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Well ID: 34-031-22864 | Loading map...
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Country: United States | |
State: Ohio | |
County: Coshocton | |
Municipality: Tiverton Township | |
Operator Name: BUCKEYE OIL PRODUCING CO | |
Well Pad ID: | |
Farm/Lease Name: FESLER DON | |
License Status: Final Restoration | |
License Date: 2014-05-22 | |
Spud Date: 1976-12-30 | |
Spud Drilling Contractor: | |
Final Drill Date: 1977-01-27 | |
Well Total Depth: 3370.00 ft | |
Configuration: Vertical | |
Latitude: 40.400000 | |
Longitude: -82.120000 |
For data sources see[1]
Well Status | Well Status Date | Comment |
---|---|---|
CO | 1976-09-07 | 94 HAMBLIN RALPH INC GeoDate 9/7/76 |
Original Spud | 1976-12-30 | UPDATE LOCATION PER SURVEYOR-ALE 03/29/2017. |
Completed | 1977-01-27 | UPDATE LOCATION PER SURVEYOR-ALE 03/29/2017. |
Reached Total Depth | 1977-01-27 | UPDATE LOCATION PER SURVEYOR-ALE 03/29/2017. |
CO | 1992-07-31 | 296 DERRICK PETROLEUM INC GeoDate 9/7/76 |
Change of Owner | 1998-08-07 | Operator changed from 296, DERRICK PETROLEUM INC to 56, BUCKEYE OIL PRODUCING CO |
APP | 2014-05-22 | Proposed Formations:CLINTON, Issued Date:5/22/2014, Expired Date:5/21/2016 12:00:00 PM, Drilling unit acres:73, Proposed Well Type:OG, Proposed Well Class: |
Plugged/Abandoned | 2014-07-14 | UPDATE LOCATION PER SURVEYOR-ALE 03/29/2017. |
Construction Permit Expires | 2016-05-21 | UPDATE LOCATION PER SURVEYOR-ALE 03/29/2017. |
Record Last Modified | 2017-03-29 | UPDATE LOCATION PER SURVEYOR-ALE 03/29/2017. |
For data sources see[2]
Perforation Date | Interval Top (ft) | Interval Base (ft) | Number of Shots |
---|---|---|---|
2006-09-11 | 3232 | 3236 | 3 |
2006-09-11 | 3255 | 3280 | 17 |
3232 | 3236 | 3 | |
3232 | 3236 | 3 |
For data sources see[3]
Stimulation Date | Chemical Agent | Chemical Agent Concentration (%) | Fracking Fluid Volume | Mass of Proppant Used (lb) | Fracking Company | Comments |
---|---|---|---|---|---|---|
H2O | 0 | 1650 Bbl | 30000 |
For data sources see[4]
Period | Operator Name | Gas Quantity (mcf) | Oil Quantity (bbl) | Production Days |
---|---|---|---|---|
1984 | HAMBLIN RALPH INC | 0.00 | 520.00 | 0 |
1985 | HAMBLIN RALPH INC | 0.00 | 608.00 | 0 |
1986 | HAMBLIN RALPH INC | 0.00 | 456.00 | 365 |
1987 | HAMBLIN RALPH INC | 0.00 | 465.00 | 365 |
1988 | HAMBLIN RALPH INC | 0.00 | 461.00 | 365 |
1989 | HAMBLIN RALPH INC | 0.00 | 309.00 | 365 |
1990 | HAMBLIN RALPH INC | 0.00 | 410.00 | 365 |
1991 | HAMBLIN RALPH INC | 0.00 | 294.00 | 365 |
1992 | DERRICK PETROLEUM INC | 0.00 | 46.00 | 0 |
1993 | DERRICK PETROLEUM INC | 0.00 | 301.00 | 365 |
1994 | DERRICK PETROLEUM INC | 0.00 | 213.00 | 365 |
1995 | DERRICK PETROLEUM INC | 0.00 | 163.00 | 365 |
1996 | DERRICK PETROLEUM INC | 0.00 | 356.00 | 365 |
1997 | DERRICK PETROLEUM INC | 0.00 | 304.00 | 365 |
1998 | BUCKEYE OIL PRODUCING CO | 0.00 | 442.00 | 0 |
2001 | BUCKEYE OIL PRODUCING CO | 0.00 | 0.00 | 365 |
2013 | BUCKEYE OIL PRODUCING CO | 0.00 | 79.00 | 365 |
Period | Operator Name | Waste Type | Quantity (bbl) | Production Days |
---|---|---|---|---|
1984 | HAMBLIN RALPH INC | Brine | 0 | 0 |
1985 | HAMBLIN RALPH INC | Brine | 40 | 0 |
1986 | HAMBLIN RALPH INC | Brine | 69 | 365 |
1987 | HAMBLIN RALPH INC | Brine | 56 | 365 |
1988 | HAMBLIN RALPH INC | Brine | 42 | 365 |
1989 | HAMBLIN RALPH INC | Brine | 50 | 365 |
1990 | HAMBLIN RALPH INC | Brine | 0 | 365 |
1991 | HAMBLIN RALPH INC | Brine | 50 | 365 |
1992 | DERRICK PETROLEUM INC | Brine | 0 | 0 |
1993 | DERRICK PETROLEUM INC | Brine | 0 | 365 |
1994 | DERRICK PETROLEUM INC | Brine | 0 | 365 |
1995 | DERRICK PETROLEUM INC | Brine | 0 | 365 |
1996 | DERRICK PETROLEUM INC | Brine | 60 | 365 |
1997 | DERRICK PETROLEUM INC | Brine | 120 | 365 |
1998 | BUCKEYE OIL PRODUCING CO | Brine | 115 | |
2001 | BUCKEYE OIL PRODUCING CO | Brine | 0 | 365 |
2013 | BUCKEYE OIL PRODUCING CO | Brine | 516 | 365 |
Inspection ID | Inspection Date | Inspection Type | Inspection Result | Inspection Comments |
---|---|---|---|---|
-371879468 | 2007-11-8 0:00: | PW | No Violations | |
0371879468 | 2007-11-08 | Production Wells | No Violations | Well in production . |
0873159421 | 2016-10-12 | Final Restoration | No Violations | On the day of my inspection I escorted surveyor Tom Smith to the plugged well site in order to mark the location with a flagged stake at the final recorded GPS coordinates. I found that the vegetation was well established and there were no signs of erosion. There was no evidence that the plugged well was leaking. |
1405001409 | 2014-07-10 | Plug / Plug Back | No Violations | On the day of my inspection Gene Matheny washed two tons of clay down the 4.5 casing. They got a telegraph at 2725 and attempted to rip the casing. |
1405100072 | 2014-07-11 | Plug / Plug Back | No Violations | On the day of my inspection I found that Gene Matheny was still trying to get the 4.5 casing ripped off at 2725. |
1405360595 | 2014-07-14 | Plug / Plug Back | No Violations | On the day of my inspection I found that Gene Matheny had ripped the 4.5 casing off at 2575 and washed another 3 tons of clay down for a total of 5 tons on the bottom. They pulled the casing and then set a pre-cast cement plug on the 6 casing seat at 972. Matheny washed 5 tons of clay down the well then attempted to pull the 8.625 casing. The casing was rotted and pulled apart at 100. They recovered what casing they could and washed another 8 tons down the well filling it to surface. They clay was allowed to settle for a couple hours and then they topped it off with another 2 tons filling it to surface again. The clay was sitting firm at the surface when they started prepping the casing to be capped with the steel plate. |
1437544692 | 2015-05-05 | Final Restoration | No Violations | On the day of my inspection I found that the well site was graded out and growing with well established short grasses. All oilfield related materials and debris had been removed from the site. The lease road and tank battery is still in use for permit 2146. This site passes final restoration. |
1645183624 | 2007-06-08 | Production Wells | No Violations | Well in production . |
1781213599 | 2014-07-09 | Plug / Plug Back | No Violations | On the day of my inspection I found that Gene Matheny was pulling rods and tubing. |
873159421 | 2016-10-12 0:00 | FR | No Violations | 0.50 |
For data sources see[9]