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| Well ID: 34-031-25047 | Loading map...
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| Country: United States | |
| State: Ohio | |
| County: Coshocton | |
| Municipality: Perry Township | |
| Operator Name: KUKLA ROBERT | |
| Well Pad ID: | |
| Farm/Lease Name: DALE C JANE & HEDDRICK DAVID | |
| License Status: Final Restoration | |
| License Date: 2017-08-04 | |
| Spud Date: 1983-03-06 | |
| Spud Drilling Contractor: EDCO DRLG | |
| Final Drill Date: 1983-03-18 | |
| Well Total Depth: 3451.00 ft | |
| Configuration: Vertical | |
| Latitude: 40.240000 | |
| Longitude: -82.100000 |
For data sources see[1]
| Well Status | Well Status Date | Comment |
|---|---|---|
| CO | 1983-02-22 | 962 PARAGON ENERGY CO GeoDate 2/22/83 |
| Oil and Gas | 1983-02-22 | Issued Date 2/22/83 Expired Date 8/21/83 Acres 0020000 Tool Type RTF Proposed Formation CLINTON Proposed Depth 03451 Proposed Drill Depth 03451 |
| Original Spud | 1983-03-11 | CHANGED STATUS OF WELL FROM PR TO DM PER TRANSFER FROM ROYALTY ENTERPRISES, INC. #4484 TO OWNER ON 6/9/2017 CM. UPDATE LOCATION PER DOGRM SURVEYOR COORDINATES. |
| Completed | 1983-03-18 | CHANGED STATUS OF WELL FROM PR TO DM PER TRANSFER FROM ROYALTY ENTERPRISES, INC. #4484 TO OWNER ON 6/9/2017 CM. UPDATE LOCATION PER DOGRM SURVEYOR COORDINATES. |
| Reached Total Depth | 1983-03-18 | CHANGED STATUS OF WELL FROM PR TO DM PER TRANSFER FROM ROYALTY ENTERPRISES, INC. #4484 TO OWNER ON 6/9/2017 CM. UPDATE LOCATION PER DOGRM SURVEYOR COORDINATES. |
| Completion Report Received | 1984-01-18 | CHANGED STATUS OF WELL FROM PR TO DM PER TRANSFER FROM ROYALTY ENTERPRISES, INC. #4484 TO OWNER ON 6/9/2017 CM. UPDATE LOCATION PER DOGRM SURVEYOR COORDINATES. |
| CO | 1986-09-15 | 254 EDCO DRILLING & PRODUCING GeoDate 9/15/86 |
| Unknown | 1986-09-15 | Issued Date 9/15/86 Expired Date 9/15/87 Proposed Purpose OG Was Plug Supervised Who Superivsed Plug and Abandon Date |
| CO | 1988-01-14 | 254 EDCO DRILLING & PRODUCING GeoDate 1/14/88 |
| Unknown | 1988-01-14 | Issued Date 12/31/87 Expired Date 12/30/88 Proposed Purpose OG Was Plug Supervised Who Superivsed Plug and Abandon Date |
| Change of Owner | 2014-10-17 | Operator changed from 254, EDCO DRILLING & PRODUCING to 4484, ROYALTY ENTERPRISES INC. WELL TRANFERRED PER MEGAN DELISI ON 10/09/2014. REFER TO THE LEGAL DEPARTMENT FOR MORE INFORMATION.EAF |
| Change of Owner | 2017-06-09 | Operator changed from 4484, ROYALTY ENTERPRISES INC to 9940, KUKLA ROBERTS |
| APP | 2017-08-04 | Proposed Formations:CLINTON SAND, Issued Date:8/4/2017, Expired Date:8/4/2019 12:00:00 PM, Drilling unit acres:20, Proposed Well Type:OG, Proposed Well Class: |
| Plugged/Abandoned | 2018-04-10 | CHANGED STATUS OF WELL FROM PR TO DM PER TRANSFER FROM ROYALTY ENTERPRISES, INC. #4484 TO OWNER ON 6/9/2017 CM. UPDATE LOCATION PER DOGRM SURVEYOR COORDINATES. |
| Record Last Modified | 2018-08-07 | CHANGED STATUS OF WELL FROM PR TO DM PER TRANSFER FROM ROYALTY ENTERPRISES, INC. #4484 TO OWNER ON 6/9/2017 CM. UPDATE LOCATION PER DOGRM SURVEYOR COORDINATES. |
| Construction Permit Expires | 2019-08-04 | CHANGED STATUS OF WELL FROM PR TO DM PER TRANSFER FROM ROYALTY ENTERPRISES, INC. #4484 TO OWNER ON 6/9/2017 CM. UPDATE LOCATION PER DOGRM SURVEYOR COORDINATES. |
For data sources see[2]
| Perforation Date | Interval Top (ft) | Interval Base (ft) | Number of Shots |
|---|---|---|---|
| 1997-06-29 | 0 | 0 | |
| 0 | 0 | ||
| 2006-09-11 | 3359 | 3379 | 40 |
| 3359 | 3379 | 40 | |
| 0 | 0 |
For data sources see[3]
| Stimulation Date | Chemical Agent | Chemical Agent Concentration (%) | Fracking Fluid Volume | Mass of Proppant Used (lb) | Fracking Company | Comments |
|---|---|---|---|---|---|---|
| GEL | 0 | 900 Bbl | 50000 | FRAC; FLUID &SAND |
For data sources see[4]
| Period | Operator Name | Gas Quantity (mcf) | Oil Quantity (bbl) | Production Days |
|---|---|---|---|---|
| 2014 | ROYALTY ENTERPRISES INC | 0.00 | 0.00 | 0 |
| 2015 | ROYALTY ENTERPRISES INC | 0.00 | 0.00 | 0 |
| 2016 | ROYALTY ENTERPRISES INC | 0.00 | 0.00 | 0 |
| Period | Operator Name | Waste Type | Quantity (bbl) | Production Days |
|---|---|---|---|---|
| 2014 | ROYALTY ENTERPRISES INC | Brine | 0 | 0 |
| 2015 | ROYALTY ENTERPRISES INC | Brine | 0 | 0 |
| 2016 | ROYALTY ENTERPRISES INC | Brine | 0 | 0 |
| Inspection ID | Inspection Date | Inspection Type | Inspection Result | Inspection Comments |
|---|---|---|---|---|
| -1041742966 | 2015-1-23 0:00: | PW | No Violations | |
| -1807583545 | 2015-7-2 0:00:0 | PW | No Violations | |
| -613898669 | 2015-9-2 0:00:0 | PW | No Violations | |
| -668216829 | 2018-4-4 0:00:0 | PB | No Violations | 0.70 |
| -740527965 | 2018-7-20 0:00: | FR | No Violations | 0.30 |
| -76587462 | 2015-7-21 0:00: | PW | No Violations | |
| 0032054354 | 2014-01-21 | Administrative Inspection | No Violations | FOLLOW UP TO CA #386042156: I received a phone call from Eric Brown, who reported that Clayton King of Royalty Enterprises has allegedly claimed ownership of the well. Mr. Brown claimed that he is waiting on Mr. King to sign the form 7 for the transfer of ownership. |
| 0076587462 | 2015-07-21 | Production Wells | No Violations | On the day of my inspection I found that the crude oil/paraffin contamination had not been cleaned up. I called Clayton King. He claimed that he would be out within the next two days to get it cleaned up. |
| 0210441542 | 2015-06-23 | Production Wells | Violations Noted | On the day of my inspection I found that there had been a leak at the wellhead. There was a circle of crude oil contamination approximately 8 to 10 in diameter. I called Clayton King to report the leak. He said he would be out to start cleaning it up. |
| 0229583183 | 2018-04-11 | Plug / Plug Back | No Violations | On the day of my inspection I found that Berry Well Service had rigged down and moved all of their equipment out, except one bulldozer and one track-hoe that were parked at the access road entrance. The well site was rough graded to the approximate contour of the surrounding landscape. The only oilfield related materials left at the site was 2 feet of yellow plastic 1 inch diameter gas line protruding from the ground. The line was used by Clayton King when he owned the well. I called Clayton to ask about removing the line, but he didnt answer. I spoke with Donny Strange of Knox Energy/ Berry Well Service and he said that the cement had fallen a little over night. Donny claimed that it took 13 bags of sack cement to top it off before they cut, capped and buried the casing. |
| 0386042156 | 2013-05-21 | Production Wells | Violations Noted | I received a call from Robert Kukla (803-528-9233) in regards to an idle well on his property. On the day of my inspection I found that the well head was completely overgrown with multiflora rose. The well head was still equipped with rods, although the pumping unit was disconnected. There was no motor on the pumping unit and it had been moved approximately 15 feet from the well head. There were newer plastic one inch lines hooked up to the well head. I found no production equipment and no identification. ODNR records show that no production has ever been reported for this well. In its current state this well is incapable of production. Make well capable of commercial production within 30 days; or plugging is required within 90 days. Failure to comply may result in forfeiture of bond. |
| 0391587320 | 2015-09-09 | Production Wells | No Violations | On the day of my inspection I found that the oil and paraffin had finally been cleaned up. This violation is resolved. |
| 0589656275 | 2015-01-16 | Production Wells | No Violations | On the day of my inspection I found that the wellhead had been equipped with a pumping unit. There was no motor on the unit and the bridle was not connected. Clayton King claimed that he was working on the motor and hoped to have it pumping by 1/19/15. |
| 0613898669 | 2015-09-02 | Production Wells | No Violations | On the day of my inspection I found that the oil and paraffin had not been cleaned up. I called Clayton King. This time he claimed that the landowner Bob Kukla had granted him access to the well. He claimed again that he would get it cleaned up over the weekend. |
| 0668216829 | 2018-04-04 | Plug / Plug Back | No Violations | On the day of my inspection I found that Berry Well Service was rigged up t plug the well. No one was working at the site. I called Donny Strange with Knox Energy and he said that they are waiting for the ground to dry up a little before they come back in. I also told Donny that I had spoke with the previous well owner, Clayton king, who said that he believed there was a hole in the production casing. Donny said that he would keep an eye on it when they were pulling the tubing. |
| 0733930665 | 2007-10-17 | Production Wells | Violations Noted | Well equipped for production , motor on unit hasnt ran for a long time , vines growing up thru pulleys . No production ever reported , well drilled in 1983 . Well is owned by ROYALTY ENTERPRISES INC . There is no transfer to this company . 9/17/07 notified Mr. King owner of well to transfer well to his company and produce or plug well . |
| 0740527965 | 2018-07-20 | Final Restoration | No Violations | On the day of my inspection I found that the drill site and access road were graded, plowed, planted and growing in soy beans. There were no materials or debris left behind and there were no signs that the plugged well was leaking. There were no signs of erosion. The tanks are still in use for permits 2464, 2465 and 3709. This site passes final restoration. |
| 0889172601 | 2015-06-23 | Production Wells | No Violations | On the day of my inspection I found that the wellhead was equipped with a pumping unit. The motor was intact. There were belts on the pulley and the gearbox. The bridle was connected. The valve on the casing was closed. The valve on the tubing was open. I saw no pressure on the gauge. The lines at the wellhead were connected. The was also 1 yellow plastic gas line connected. I called Clayton King to come out and start the well. He said he could meet me at 13:00 on 6/24/15 to demonstrate that the well is capable of pumping. There was still no identification at the wellhead or tank battery. |
| 1041742966 | 2015-01-23 | Production Wells | No Violations | On the day of my inspection I found that there had been no motor installed on the pump jack and the bridle was still not hooked up. This well is still idle. |
| 1059641152 | 2017-04-26 | Exempt Well Pre Transfer | No Violations | On the day of my inspection I found that the well was equipped with a natural gas powered pumping unit. The engine and drive belts were intact. The flow lines were connected at the wellhead. The valves were closed. There was identification written on the pumping unit. I did not find any leaks or spills at the wellhead. There are no existing structures on this property to receive domestic gas. I spoke with the owner Clayton King of Royalty Enterprises and he said that he used to get gas off of the well, but he has not been able to pump it due to legal matters. The well is currently idle. |
| 1147275259 | 2006-05-10 | Production Wells | Violations Noted | Well equipped for production , motor on unit hasnt ran for a long time , vines growing up thru pulleys . No production ever reported , well drilled in 1983 . No storage tanks found . Void NOV , resent to Royalty enterprises . |
| 1152287279 | 2006-07-07 | Production Wells | No Violations | Well head has gas line hooked up , may be used for domestic gas , stopped at house , no one home to ask if they were using gas from well . There is no identification at well . Motor on pumping unit not in running order ( no plug wires ) . |
| 1196357673 | 2007-11-29 | Production Wells | No Violations | Pumping unit removed since last inspection . No production ever reported . Request chiefs order to plug . |
| 1246550639 | 2009-07-02 | Administrative Inspection | No Violations | Prepared chiefs order request to plug well . |
| 1268120185 | 2018-04-10 | Plug / Plug Back | No Violations | On the day of my inspection I found that Berry Well Service has 1.5 inch diameter tubing ran to a depth of 2371 feet for the Big Lime plug. Cemenco hooked up and started pumping to establish circulation. The tubing immediately pressured up to 800 pounds. Cemenco gave it some time to monitor the pressure for the obstruction to be cleared. The pressure decrease was minimal, so Berry pulled the tubing and found that the bottom joint was plugged with downhole formation material. They cleared the obstruction and ran the tubing back in, leaving two joints out for a depth of 2305 feet. Cemenco started pumping and the tubing pressured up again. Berry removed one joint at a time while Cemenco continued to attempt circulation. Berry pulled a total of five more joints for a depth of 2140 feet when the fluid started to move. Berry worked the tubing up and down while Cemenco pumped until they had good circulation. The rig operator, cement engineer and myself suspected that the hole had caved in above the ripped 4.5 inch casing top. I allowed them to set a 250 foot Big Lime isolation plug where they finally achieved good circulation. Berry Well Service and Cemenco also set 200 foot cement plugs through the Berea, at the base of the surface casing and at the surface. Circulation was established and maintained through all of the plugs, with cement being circulated to surface on the final plug. The cement had fallen to approximately 50 feet by the time the rig crew had finished cleaning up. Cemenco topped it off and Berry left the casing open over night. |
| 1337981404 | 2011-01-18 | Production Wells | No Violations | Took updated picture of well. Well is equipped with tubing and rods, there is a pumping unit on location that isnt in working order (missing motor and parts of gear box) and not hooked up to well. No production ever reported , well drilled in 1983 . Well |
| 1398358457 | 2014-04-24 | Production Wells | No Violations | FOLLOW UP TO CA #386042156: This inspection pertains to complaint #4331. On the day of my inspection I met with Robert Kukla at the well and took updated photographs. I found that the well was still sitting idle equipped with a stuffing box and polished rod. The pumping unit was still disconnected. The valves were closed and the gauge showed 40 lbs. on the tubing. There was new yellow plastic gas line connected to this well that entered the ground in an easterly direction. There were no storage tanks and no identification. |
| 1436359705 | 2015-07-07 | Production Wells | No Violations | On the day of my inspection I found that identification had been posted at the wellhead and tank battery. The well has been made capable of production. Royalty Enterprises did submit an annual statement of production for 2014. This violation is resolved. |
| 1523025492 | 2018-04-05 | Plug / Plug Back | No Violations | On the day of my inspection I found that Berry Well Service has the rods out and they were finishing up with pulling the tubing. Donny Strange said that the fluid was up to approximately 200 feet, so he was certain the production casing did have a hole in it. They were going to bring a sting of 1.5 inch diameter tubing back in to use for setting the cement plugs. Donny said that they will be ready to set the bottom plug tomorrow around noon. |
| 1523044343 | 2018-04-06 | Plug / Plug Back | No Violations | On the day of my inspection I found that Berry Well Service was running the 1.5 inch tubing in the well. They ran the tubing to a depth of 3353 feet. Cemenco established circulation into the steel half-round tank and then pumped a 30 sack cement plug through the Clinton sand. |
| 1523287184 | 2018-04-09 | Plug / Plug Back | No Violations | On the day of my inspection I found that Berry Well Service had the 1.5 inch diameter tubing out and they were running in the 4.5 inch diameter casing with their ripping tools. The tools kept getting hung up at a depth of 1300 feet. They removed the knife from the tools and were able to get through the tight spot. Donny Strange was operating the service rig. He started looking for a telegraph around 2800 feet and came up the hole in 50 foot increments until they finally got a good telegraph at a depth of 2357 feet. Donny parted the casing there and they started removing it from t he well. They plan to remove all of the 4.5 inch casing and then run back in with the 1.5 inch tubing to set the rest of the cement plugs. |
| 1621931216 | 2015-08-05 | Production Wells | No Violations | On the day of my inspection I found that the oil and paraffin had not been cleaned up. I tried to call Clayton King. He did not answer and his phone would not accept voice mail. |
| 1661785787 | 2015-01-12 | Production Wells | No Violations | On the day of my inspection I found that there has been no change in the status of this well. It was still sitting idle equipped with a stuffing box and polished rod. The pumping unit was still disconnected. I met with Clayton King of Royalty Enterprises, who claimed that he was waiting on H&D Drilling to move a functional pumping unit to the well in an attempt to produce it. He claimed that H&D Drilling was scheduled to be there on 1/13/15. |
| 1807583545 | 2015-07-02 | Production Wells | No Violations | On the day of my inspection I found that the well was still not identified and the oil/paraffin had not been cleaned up. I called Clayton King. He blamed the weather. He claimed that he would have everything done by Monday, July 6. |
| 1861577013 | 2014-01-17 | Administrative Inspection | No Violations | FOLLOW UP TO CA #386042156: I tried to contact Eric Brown of Edco to get an update on the status of this well. There was no answer, so I left a voice message. |
| 2072259816 | 2015-08-17 | Production Wells | No Violations | On the day of my inspection I found that the oil and paraffin had not been cleaned up. I called Clayton King. He claimed that the landowner, Bob Kukla was denying him access to the well. |
| 2097220501 | 2015-06-24 | Production Wells | No Violations | On the day of my inspection I met Clayton King at the well. He started the motor and I witnessed the well pumping. There was pressure on the gauge, and I could feel fluid surging through the lead line as the well pumped. In its current state this well is mechanically capable of production. |
| 210441542 | 2015-6-23 0:00: | PW | No Violations | |
| 229583183 | 2018-4-11 0:00: | PB | No Violations | 0.40 |
| 32054354 | 2014-1-21 0:00: | AM | No Violations | |
| 386042156 | 2013-5-21 0:00: | PW | No Violations | |
| 391587320 | 2015-9-9 0:00:0 | PW | No Violations | |
| 589656275 | 2015-1-16 0:00: | PW | No Violations | |
| 733930665 | 2007-10-17 0:00 | PW | No Violations | |
| 889172601 | 2015-6-23 0:00: | PW | No Violations |
| Inspection ID | Violation ID | Violation Date | Violation Code | Violation Comments |
|---|---|---|---|---|
| 0210441542 | US-OH-121523 | 2015-09-17 | Well operation causing pollution and contamination | |
| 0386042156 | US-OH-124081 | 2015-08-03 | Failure to legibly identify well | |
| 0386042156 | US-OH-124082 | 2015-08-03 | Well shall be plugged | |
| 0386042156 | US-OH-124083 | 2015-08-03 | Statement of annual production not filed | |
| 0733930665 | US-OH-128347 | 2007-10-17 | Well shall be plugged | |
| 1147275259 | US-OH-103817 | 2006-05-10 | Well shall be plugged |
For data sources see[9]