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Well ID: 34-031-22464 | Loading map...
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Country: United States | |
State: Ohio | |
County: Coshocton | |
Municipality: Bedford Township | |
Operator Name: ROYALTY ENTERPRISES INC | |
Well Pad ID: | |
Farm/Lease Name: KANUCKLE KENNETH | |
License Status: Producing | |
License Date: 1986-03-27 | |
Spud Date: 1974-08-27 | |
Spud Drilling Contractor: | |
Final Drill Date: 1974-09-29 | |
Well Total Depth: 3404.00 ft | |
Configuration: Vertical | |
Latitude: 40.240000 | |
Longitude: -82.090000 |
For data sources see[1]
Well Status | Well Status Date | Comment |
---|---|---|
Original Spud | 1974-08-27 | |
Completed | 1974-09-29 | |
Reached Total Depth | 1974-09-29 | |
CO | 1986-03-27 | 2136 KANUCKLE KENNETH P GeoDate 3/27/86 |
Unknown | 1986-03-27 | Issued Date 3/27/86 Expired Date 3/27/87 Proposed Purpose OG Was Plug Supervised Who Superivsed Plug and Abandon Date |
Construction Permit Expires | 1987-03-27 | |
CO | 1993-01-26 | 2136 KANUCKLE KENNETH P |
CO | 1993-01-26 | 4484 ROYALTY ENTERPRISES INC GeoDate 3/27/86 |
Record Last Modified | 2013-10-03 |
For data sources see[2]
Stimulation Date | Chemical Agent | Chemical Agent Concentration (%) | Fracking Fluid Volume | Mass of Proppant Used (lb) | Fracking Company | Comments |
---|---|---|---|---|---|---|
H2O | 0 | 1619 Bbl | 15000 |
For data sources see[3]
Period | Operator Name | Gas Quantity (mcf) | Oil Quantity (bbl) | Production Days |
---|---|---|---|---|
1984 | CALLANDER & KIMBREL INC | 0.00 | 97.00 | 0 |
1985 | CALLANDER & KIMBREL INC | 0.00 | 66.00 | 0 |
1986 | CALLANDER & KIMBREL INC | 0.00 | 0.00 | 365 |
2012 | ROYALTY ENTERPRISES INC | 0.00 | 10.00 | 365 |
2013 | ROYALTY ENTERPRISES INC | 0.00 | 5.00 | 365 |
2014 | ROYALTY ENTERPRISES INC | 150.00 | 0.00 | 365 |
2015 | ROYALTY ENTERPRISES INC | 90.00 | 10.00 | 365 |
2016 | ROYALTY ENTERPRISES INC | 100.00 | 15.00 | 365 |
2017 | ROYALTY ENTERPRISES INC | 120.00 | 10.00 | 365 |
Period | Operator Name | Waste Type | Quantity (bbl) | Production Days |
---|---|---|---|---|
1984 | CALLANDER & KIMBREL INC | Brine | 163 | 0 |
1985 | CALLANDER & KIMBREL INC | Brine | 90 | 0 |
1986 | CALLANDER & KIMBREL INC | Brine | 215 | 365 |
2012 | ROYALTY ENTERPRISES INC | Brine | 20 | 365 |
2013 | ROYALTY ENTERPRISES INC | Brine | 20 | 365 |
2014 | ROYALTY ENTERPRISES INC | Brine | 0 | 365 |
2015 | ROYALTY ENTERPRISES INC | Brine | 50 | 365 |
2016 | ROYALTY ENTERPRISES INC | Brine | 45 | 365 |
2017 | ROYALTY ENTERPRISES INC | Brine | 50 | 365 |
Inspection ID | Inspection Date | Inspection Type | Inspection Result | Inspection Comments |
---|---|---|---|---|
-1355121913 | 2008-7-1 0:00:0 | PW | No Violations | |
-1782663706 | 2015-7-21 0:00: | PW | No Violations | |
-193896425 | 2008-6-10 0:00: | PW | No Violations | |
-245158617 | 2011-1-18 0:00: | PW | No Violations | |
-879169508 | 2008-10-6 0:00: | PW | No Violations | |
000CENA970 | 1999-05-19 | Production Wells | No Violations | 1501:9-9-05 |
000CENA986 | 1999-09-10 | Production Wells | No Violations | 1501:9-9-05 |
0193896425 | 2008-06-10 | Production Wells | No Violations | Brine leaking at 2 pipe on bottom of storage tank . Identification faded , new identification needs posted . Follow up violation for leaking tank and identification , Tank still leaking , no identification posted . |
0245158617 | 2011-01-18 | Production Wells | No Violations | Took updated picture of well. Pump is stuck in well ( bridal is loose at well head ). Last production reported 1986 . There isnt any changes from last inspection of well. |
0291834355 | 2004-02-04 | Production Wells | Violations Noted | Well capable of production . Pumping unit on well . No production reports turned in for Royalty Enterprises . Last production 1986 . Storage tanks and well heads need identified . |
0565958402 | 2007-11-29 | Production Wells | Violations Noted | Brine leaking at 2 pipe on bottom of storage tank . Identification faded , new identification needs posted . |
0628268399 | 2015-07-21 | Production Wells | Violations Noted | On the day of my inspection I found that the wellhead was equipped with a pumping unit. The bridle was connected, the motor was intact and the valves were open. The well is capable of production and there was 150 mcf gas reported for 2014. Identification was posted at the wellhead and tank battery. I found a 5 x 3 area of standing water and mud at the edge of the tank battery near the load lines. The mud was heavily tracked by deer. I tested the water with a Quantab test strip which indicated a chloride level of 1435 parts per million (ppm). The brine contaminated soil must be removed from the tank battery within 14 days. |
0839606219 | 2007-11-29 | Production Wells | Violations Noted | FOLLOW UP TO NOV # 565958402 Brine leaking at 2 pipe on bottom of storage tank . Identification faded , new identification needs posted . |
0866373524 | 2015-01-12 | Production Wells | No Violations | On the day of my inspection I found that the well was equipped with a pumping unit. The bridle was loose and the unit was overgrown with small trees. The trees had been recently cut down to gain access to the unit. There was no identification at the wellhead or at the tank battery. The brine leak at the tank battery had been resolved. I met with Clayton King of Royalty Enterprises in regards to the status of this well. He claimed that the pump was stuck and he was waiting on Matheney Well Service to service the well. He also claimed that he would get the identification posted. |
0879169508 | 2008-10-06 | Production Wells | No Violations | Follow up inspection for pollution and idle well . Pump is stuck in well , bridle is loose on horse head . Brine tank is dripping brine from bottom 2 valve . Checked spill area with Quantab , reading of 624 ppm that is as high as the low chart will go . |
1040923156 | 2002-12-26 | Production Wells | No Violations | compliance |
1057914987 | 2015-08-05 | Production Wells | No Violations | On the day of my inspection I found that the brine contaminated soil had not been removed. I tried to call Clayton King. He did not answer and his phone would not accept voice mail. |
1099418823 | 2004-11-02 | Production Wells | No Violations | Compliance id posted . CHANGE IN STATUS OF WELL ( WAS UNKNOWN ) . REMOVE FROM PERMIT HOLD LIST . |
1163568109 | 2015-08-17 | Production Wells | No Violations | On the day of my inspection I found that the contaminated soil had been removed. This violation is resolved. |
1231352896 | 2009-01-07 | Production Wells | No Violations | Pit has been dug beside storage tank , no dike to direct contents of storage tank to pit . Pit is full of fresh water and will not contain a spill for tank . Non compliance for notice of violation . |
1268412494 | 2010-03-12 | Production Wells | No Violations | Inspection of well for Domestic gas use . Well has 10 psi. checked with personal gauge , line going to storage tank site , separator is by passed and 1 plastic line going in direction of land owners house . Looks to be in production for domestic use . Pump is still stuck in well ( bridal is loose at well head ) . |
1355121913 | 2008-07-01 | Production Wells | Violations Noted | Follow up brine leak . Tank is still dripping . Inspection of well shows well is idle . Bridal on horse head is loose ( pump is stuck ) . |
1425650181 | 2015-03-05 | Production Wells | No Violations | On the day of my inspection I found that Gene Matheny was rigged up on the well. He was pulling rods and tubing in an attempt to make this well capable of production. |
1505331798 | 2017-09-13 | Production Wells | No Violations | On the day of my inspection I found that the well was equipped with a natural gas powered pumping unit. The engine, drive belts and fuel line were intact. The flow lines were connected and the valves were open. There was some oil staining in the soil directly around the wellhead, but there were no active leaks or fresh oil on the ground. Identification was written on the pumping unit. There was a 30 barrel steel tank back near the well that didnt appear to be in use. The production equipment is shared with permits 2465 and 3709. It consisted of two 100 barrel steel tanks and one 2600 gallon poly tank in a shallow earthen dike. Correct, legible identification was posted and I found no leaks or spills. |
1536666101 | 2006-05-10 | Production Wells | No Violations | Well capable of production . WELL STATUS CHANGED TO PRODUCING |
1608342460 | 2004-03-08 | Production Wells | No Violations | No change , id not posted . REMOVE FROM PERMIT HOLD LIST . |
1782663706 | 2015-07-21 | Production Wells | No Violations | On the day of my inspection I found that identification was posted at the wellhead and tank battery. The tank that was reference as leaking in 2007 has been removed. This violation is resolved. |
291834355 | 2004-2-4 0:00:0 | PW | No Violations | |
565958402 | 2007-11-29 0:00 | PW | No Violations | |
628268399 | 2015-7-21 0:00: | PW | No Violations | |
839606219 | 2007-11-29 0:00 | PW | No Violations | |
866373524 | 2015-1-12 0:00: | PW | No Violations | |
CENA970 | 1999-5-19 0:00: | PW | No Violations | |
CENA986 | 1999-9-10 0:00: | PW | No Violations |
Inspection ID | Violation ID | Violation Date | Violation Code | Violation Comments |
---|---|---|---|---|
0291834355 | US-OH-122997 | 2004-02-04 | Failure to legibly identify well | |
0565958402 | US-OH-126352 | 2007-11-29 | Failure to legibly identify well | |
0628268399 | US-OH-127120 | 2015-08-27 | Well operation causing pollution and contamination | |
0839606219 | US-OH-129556 | 2016-07-26 | 9-1-07 | Well operation causing pollution and contamination |
0839606219 | US-OH-129557 | 2016-07-26 | 9-9-05(A)10 | Failure to legibly identify well |
1355121913 | US-OH-110269 | 2008-07-01 | Well operation causing pollution and contamination | |
1355121913 | US-OH-110270 | 2008-07-01 | Well shall be plugged |
For data sources see[8]