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Well ID: 34-031-25430 | Loading map...
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Country: United States | |
State: Ohio | |
County: Coshocton | |
Municipality: Crawford Township | |
Operator Name: NORTHWOOD ENERGY CORP | |
Well Pad ID: | |
Farm/Lease Name: HERSHBERGER ANDY L | |
License Status: Final Restoration | |
License Date: 2012-04-09 | |
Spud Date: 1984-09-06 | |
Spud Drilling Contractor: R & B DRLG | |
Final Drill Date: 1984-10-11 | |
Well Total Depth: 4393.00 ft | |
Configuration: Vertical | |
Latitude: 40.440000 | |
Longitude: -81.750000 |
For data sources see[1]
Well Status | Well Status Date | Comment |
---|---|---|
Oil and Gas | 1984-08-22 | Issued Date 8/22/84 Expired Date 2/18/85 Acres 0100000 Tool Type CT Proposed Formation CLINTON Proposed Depth 04393 Proposed Drill Depth 04393 |
Original Spud | 1984-09-06 | |
Completed | 1984-10-11 | |
Reached Total Depth | 1984-10-11 | |
CO | 1985-01-29 | 124 MOORE JERRY INC GeoDate 8/22/84 |
Completion Report Received | 1985-01-31 | |
Change of Owner | 1999-10-21 | Operator changed from 4884, EASTERN STATES OIL & GAS INC to 1634, NORTHWOOD ENERGY CORP |
APP | 2004-04-28 | Proposed Formations:CLINTON, Issued Date:4/28/2004, Expired Date:4/28/2005 6:00:00 AM, Drilling unit acres:100, Proposed Well Type:OG, Proposed Well Class: |
APP | 2012-04-09 | Proposed Formations:CLINTON, Issued Date:4/9/2012, Expired Date:4/9/2014 12:00:00 PM, Drilling unit acres:100, Proposed Well Type:OG, Proposed Well Class: |
Plugged/Abandoned | 2012-12-13 | |
Construction Permit Expires | 2014-04-09 | |
Record Last Modified | 2017-02-15 |
For data sources see[2]
Perforation Date | Interval Top (ft) | Interval Base (ft) | Number of Shots |
---|---|---|---|
1997-06-29 | 4264 | 4332 | 0 |
4264 | 4332 | 0 | |
2006-09-11 | 4276 | 4332 | 54 |
4276 | 4332 | 54 | |
4264 | 4332 | 0 |
For data sources see[3]
Stimulation Date | Chemical Agent | Chemical Agent Concentration (%) | Fracking Fluid Volume | Mass of Proppant Used (lb) | Fracking Company | Comments |
---|---|---|---|---|---|---|
ACID | 15 | 300 Gal | 0 | |||
H2O | 0 | 45020 Gal | 40000 | FRAC;H2O,SAND,N2 | ||
N2 | 0 | 10 Mscf | 0 |
For data sources see[4]
Period | Operator Name | Gas Quantity (mcf) | Oil Quantity (bbl) | Production Days |
---|---|---|---|---|
1985 | JERRY MOORE INC | 14976.00 | 104.00 | 0 |
1986 | JERRY MOORE INC | 8400.00 | 14.00 | 365 |
1987 | JERRY MOORE INC | 2946.00 | 0.00 | 365 |
1988 | JERRY MOORE INC | 3094.00 | 20.00 | 365 |
1989 | JERRY MOORE INC | 5944.00 | 30.00 | 365 |
1990 | JERRY MOORE INC | 2219.00 | 16.00 | 365 |
1991 | JERRY MOORE INC | 1785.00 | 0.00 | 365 |
1992 | JERRY MOORE INC | 1153.00 | 10.00 | 365 |
1993 | JERRY MOORE INC | 65.00 | 0.00 | 365 |
1994 | JERRY MOORE INC | 7.00 | 10.00 | 365 |
1995 | JERRY MOORE INC | 2.00 | 0.00 | 365 |
1996 | JERRY MOORE INC | 1.00 | 0.00 | 365 |
1997 | EASTERN STATES OIL & GAS INC | 0.00 | 0.00 | 365 |
1998 | EASTERN STATES OIL & GAS INC | 0.00 | 0.00 | 365 |
1999 | NORTHWOOD ENERGY CORP | 0.00 | 0.00 | 365 |
2000 | NORTHWOOD ENERGY CORP | 0.00 | 0.00 | 365 |
2001 | NORTHWOOD ENERGY CORP | 0.00 | 0.00 | 365 |
2002 | NORTHWOOD ENERGY CORP | 0.00 | 0.00 | 365 |
2003 | NORTHWOOD ENERGY CORP | 0.00 | 0.00 | 365 |
2004 | NORTHWOOD ENERGY CORP | 0.00 | 0.00 | 0 |
2005 | NORTHWOOD ENERGY CORP | 0.00 | 0.00 | 0 |
2006 | NORTHWOOD ENERGY CORP | 0.00 | 0.00 | 0 |
2007 | NORTHWOOD ENERGY CORP | 0.00 | 0.00 | 0 |
2008 | NORTHWOOD ENERGY CORP | 0.00 | 0.00 | 0 |
2009 | NORTHWOOD ENERGY CORP | 0.00 | 0.00 | 0 |
2010 | NORTHWOOD ENERGY CORP | 0.00 | 0.00 | 0 |
2011 | NORTHWOOD ENERGY CORP | 0.00 | 0.00 | 0 |
2012 | NORTHWOOD ENERGY CORP | 0.00 | 0.00 | 0 |
2013 | NORTHWOOD ENERGY CORP | 0.00 | 10.00 | 0 |
Inspection ID | Inspection Date | Inspection Type | Inspection Result | Inspection Comments |
---|---|---|---|---|
-1961089753 | 2012-12-7 0:00: | PB | No Violations | |
-801070948 | 2012-12-11 0:00 | PB | No Violations | |
0801070948 | 2012-12-11 | Plug / Plug Back | No Violations | On the day of my inspection Davis Well Service ripped the 8.625 casing at 260 and pulled one joint. They shoveled approximately 10 tons of clay into the well. |
1354206429 | 2012-11-29 | Plug / Plug Back | No Violations | On the day of my inspection Davis Well Service ran 1.5 tubing to 4000. Cemenco broke circulation and pumped a 400 isolation plug above the Clinton. The service rig could not get the tubing any deeper. They pulled 1000 of tubing and Cemenco circulated the oil into the pit. Appalachian Well Surveys shot the 2.875 tubing off at 3150. Davis Well Service pulled 2 joints and shut the well head in with the tubing set at 3088. |
1354296608 | 2012-11-30 | Production Wells | No Violations | On the day of my inspection Cemenco pumped a 200 plug at the top of the Big Lime and a 200 plug through the Berea. Both plugs were pumped through 2.875 tubing. |
1354646673 | 2012-12-04 | Plug / Plug Back | No Violations | On the day of my inspection Davis Well Service pulled a 12 section of 8 casing and a 21 section of 10 casing. The 8 casing was stuck inside of the 10 section. They separated the two sections of casing, cleaned the threads and screwed the 8 casing back onto the string that was still in the well. The top joint separated immediately when the service rig attempted to pull. The crew will return tomorrow to make another attempt at recovering the 8 casing with a spear. |
1354901374 | 2012-12-05 | Plug / Plug Back | No Violations | On the day of my inspection Davis Well Service successfully made a connection with the spear and the 8 casing. They pulled the casing approximately 20 up the well bore. The casing was pulling very hard and there were many lags in actual pull time to make rig repairs and adjustments. |
1355163260 | 2012-12-10 | Plug / Plug Back | No Violations | On the day of my inspection Davis Well Service cut the collar on the top joint of 8 casing to release the spear. They went in with a ripping tool and got a telegraph at 260. Then they set a brush and stone bridge at 680. They welded the collar shut and began ripping the 8 casing. |
1355407628 | 2012-12-12 | Plug / Plug Back | No Violations | On the day of my inspection Davis Well Service tagged the clay plug at 175 and pulled 4 joints of 8.625 casing. They shoveled approximately 5 tons of clay into the well. They pulled two more joints and put one 13 section of 8.625 casing back in the well. Northwood Energy removed all of the tank battery components. |
1355497853 | 2012-12-13 | Plug / Plug Back | No Violations | On the day of my inspection Davis Well Service pulled the 13 section of 8.625 casing and shoveled 0.5 tons of clay. They set the casing back in the well, driving it down to approximately 36 below grade. Then they shoveled another 0.5 tons of clay to fill the well to surface. |
1371058108 | 2013-06-12 | Final Restoration | No Violations | I received by mail, a signed landowner waiver for the final restoration of this plug well site. This final restoration is passed. |
1961089753 | 2012-12-07 | Plug / Plug Back | No Violations | On the day of my inspection Davis Well Service pulled the 8 casing up to the point where the spear and collar connection was exposed. They were unsuccessful at releasing the spear. The collar will need to be cut open. |
For data sources see[9]