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34-031-22270

Well Details

Well ID: 34-031-22270
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Country: United States
State: Ohio
County: Coshocton
Municipality: White Eyes Township
Operator Name: JERRY MOORE INC
Well Pad ID:
Farm/Lease Name: H W GILLETTE
License Status: Final Restoration
License Date: 2012-01-30
Spud Date: 1974-07-11
Spud Drilling Contractor:
Final Drill Date: 1974-08-17
Well Total Depth: 995.00 ft
Configuration: Vertical
Latitude: 40.340000
Longitude: -81.800000

For data sources see[1]

Well History

Well Status Well Status Date Comment
Original Spud 1974-07-11 RE-ISSUE 6-19-74
Completed 1974-08-17 RE-ISSUE 6-19-74
Reached Total Depth 1974-08-17 RE-ISSUE 6-19-74
CO 1981-09-29 124 MOORE JERRY INC GeoDate 9/29/81
APP 2012-01-30 Proposed Formations:BEREA, Issued Date:1/30/2012, Expired Date:1/29/2014 12:00:00 PM, Drilling unit acres:0, Proposed Well Type:OG, Proposed Well Class:
Plugged/Abandoned 2013-07-15 RE-ISSUE 6-19-74
Construction Permit Expires 2014-01-29 RE-ISSUE 6-19-74
Record Last Modified 2014-07-25 RE-ISSUE 6-19-74

For data sources see[2]

Perforation Treatments

Perforation Date Interval Top (ft) Interval Base (ft) Number of Shots
2006-09-11 0 0
0 0
0 0

For data sources see[3]

Inspection Data

Inspections Performed

Inspection ID Inspection Date Inspection Type Inspection Result Inspection Comments
-1066338689 2011-9-29 0:00: PW No Violations
-1336729587 2011-9-29 0:00: PW No Violations
-1586946362 2006-3-20 0:00: PW No Violations
-484583446 2013-9-5 0:00:0 FR No Violations
0484583446 2013-09-05 Final Restoration No Violations On the day of my inspection I found that location had been graded out to the approximate original contour, seeded and strawed. The area was covered in well established short grasses. There were no oilfield related materials or debris left at the location. There were no signs of leaking. This site passes final restoration.
0582785650 2013-07-11 Plug / Plug Back No Violations On the day of my inspection Thompsons Well Service uncovered the well to find that the clay had fallen approximately 120. They shoveled another 2 tons into the well to fill it to surface. It will be allowed to settle overnight.
0799908154 2013-07-08 Plug / Plug Back No Violations On the day of my inspection Thompson Well Service hooked up to the well head and ran in to 1010. They shoveled approximately 3 tons of clay into the well and then tried pulling on the 5.5 casing. The casing came free and Thompson pulled 525. Then they shoveled 9 more tons of clay into the well, filling it to surface. The clay will be allowed to settle overnight.
1066338689 2011-09-29 Production Wells Violations Noted Berea gas well is idle, well is shut in at well head, lead line or gas line has been disconnected from well head. no storage tanks or other equipment at site. There is a change of owner showing the number 1 and 2 wells were transferred to Jerry Moore in
1142883632 2006-03-20 Production Wells Violations Noted Well equipped with 5.5 casing and 1.5 tubing , no lead line or storage tanks at well site . Well is idle .
1143133321 2006-03-23 Administrative Inspection No Violations Call from Lewis with Jerry Moore , asked for extension to plug ( 6/15/06 ) Granted , RLK.
1336729587 2011-09-29 Production Wells No Violations FOLLOW UP TO NOV # -1066338689 Berea gas well is idle, well is shut in at well head, lead line or gas line has been disconnected from well head. no storage tanks or other equipment at site. There is a change of owner showing the number 1 and 2 wells were transferred to Jerry Moore in
1373656066 2013-07-12 Plug / Plug Back No Violations On the day of my inspection I found that the fluid level was down approximately one foot from the top of the casing. I probed into the fluid with a five foot section of fence post and found that the clay was sitting approximately four feet below grade. I instructed the plugging crew to top it off again and let it settle over the weekend.
1485689919 2007-08-06 Production Wells No Violations Well equipped with 7 casing and tubing . No other equipment , took pictures of well and location .
1586946362 2006-03-20 Production Wells No Violations FOLLOW UP TO NOV # 1142883632 Well equipped with 5.5 casing and 1.5 tubing , no lead line or storage tanks at well site . Well is idle .
1689799974 2013-07-25 Plug / Plug Back No Violations On the day of my inspection I found that the soil was graded out to the approximate original contour. There were no signs of leaking. I spoke with Mark Fluharty, who claims to have cut the casing off 36 below grade and capped it with a steel plate inscribed with the permit number.
1856269810 2013-07-15 Production Wells No Violations FOLLOW UP TO NOV # 1142883632 and # -1066338689: This well has been plugged and abandoned. These violations are resolved.
1876010325 2013-07-15 Plug / Plug Back No Violations On the day of my inspection I found that the well was filled to surface with clay.
582785650 2013-7-11 0:00: PB No Violations
799908154 2013-7-8 0:00:0 PB No Violations

Violations Commited

Inspection ID Violation ID Violation Date Violation Code Violation Comments
1066338689 US-OH-101342 2011-09-29 Well shall be plugged
1142883632 US-OH-103627 2006-03-20 Well shall be plugged

For data sources see[4]

References