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Well ID: 34-031-22306 | ![]() Sorry, we have no imagery here. Sorry, we have no imagery here. Sorry, we have no imagery here. ![]() |
Country: United States | |
State: Ohio | |
County: Coshocton | |
Municipality: Washington Township | |
Operator Name: KNOX ENERGY INC. | |
Well Pad ID: | |
Farm/Lease Name: ADAMS | |
License Status: Final Restoration | |
License Date: 2013-08-05 | |
Spud Date: 1974-02-06 | |
Spud Drilling Contractor: | |
Final Drill Date: 1974-04-11 | |
Well Total Depth: 3545.00 ft | |
Configuration: Vertical | |
Latitude: 40.170000 | |
Longitude: -82.080000 |
For data sources see[1]
Well Status | Well Status Date | Comment |
---|---|---|
Original Spud | 1974-02-06 | |
Completed | 1974-04-11 | |
Reached Total Depth | 1974-04-11 | |
CO | 1989-11-14 | 28 CGAS EXPLORATION,INC |
Change of Owner | 1999-06-17 | Operator changed from 28, CGAS EXPLORATION to 5632, RAMSEY TERRY |
Change of Owner | 2013-07-03 | Operator changed from 5632, TERRGIN OIL & GAS LLC to 6295, KNOX ENERGY INC. |
APP | 2013-08-05 | Proposed Formations:CLINTON, Issued Date:8/5/2013, Expired Date:8/5/2015 12:00:00 PM, Drilling unit acres:100, Proposed Well Type:OG, Proposed Well Class: |
Plugged/Abandoned | 2014-03-20 | |
Construction Permit Expires | 2015-08-05 | |
Record Last Modified | 2017-02-10 |
For data sources see[2]
Period | Operator Name | Gas Quantity (mcf) | Oil Quantity (bbl) | Production Days |
---|---|---|---|---|
1984 | LEADER EQUITIES INC | 0.00 | 301.00 | 0 |
1985 | LEADER EQUITIES INC | 0.00 | 227.00 | 365 |
1986 | LEADER EQUITIES INC | 0.00 | 262.00 | 365 |
1987 | LEADER EQUITIES INC | 0.00 | 225.00 | 365 |
1988 | LEADER EQUITIES INC | 0.00 | 220.00 | 365 |
1989 | CGAS EXPLORATION | 0.00 | 190.00 | 365 |
1990 | CGAS EXPLORATION | 0.00 | 185.00 | 365 |
1992 | CGAS EXPLORATION | 0.00 | 209.00 | 366 |
1993 | CGAS EXPLORATION | 0.00 | 77.00 | 366 |
1994 | CGAS EXPLORATION | 0.00 | 150.00 | 365 |
1995 | CGAS EXPLORATION | 0.00 | 96.00 | 365 |
1996 | CGAS EXPLORATION | 0.00 | 143.00 | 365 |
1997 | CGAS EXPLORATION | 0.00 | 130.00 | 365 |
1998 | CGAS EXPLORATION | 0.00 | 148.00 | 365 |
1999 | CGAS EXPLORATION | 0.00 | 70.00 | 365 |
2000 | TERRGIN OIL & GAS LLC | 0.00 | 120.00 | 150 |
2001 | TERRGIN OIL & GAS LLC | 0.00 | 120.00 | 150 |
2002 | TERRGIN OIL & GAS LLC | 0.00 | 120.00 | 150 |
2003 | TERRGIN OIL & GAS LLC | 0.00 | 120.00 | 150 |
2004 | TERRGIN OIL & GAS LLC | 0.00 | 65.00 | 150 |
2005 | TERRGIN OIL & GAS LLC | 0.00 | 100.00 | 150 |
2006 | TERRGIN OIL & GAS LLC | 0.00 | 100.00 | 150 |
2007 | TERRGIN OIL & GAS LLC | 0.00 | 80.00 | 150 |
2008 | TERRGIN OIL & GAS LLC | 0.00 | 50.00 | 365 |
2009 | TERRGIN OIL & GAS LLC | 0.00 | 60.00 | 365 |
2011 | TERRGIN OIL & GAS LLC | 0.00 | 78.00 | 365 |
2012 | TERRGIN OIL & GAS LLC | 0.00 | 28.00 | 366 |
2013 | KNOX ENERGY INC. | 0.00 | 0.00 | 0 |
2014 | KNOX ENERGY INC. | 0.00 | 0.00 | 0 |
Period | Operator Name | Waste Type | Quantity (bbl) | Production Days |
---|---|---|---|---|
1984 | LEADER EQUITIES INC | Brine | 0 | 0 |
1985 | LEADER EQUITIES INC | Brine | 13 | 365 |
1986 | LEADER EQUITIES INC | Brine | 40 | 365 |
1987 | LEADER EQUITIES INC | Brine | 17 | 365 |
1988 | LEADER EQUITIES INC | Brine | 17 | 365 |
1989 | CGAS EXPLORATION | Brine | 34 | 365 |
1990 | CGAS EXPLORATION | Brine | 17 | 365 |
1992 | CGAS EXPLORATION | Brine | 50 | 366 |
1993 | CGAS EXPLORATION | Brine | 17 | 366 |
1994 | CGAS EXPLORATION | Brine | 17 | 365 |
1995 | CGAS EXPLORATION | Brine | 0 | 365 |
1996 | CGAS EXPLORATION | Brine | 40 | 365 |
1997 | CGAS EXPLORATION | Brine | 17 | 365 |
1998 | CGAS EXPLORATION | Brine | 0 | 365 |
1999 | CGAS EXPLORATION | Brine | 0 | 365 |
2000 | TERRGIN OIL & GAS LLC | Brine | 20 | 150 |
2001 | TERRGIN OIL & GAS LLC | Brine | 20 | 150 |
2002 | TERRGIN OIL & GAS LLC | Brine | 20 | 150 |
2003 | TERRGIN OIL & GAS LLC | Brine | 20 | 150 |
2004 | TERRGIN OIL & GAS LLC | Brine | 20 | 150 |
2005 | TERRGIN OIL & GAS LLC | Brine | 20 | 150 |
2006 | TERRGIN OIL & GAS LLC | Brine | 20 | 150 |
2007 | TERRGIN OIL & GAS LLC | Brine | 20 | 150 |
2008 | TERRGIN OIL & GAS LLC | Brine | 20 | 365 |
2009 | TERRGIN OIL & GAS LLC | Brine | 20 | 365 |
2011 | TERRGIN OIL & GAS LLC | Brine | 20 | 365 |
2012 | TERRGIN OIL & GAS LLC | Brine | 50 | 366 |
2013 | KNOX ENERGY INC. | Brine | 0 | 0 |
2014 | KNOX ENERGY INC. | Brine | 0 | 0 |
Inspection ID | Inspection Date | Inspection Type | Inspection Result | Inspection Comments |
---|---|---|---|---|
-1016753496 | 2015-10-16 0:00 | FR | No Violations | |
-1557287856 | 2005-9-27 0:00: | PW | No Violations | |
-803580634 | 2006-7-10 0:00: | PW | No Violations | |
0102108376 | 2014-03-14 | Plug / Plug Back | No Violations | On the day of my inspection Berry Well Service washed approximately two tons of clay down the production casing. |
0149446008 | 2015-08-18 | Final Restoration | No Violations | On the day of my inspection I found that the tank battery and well site were both graded out and growing with well established vegetation. I found no signs of erosion. The former access road was shared with permit 2317. It was still in place and showed signs of frequent use. I called Bill Mitton of Knox Energy. He claimed that they were having a difficult time contacting the owner of the property to get a waiver for the road. The property is listed under Jemm Real Estate Development, and is allegedly leased out for hunting. |
0803580634 | 2006-07-10 | Production Wells | No Violations | Compliance |
1016753496 | 2015-10-16 | Final Restoration | No Violations | Knox Energy presented a signed copy of the Landowner Waiver (form 5) to leave the existing access road. |
102108376 | 2014-3-14 0:00: | PB | No Violations | |
1021914769 | 2014-03-12 | Plug / Plug Back | No Violations | On the day of my inspection I found that Berry Well Service was pulling rods and tubing from the well. Knox Energy removed all of the tank battery components and pulled all of the flow line from the tank battery back to the well. |
1075915746 | 2004-02-04 | Production Wells | No Violations | Well in production . Pumping well |
1111431389 | 2005-03-16 | Production Wells | Violations Noted | Oil around motor on pumping unit . Well head and storage tank not identified . |
1395159584 | 2014-03-18 | Plug / Plug Back | No Violations | On the day of my inspection I found that Berry Well Service had ripped the 4.5 casing at 3019 and pulled it from the well. They claimed to have washed another 8 tons of clay down the production hole. I received clay tickets for 30 tons of clay. They claimed to have set a bridge at 1160. They also claimed to have pulled over 50,000 pounds on the 7 casing without getting it to come free. They went in with their ripping tool and didnt get a telegraph till around 450. They washed 6 tons of clay down the well before parting the 7 casing. |
1395326019 | 2014-03-20 | Plug / Plug Back | No Violations | On the day of my inspection I found that the fluid level was still at approximately 150 down after sitting overnight. Berry Well Service washed another 1.5 to 2 tons of clay down the well to fill it to surface. |
1430751095 | 2015-05-04 | Final Restoration | No Violations | On the day of my inspection I found that the well site had been graded and seeded. The area was growing with well established vegetation. I found no oilfield related materials or debris. The lease road, which was shared with permit 2317, has not been restored. I have not received a landowner waiver. The former tank battery site still needs to be seeded. This site does not pass restoration at this time. I contacted Bill Mitton, he claimed that they would get a waiver. |
149446008 | 2015-8-18 0:00: | FR | No Violations | |
1557287856 | 2005-09-27 | Production Wells | No Violations | Area beside pumping unit needs contaminated soil removed ( oil from changing motor oil in pumping unit motor ) . Storage tanks need identified . |
1860664266 | 2014-03-19 | Plug / Plug Back | No Violations | On the day of my inspection Berry Well Service got the 7 casing ripped off at 462. They pulled the casing and washed approximately 12 tons of clay down the well. They ran out of water and shut down for the day. The fluid level was approximately 150 down. The clay will be allowed to settle overnight. |
Inspection ID | Violation ID | Violation Date | Violation Code | Violation Comments |
---|---|---|---|---|
1111431389 | US-OH-102790 | 2005-03-21 | Well operation causing pollution and contamination | |
1111431389 | US-OH-102791 | 2005-03-21 | Failure to legibly identify well |
For data sources see[7]