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34-031-24743

Well Details

Well ID: 34-031-24743
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Country: United States
State: Ohio
County: Coshocton
Municipality: Pike Township
Operator Name: AP PRODUCTION LLC
Well Pad ID:
Farm/Lease Name: GOMEZ JOE
License Status: Final Restoration
License Date: 2019-07-17
Spud Date: 1982-04-26
Spud Drilling Contractor:
Final Drill Date: 1982-05-19
Well Total Depth: 3252.00 ft
Configuration: Vertical
Latitude: 40.220000
Longitude: -82.160000

For data sources see[1]

Well History

Well Status Well Status Date Comment
CO 1981-12-31 604 ASHCRAFT PETROLEUM INC GeoDate 12/31/81
Original Spud 1982-04-26 FDT=RED ROCK
Completed 1982-05-19 FDT=RED ROCK
Reached Total Depth 1982-05-19 FDT=RED ROCK
Record Last Modified 2019-05-22 FDT=RED ROCK

For data sources see[2]

Perforation Treatments

Perforation Date Interval Top (ft) Interval Base (ft) Number of Shots
2006-09-11 3201 3207 7
2006-09-11 3220 3226 7
3201 3207 7
3201 3207 7

For data sources see[3]

Stimulations Data

Stimulation Date Chemical Agent Chemical Agent Concentration (%) Fracking Fluid Volume Mass of Proppant Used (lb) Fracking Company Comments
GEL 0 0 80000 F/W=LINK GEL

For data sources see[4]

Production Data

Period Operator Name Gas Quantity (mcf) Oil Quantity (bbl) Production Days
1986 AP PRODUCTION LLC 0.00 245.00 365
1987 AP PRODUCTION LLC 0.00 246.00 365
1988 AP PRODUCTION LLC 0.00 248.00 365
1989 AP PRODUCTION LLC 0.00 164.00 365
1990 AP PRODUCTION LLC 0.00 160.00 365
1991 AP PRODUCTION LLC 0.00 166.00 365
1992 AP PRODUCTION LLC 0.00 150.00 365
1993 AP PRODUCTION LLC 0.00 153.00 365
1994 AP PRODUCTION LLC 0.00 78.00 365
1995 AP PRODUCTION LLC 0.00 0.00 180
1997 AP PRODUCTION LLC 0.00 148.00 365
1998 AP PRODUCTION LLC 0.00 0.00 365
1999 AP PRODUCTION LLC 0.00 0.00 365
2000 AP PRODUCTION LLC 0.00 0.00 365
2001 AP PRODUCTION LLC 0.00 66.00 365
2002 AP PRODUCTION LLC 0.00 0.00 365
2003 AP PRODUCTION LLC 0.00 0.00 365
2004 AP PRODUCTION LLC 0.00 0.00 365
2005 AP PRODUCTION LLC 0.00 0.00 0
2006 AP PRODUCTION LLC 0.00 50.00 365
2007 AP PRODUCTION LLC 0.00 0.00 365
2008 AP PRODUCTION LLC 0.00 192.00 365
2009 AP PRODUCTION LLC 0.00 203.00 365
2010 AP PRODUCTION LLC 0.00 119.00 365
2011 AP PRODUCTION LLC 0.00 139.00 365
2012 AP PRODUCTION LLC 0.00 50.00 366
2013 AP PRODUCTION LLC 0.00 165.00 365
2014 AP PRODUCTION LLC 0.00 100.00 365
2015 AP PRODUCTION LLC 0.00 110.00 365
2016 AP PRODUCTION LLC 0.00 54.00 365
2017 AP PRODUCTION LLC 0.00 30.00 365
2018 AP PRODUCTION LLC 0.00 55.00 365

For data sources see[5] [6]

Waste Data

Period Operator Name Waste Type Quantity (bbl) Production Days
1986 AP PRODUCTION LLC Brine 180 365
1987 AP PRODUCTION LLC Brine 180 365
1988 AP PRODUCTION LLC Brine 120 365
1989 AP PRODUCTION LLC Brine 120 365
1990 AP PRODUCTION LLC Brine 230 365
1991 AP PRODUCTION LLC Brine 180 365
1992 AP PRODUCTION LLC Brine 70 365
1993 AP PRODUCTION LLC Brine 140 365
1994 AP PRODUCTION LLC Brine 70 365
1995 AP PRODUCTION LLC Brine 0 180
1997 AP PRODUCTION LLC Brine 60 365
1998 AP PRODUCTION LLC Brine 0 365
1999 AP PRODUCTION LLC Brine 60 365
2000 AP PRODUCTION LLC Brine 0 365
2001 AP PRODUCTION LLC Brine 60 365
2002 AP PRODUCTION LLC Brine 0 365
2003 AP PRODUCTION LLC Brine 0 365
2004 AP PRODUCTION LLC Brine 0 365
2005 AP PRODUCTION LLC Brine 0 0
2006 AP PRODUCTION LLC Brine 0 365
2007 AP PRODUCTION LLC Brine 0 365
2008 AP PRODUCTION LLC Brine 0 365
2009 AP PRODUCTION LLC Brine 0 365
2010 AP PRODUCTION LLC Brine 0 365
2011 AP PRODUCTION LLC Brine 0 365
2012 AP PRODUCTION LLC Brine 0 366
2013 AP PRODUCTION LLC Brine 0 365
2014 AP PRODUCTION LLC Brine 0 365
2015 AP PRODUCTION LLC Brine 0 365
2016 AP PRODUCTION LLC Brine 0 365
2017 AP PRODUCTION LLC Brine 0 365
2018 AP PRODUCTION LLC Brine 60 365

For data sources see[7] [8]

Inspection Data

Inspections Performed

Inspection ID Inspection Date Inspection Type Inspection Result Inspection Comments
-148132348 2020-7-28 0:00: FR No Violations 0.80
0365746780 2007-09-24 Production Wells No Violations Well in production . No identification .
0816938117 2013-06-05 Production Wells No Violations FOLLOW UP TO CA# 1366734900: On the day of my inspection I found that proper identification had been posted. This violation is resolved.
1366734900 2013-04-23 Production Wells Violations Noted On the day of my inspection I found that the well head was equipped with a pumping unit. The soil around the well head was soaked with oil and covered in some type of absorbent material. There was also a 2 ft by 15 ft strip of contamination extending downhill from the well head. There was one tank battery consisting of two 100 barrel stock tanks and an earthen dike on top of the hill near the well head. There was another tank battery down close to the road which consisted of two 100 barrel stock tanks and an earthen dike. The tanks were so close they were touching. No identification was posted at either tank battery or well head. Clean up contaminated soil around well head, move the tanks to meet spacing requirements, and post proper identification.
1369842843 2013-05-29 Production Wells No Violations FOLLOW UP TO CA# 1366734900: On the day of my inspection I found that one of the 100 barrel tanks in the lower tank battery had been removed. The remaining tank had been freshly painted and the dike was built up. The contaminated soil at the well head had been cleaned up and there were no more signs of leaking. This well still needs proper identification.
1568049962 2019-9-9 0:00:0 PB No Violations 0.20
1568134666 2019-9-10 0:00: PB No Violations
1568322757 2019-9-12 0:00: PB No Violations
1568723267 2019-9-11 0:00: PB No Violations 4.30
1838153387 2019-9-17 0:00: PB No Violations 0.40
365746780 2007-9-24 0:00: PW No Violations
816938117 2013-6-5 0:00:0 PW No Violations

Violations Commited

Inspection ID Violation ID Violation Date Violation Code Violation Comments
1366734900 US-OH-110805 2013-06-05 Well operation causing pollution and contamination
1366734900 US-OH-110806 2013-06-05 Failure to legibly identify well
1366734900 US-OH-110807 2013-06-05 Violation of tank spacing requirements

For data sources see[9]

References