5-79. PER WELL INSPECTION BY CHRIS GRIMM AND PLUGGING INFORMATION ON FILE, WELL NO LONGER EXISTS AND WAS PLUGGED ON 5/1/1979 AFTER AN ATTEMPT TO REPOPEN. WELL AKA FOX #5, B.M. LADD 1A. PREVIOUS STATUS DATE 07/03/1978-ALE 09/29/2016 |
Change of Owner | 2016-01-08 | Operator changed from 745, G & S OIL & GAS INC to 4031, DELTA PETROLEUM CORP |
Change of Owner | 2016-10-13 | Operator changed from 4031, DELTA PETROLEUM CORP to 745, G & S OIL & GAS INC |
Record Last Modified | 2019-06-05 | REOPEN & R.L. 7-5-79. PER WELL INSPECTION BY CHRIS GRIMM AND PLUGGING INFORMATION ON FILE, WELL NO LONGER EXISTS AND WAS PLUGGED ON 5/1/1979 AFTER AN ATTEMPT TO REPOPEN. WELL AKA FOX #5, B.M. LADD 1A. PREVIOUS STATUS DATE 07/03/1978-ALE 09/29/2016 |
For data sources see[2]
Period | Operator Name | Gas Quantity (mcf) | Oil Quantity (bbl) | Production Days |
---|---|---|---|---|
1993 | G & S OIL & GAS INC | 0.00 | 331.00 | 365 |
1995 | G & S OIL & GAS INC | 0.00 | 291.00 | 365 |
1997 | G & S OIL & GAS INC | 0.00 | 310.00 | 365 |
2001 | G & S OIL & GAS INC | 0.00 | 274.00 | 365 |
2002 | G & S OIL & GAS INC | 0.00 | 208.00 | 365 |
2003 | G & S OIL & GAS INC | 0.00 | 106.00 | 365 |
2006 | G & S OIL & GAS INC | 0.00 | 224.00 | 365 |
2007 | G & S OIL & GAS INC | 0.00 | 167.00 | 365 |
2008 | G & S OIL & GAS INC | 0.00 | 74.00 | 365 |
2009 | G & S OIL & GAS INC | 0.00 | 185.00 | 365 |
2010 | G & S OIL & GAS INC | 0.00 | 255.00 | 365 |
2011 | G & S OIL & GAS INC | 0.00 | 80.00 | 365 |
2012 | G & S OIL & GAS INC | 0.00 | 168.00 | 366 |
2013 | G & S OIL & GAS INC | 0.00 | 0.00 | 0 |
2014 | G & S OIL & GAS INC | 0.00 | 66.00 | 365 |
2015 | G & S OIL & GAS INC | 0.00 | 298.00 | 365 |
Period | Operator Name | Waste Type | Quantity (bbl) | Production Days |
---|---|---|---|---|
1993 | G & S OIL & GAS INC | Brine | 0 | 365 |
1995 | G & S OIL & GAS INC | Brine | 0 | 365 |
1997 | G & S OIL & GAS INC | Brine | 0 | 365 |
2001 | G & S OIL & GAS INC | Brine | 0 | 365 |
2002 | G & S OIL & GAS INC | Brine | 0 | 365 |
2003 | G & S OIL & GAS INC | Brine | 0 | 365 |
2006 | G & S OIL & GAS INC | Brine | 0 | 365 |
2007 | G & S OIL & GAS INC | Brine | 0 | 365 |
2008 | G & S OIL & GAS INC | Brine | 0 | 365 |
2009 | G & S OIL & GAS INC | Brine | 0 | 365 |
2010 | G & S OIL & GAS INC | Brine | 0 | 365 |
2011 | G & S OIL & GAS INC | Brine | 0 | 365 |
2012 | G & S OIL & GAS INC | Brine | 0 | 366 |
2013 | G & S OIL & GAS INC | Brine | 0 | 0 |
2014 | G & S OIL & GAS INC | Brine | 0 | 365 |
2015 | G & S OIL & GAS INC | Brine | 0 | 365 |
Inspection ID | Inspection Date | Inspection Type | Inspection Result | Inspection Comments |
---|---|---|---|---|
-1197376530 | 2016-9-7 0:00:0 | NF | No Violations | 1.50 |
-795476703 | 2010-2-5 0:00:0 | PW | No Violations | |
0795476703 | 2010-02-05 | Production Wells | No Violations | Well capable of production , notified pumper to post identification . |
1197376530 | 2016-09-07 | Field Inspected, Well Not Found | No Violations | I was contacted by Jim Dunfee requesting my assistance in resolving a case of mistaken well identity. I met with Jim, and John and Margaret Grim of G&S Oil & Gas at the well site. I found that the well was being produced with an electric powered pumping unit. The lines were connected and the valves were open. There was one 210 barrel steel tank staged approximately 25 feet from the wellhead. The identification on the tank was posted for permit 0601. I took GPS coordinates on the well to compare them to ODNR records. I plotted the new coordinates on a computer generated map in Topo 9 with the coordinates stored in RBDMS. I also compared the computer generated map with the original plat map used in the well permit application. I determined that the well in question was actually permit 0553. I also used my handheld GPS unit to walk to the coordinate location of permit 0601 stored in RBDMS. I found no existing well or well components. I did find that the coordinates plotted 43 feet from an open, flat area surrounded by mixed forest. Although no oilfield related materials were found, the area exhibited the characteristics of a plugged well site. I advised Mr. and Mrs. Grim to make an attempt to locate any old documents pertaining to the well being plugged. |
1480529533 | 2016-11-30 | Final Restoration | No Violations | I searched ODNR records and found a signed, completed plugging report, dated 5/1/79 for this well. I recommend that this well be placed in final restoration status, based on my field inspection of the well site on 9/7/16 where I found the stored well coordinates plotted within 43 feet of an open flat area in mixed forest that was covered in grasses and broadleaf vegetation. I found no oilfield related materials or debris. I found no open pits and no signs of erosion. I found no contamination or signs of a leaking plugged well. There was no existing access road, and I found no existing production equipment. This well site meets the requirements for final restoration. |
For data sources see[7]