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Well ID: 34-031-21398 | Loading map...
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Country: United States | |
State: Ohio | |
County: Coshocton | |
Municipality: Bethlehem Township | |
Operator Name: BRATTON ENERGY | |
Well Pad ID: | |
Farm/Lease Name: MEISER | |
License Status: Final Restoration | |
License Date: 2013-04-24 | |
Spud Date: 1960-12-03 | |
Spud Drilling Contractor: | |
Final Drill Date: 1961-03-01 | |
Well Total Depth: 3373.00 ft | |
Configuration: Vertical | |
Latitude: 40.370000 | |
Longitude: -81.990000 |
For data sources see[1]
Well Status | Well Status Date | Comment |
---|---|---|
Original Spud | 1960-12-03 | RE-OPEN 9-28-77 |
Completed | 1961-03-01 | RE-OPEN 9-28-77 |
Reached Total Depth | 1961-03-01 | RE-OPEN 9-28-77 |
Change of Owner | 2003-04-09 | Operator changed from 9999, UNKNOWN to 5430, BRATTON ENERGY |
APP | 2013-04-24 | Proposed Formations:, Issued Date:4/24/2013, Expired Date:4/24/2015 12:00:00 PM, Drilling unit acres:0, Proposed Well Type:OG, Proposed Well Class: |
Plugged/Abandoned | 2013-10-21 | RE-OPEN 9-28-77 |
Construction Permit Expires | 2015-04-24 | RE-OPEN 9-28-77 |
Record Last Modified | 2017-02-10 | RE-OPEN 9-28-77 |
For data sources see[2]
Stimulation Date | Chemical Agent | Chemical Agent Concentration (%) | Fracking Fluid Volume | Mass of Proppant Used (lb) | Fracking Company | Comments |
---|---|---|---|---|---|---|
H2O | 0 | 875 Bbl | 23000 |
For data sources see[3]
Period | Operator Name | Gas Quantity (mcf) | Oil Quantity (bbl) | Production Days |
---|---|---|---|---|
2003 | BRATTON ENERGY | 0.00 | 0.00 | 0 |
2004 | BRATTON ENERGY | 0.00 | 0.00 | 0 |
2005 | BRATTON ENERGY | 0.00 | 99.00 | 365 |
2006 | BRATTON ENERGY | 0.00 | 91.00 | 365 |
2007 | BRATTON ENERGY | 0.00 | 0.00 | 365 |
2008 | BRATTON ENERGY | 0.00 | 86.00 | 365 |
2009 | BRATTON ENERGY | 0.00 | 112.00 | 365 |
2010 | BRATTON ENERGY | 0.00 | 0.00 | 365 |
2011 | BRATTON ENERGY | 0.00 | 0.00 | 365 |
2012 | BRATTON ENERGY | 0.00 | 113.00 | 366 |
2013 | BRATTON ENERGY | 0.00 | 0.00 | 200 |
Period | Operator Name | Waste Type | Quantity (bbl) | Production Days |
---|---|---|---|---|
2003 | BRATTON ENERGY | Brine | 0 | 0 |
2004 | BRATTON ENERGY | Brine | 0 | 0 |
2005 | BRATTON ENERGY | Brine | 0 | 365 |
2006 | BRATTON ENERGY | Brine | 0 | 365 |
2007 | BRATTON ENERGY | Brine | 0 | 365 |
2008 | BRATTON ENERGY | Brine | 0 | 365 |
2009 | BRATTON ENERGY | Brine | 0 | 365 |
2010 | BRATTON ENERGY | Brine | 0 | 365 |
2011 | BRATTON ENERGY | Brine | 0 | 365 |
2012 | BRATTON ENERGY | Brine | 0 | 366 |
2013 | BRATTON ENERGY | Brine | 0 | 200 |
Inspection ID | Inspection Date | Inspection Type | Inspection Result | Inspection Comments |
---|---|---|---|---|
-1598652171 | 2013-10-10 0:00 | PB | No Violations | |
-1831304769 | 2013-10-21 0:00 | PB | No Violations | |
-1924821056 | 2014-7-23 0:00: | FR | No Violations | |
0201503733 | 2014-06-17 | Final Restoration | Violations Noted | On the day of my inspection I found that the site had been graded out and it was growing with well established weedy vegetation. I found no signs of erosion or sedimentation. The access road was also grown over with weedy vegetation and the tank battery is still in use for permit 0545. I did find a 3 foot section of 2 steel line and multiple sections of 1 steel cable protruding from the ground. All oil & gas related materials and debris must be removed from the site. This final restoration was due on 4/21/14. |
1045159481 | 2003-02-13 | Production Wells | No Violations | well is idle . Request from Ted brat ton to find owner . He is wanting to take well over to produce . Last owner with state was frank meiser ( dba ) meiser bros. Well was plugged in 1965 . And reopened in 1978 sometime. Lease name is meiser # 2 |
1382112231 | 2013-10-17 | Plug / Plug Back | No Violations | On the day of my inspection Mike Wheeler reported that the fluid level was approximately 1000 and there was concern over getting hung up in the undocumented 3 casing if they tried to run tubing in to spot a plug. The decision was made to shoot the casing off at the deepest possible point and set a 400 isolation plug. Jet Wireline Services shot the 3 casing off at 2815 and Wheeler pulled up approximately 2 feet. Cemenco pumped 80 sacks of class A cement. The well circulated almost immediately when they began pumping the plug. Wheeler pulled up to the top of the Big Lime and Cemenco set a 200 plug. |
1598652171 | 2013-10-10 | Plug / Plug Back | No Violations | On the day of my inspection I found that Wheeler Drilling pulled rods and tubing from the well. They encountered 3 casing in the well that was not reported in the records. They suspect the casing is on a packer. The service rig broke down before they could make an attempt at pulling the 3 casing. |
1831304769 | 2013-10-21 | Plug / Plug Back | No Violations | On the day of my inspection I found that Mike Wheeler had tubing set at 900. Cemenco broke circulation and pumped a 250 cement plug through the Berea. Wheeler pulled up to 300 and Cemenco pumped until cement was circulated to surface. |
1924821056 | 2014-07-23 | Final Restoration | No Violations | On the day of my inspection I found that the 2 line and the drill cable had been removed. This violation is resolved. This site passes final restoration. |
201503733 | 2014-6-17 0:00: | FR | No Violations |
Inspection ID | Violation ID | Violation Date | Violation Code | Violation Comments |
---|---|---|---|---|
0201503733 | US-OH-120449 | 2014-08-05 | Failure to complete final restoration within six months |
For data sources see[8]