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Well ID: 34-031-25173 | Loading map...
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Country: United States | |
State: Ohio | |
County: Coshocton | |
Municipality: Pike Township | |
Operator Name: T JS OIL & GAS INC | |
Well Pad ID: | |
Farm/Lease Name: CODY | |
License Status: Final Restoration | |
License Date: 2012-12-13 | |
Spud Date: 1984-01-06 | |
Spud Drilling Contractor: LOTHES & LOTHES | |
Final Drill Date: 1984-03-15 | |
Well Total Depth: 3120.00 ft | |
Configuration: Vertical | |
Latitude: 40.170000 | |
Longitude: -82.160000 |
For data sources see[1]
Well Status | Well Status Date | Comment |
---|---|---|
Oil and Gas | 1983-09-19 | Issued Date 9/19/83 Expired Date 3/17/84 Acres 0020000 Tool Type CT Proposed Formation CLINTON Proposed Depth 03120 Proposed Drill Depth 03120 |
Completed | 1984-03-15 | PERMIT EXPIRED |
Reached Total Depth | 1984-03-15 | PERMIT EXPIRED |
CO | 1984-04-21 | 642 LOTHES OIL & GAS INC GeoDate 9/19/83 |
Original Spud | 1985-12-23 | PERMIT EXPIRED |
Completion Report Received | 1986-04-25 | PERMIT EXPIRED |
APP | 2012-12-13 | Proposed Formations:CLINTON, Issued Date:12/13/2012, Expired Date:12/13/2014 12:00:00 PM, Drilling unit acres:20, Proposed Well Type:OG, Proposed Well Class: |
Plugged/Abandoned | 2014-05-28 | PERMIT EXPIRED |
Construction Permit Expires | 2014-12-13 | PERMIT EXPIRED |
Record Last Modified | 2017-02-15 | PERMIT EXPIRED |
For data sources see[2]
Stimulation Date | Chemical Agent | Chemical Agent Concentration (%) | Fracking Fluid Volume | Mass of Proppant Used (lb) | Fracking Company | Comments |
---|---|---|---|---|---|---|
H2O | 0 | 1800 Bbl | 50000 | |||
CO2 | 0 | 19 Tons | 0 |
For data sources see[3]
Period | Operator Name | Gas Quantity (mcf) | Oil Quantity (bbl) | Production Days |
---|---|---|---|---|
1987 | LOTHES JOHN W | 0.00 | 1048.00 | 365 |
1988 | LOTHES JOHN W | 0.00 | 1056.00 | 365 |
1990 | LOTHES JOHN W | 0.00 | 707.00 | 365 |
1991 | LOTHES JOHN W | 0.00 | 860.00 | 365 |
1992 | LOTHES JOHN W | 0.00 | 822.00 | 365 |
1993 | LOTHES JOHN W | 0.00 | 806.00 | 365 |
1994 | LOTHES JOHN W | 0.00 | 580.00 | 365 |
1995 | LOTHES JOHN W | 0.00 | 669.00 | 365 |
1996 | LOTHES JOHN W | 0.00 | 740.00 | 365 |
1997 | LOTHES JOHN W | 0.00 | 550.00 | 365 |
1998 | LOTHES JOHN W | 0.00 | 208.00 | 135 |
1999 | T JS OIL & GAS INC | 0.00 | 310.00 | 365 |
2000 | T JS OIL & GAS INC | 0.00 | 302.00 | 365 |
2001 | T JS OIL & GAS INC | 0.00 | 539.00 | 365 |
2002 | T JS OIL & GAS INC | 0.00 | 443.00 | 365 |
2003 | T JS OIL & GAS INC | 0.00 | 505.00 | 365 |
2004 | T JS OIL & GAS INC | 0.00 | 494.00 | 365 |
2005 | T JS OIL & GAS INC | 0.00 | 563.00 | 365 |
2006 | T JS OIL & GAS INC | 0.00 | 476.00 | 365 |
2007 | T JS OIL & GAS INC | 0.00 | 135.00 | 365 |
2008 | T JS OIL & GAS INC | 0.00 | 93.00 | 365 |
2009 | T JS OIL & GAS INC | 0.00 | 93.00 | 365 |
2010 | T JS OIL & GAS INC | 0.00 | 0.00 | 365 |
2011 | T JS OIL & GAS INC | 0.00 | 0.00 | 0 |
2012 | T JS OIL & GAS INC | 0.00 | 0.00 | 0 |
2013 | T JS OIL & GAS INC | 0.00 | 0.00 | 0 |
2014 | T JS OIL & GAS INC | 0.00 | 0.00 | 0 |
Period | Operator Name | Waste Type | Quantity (bbl) | Production Days |
---|---|---|---|---|
1987 | LOTHES JOHN W | Brine | 0 | 365 |
1988 | LOTHES JOHN W | Brine | 0 | 365 |
1990 | LOTHES JOHN W | Brine | 0 | 365 |
1991 | LOTHES JOHN W | Brine | 0 | 365 |
1992 | LOTHES JOHN W | Brine | 0 | 365 |
1993 | LOTHES JOHN W | Brine | 0 | 365 |
1994 | LOTHES JOHN W | Brine | 0 | 365 |
1995 | LOTHES JOHN W | Brine | 0 | 365 |
1996 | LOTHES JOHN W | Brine | 0 | 365 |
1997 | LOTHES JOHN W | Brine | 0 | 365 |
1998 | LOTHES JOHN W | Brine | 0 | 135 |
1999 | T JS OIL & GAS INC | Brine | 0 | 365 |
2000 | T JS OIL & GAS INC | Brine | 0 | 365 |
2001 | T JS OIL & GAS INC | Brine | 0 | 365 |
2002 | T JS OIL & GAS INC | Brine | 0 | 365 |
2003 | T JS OIL & GAS INC | Brine | 0 | 365 |
2004 | T JS OIL & GAS INC | Brine | 0 | 365 |
2005 | T JS OIL & GAS INC | Brine | 0 | 365 |
2006 | T JS OIL & GAS INC | Brine | 70 | 365 |
2007 | T JS OIL & GAS INC | Brine | 0 | 365 |
2008 | T JS OIL & GAS INC | Brine | 405 | 365 |
2009 | T JS OIL & GAS INC | Brine | 315 | 365 |
2010 | T JS OIL & GAS INC | Brine | 708 | 365 |
2011 | T JS OIL & GAS INC | Brine | 0 | 0 |
2012 | T JS OIL & GAS INC | Brine | 0 | 0 |
2013 | T JS OIL & GAS INC | Brine | 0 | 0 |
2014 | T JS OIL & GAS INC | Brine | 75 | 0 |
Inspection ID | Inspection Date | Inspection Type | Inspection Result | Inspection Comments |
---|---|---|---|---|
-1617749293 | 2014-5-23 0:00: | PB | No Violations | |
-60246489 | 2014-5-27 0:00: | PB | No Violations | |
0060246489 | 2014-05-27 | Plug / Plug Back | No Violations | On the day of my inspection Gene Matheny set a pre-cast cement plug at 828 and washed 5 tons of clay down the well. They pulled 512 of 8.625 casing and washed another 8 tons of clay down the well, filling it to surface. The clay will be allowed to settle overnight. |
0100822203 | 2014-12-15 | Final Restoration | No Violations | On the day of my inspection I found that the site had been graded out to the approximate original contour, seeded and covered in straw. The site was 85% covered in short grasses. I found no signs of erosion. There were no oilfield related materials or debris left at the location. I received a signed landowner waiver to leave the lease road in place. This site passes final restoration. |
100822203 | 2014-12-15 0:00 | FR | No Violations | |
1401285151 | 2014-05-28 | Plug / Plug Back | No Violations | On the day of my inspection I found that the clay had fallen approximately 150 down from surface. Gene Matheny washed another 2 tons of clay down the well, filling it to surface. I checked the well again an hour later and the clay was still sitting firm at the surface. |
1617749293 | 2014-05-23 | Plug / Plug Back | No Violations | The well kicked off when Gene Matheny was pulling the rods. It blew gas for 30 minutes. The well head was intact and they were able to control the kick. They got the well blown down and continued to pull rods and tubing. |
For data sources see[8]