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34-031-20739

Well Details

Well ID: 34-031-20739
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Country: United States
State: Ohio
County: Coshocton
Municipality: Newcastle Township
Operator Name: TWINOAKS OIL & GAS CO
Well Pad ID:
Farm/Lease Name: HEFFELFINGER GERTIE R
License Status: Final Restoration
License Date: 1985-06-04
Spud Date: 1980-07-05
Spud Drilling Contractor:
Final Drill Date: 1980-08-03
Well Total Depth: 3173.00 ft
Configuration: Vertical
Latitude: 40.350000
Longitude: -82.140000

For data sources see[1]

Well History

Well Status Well Status Date Comment
CO 1979-05-22 260 TWINOAKS OIL & GAS CO GeoDate 5/22/79
Original Spud 1980-07-05 REOPENED 5-23-79. ORIGINALLY PLUGGED 1/19/1970.
Completed 1980-08-03 REOPENED 5-23-79. ORIGINALLY PLUGGED 1/19/1970.
Reached Total Depth 1980-08-03 REOPENED 5-23-79. ORIGINALLY PLUGGED 1/19/1970.
Plugged/Abandoned 1985-06-28 REOPENED 5-23-79. ORIGINALLY PLUGGED 1/19/1970.
Record Last Modified 2018-05-31 REOPENED 5-23-79. ORIGINALLY PLUGGED 1/19/1970.

For data sources see[2]

Stimulations Data

Stimulation Date Chemical Agent Chemical Agent Concentration (%) Fracking Fluid Volume Mass of Proppant Used (lb) Fracking Company Comments
H2O 0 1950 Bbl 18000

For data sources see[3]

Production Data

Period Operator Name Gas Quantity (mcf) Oil Quantity (bbl) Production Days
1984 TWINOAKS OIL & GAS CO 0.00 232.00 0

For data sources see[4] [5]

Waste Data

Period Operator Name Waste Type Quantity (bbl) Production Days
1984 TWINOAKS OIL & GAS CO Brine 0 0

For data sources see[6] [7]

Inspection Data

Inspections Performed

Inspection ID Inspection Date Inspection Type Inspection Result Inspection Comments
0000013071 Final Restoration No Violations PASSED Y WITNESSED 12/30/91 INSPECTOR ROCKY KING DATE 12/3019/91 DATA FROM OLD VAX INFO
0307142825 2006-07-26 Production Wells No Violations Well in production .
13071 FR No Violations
1859349582 2018-03-15 Production Wells No Violations On the day of my inspection I found that the well coordinates were plotting in an open area, along an access road that connected with the access road for the number 1 well. I found some old sections of steel and plastic line around the general area. There was limestone gravel spread around the center of the open area and up the access road toward the number 1 well. I was with Twin Oaks pumper Steve Davis to confirm the location and status of this well. We did not find any wellhead components or casing in the area. I also did not find any indications that there was a leaking plugged well. The current well status is listed as producing and there has been production reported by Twin Oaks as recent as 2012. I found through my conversations with Steve and Glenn Lovell that they both believed the number 1 well was the number 6, and they were reporting the production from the number 1 under this permit number. I also found an inspection report from Rocky King claiming this well was in production in 2006, but when I plotted the coordinates that Rocky had recorded they plotted on the number 1 well location. I searched the well records and found the following chronology of the Heffelfinger #6, permit 0739: spud 5/18/1955, completed 6/15/1955, plugged 1/15/1970 by Preston Oil; then Twin Oaks applied to reopen the well in 1979, with a spud date of 7/5/1980, completed 8/3/1980. At this point the records are questionable, and the scanned copies in RBDMS are barely legible. I did not find an application for, or an issued plugging permit for this well after 1980. I did find a copy of a plug report from the Ohio Division of Mines dated 6/4/1986, which states that the well was plugged and abandoned on 6/28/1985. The copy of the report was in poor condition and I could not clearly read the plugging methods or materials used. Finally, I found two copies of final restoration reports. The first one was dated 5/30/1991 and I could not make out the signature of the inspector. The second wa
307142825 2006-7-26 0:00: PW No Violations

For data sources see[8]

References