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Well ID: 34-031-26077 | Loading map...
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Country: United States | |
State: Ohio | |
County: Coshocton | |
Municipality: Jackson Township | |
Operator Name: H I SMITH OIL & GAS INC | |
Well Pad ID: | |
Farm/Lease Name: RICHARDS DANIEL | |
License Status: Final Restoration | |
License Date: 2013-02-27 | |
Spud Date: 1987-12-26 | |
Spud Drilling Contractor: ARMSTRONG DRLG | |
Final Drill Date: 1987-12-31 | |
Well Total Depth: 3692.00 ft | |
Configuration: Vertical | |
Latitude: 40.300000 | |
Longitude: -81.960000 |
For data sources see[1]
Well Status | Well Status Date | Comment |
---|---|---|
Oil and Gas | 1987-12-23 | Issued Date 12/23/87 Expired Date 12/22/88 Acres 0030200 Tool Type CRAF Proposed Formation CLINTON Proposed Depth 03692 Proposed Drill Depth 03692 |
Original Spud | 1987-12-26 | IP.A.F. .05MCFG, .05 BBL BRINE:PERMIT EXPIRED |
Completed | 1987-12-31 | IP.A.F. .05MCFG, .05 BBL BRINE:PERMIT EXPIRED |
Reached Total Depth | 1987-12-31 | IP.A.F. .05MCFG, .05 BBL BRINE:PERMIT EXPIRED |
CO | 1988-03-03 | 296 DERRICK PETROLEUM INC GeoDate 12/23/87 |
Completion Report Received | 1989-09-05 | IP.A.F. .05MCFG, .05 BBL BRINE:PERMIT EXPIRED |
Change of Owner | 1998-01-12 | Operator changed from 296, DERRICK PETROLEUM INC to 511, SMITH H I OIL & GAS |
APP | 2013-02-27 | Proposed Formations:CLINTON, Issued Date:2/27/2013, Expired Date:2/27/2015 12:00:00 PM, Drilling unit acres:30.2, Proposed Well Type:TAAD, Proposed Well Class: |
Last Compliance Report | 2014-06-02 | IP.A.F. .05MCFG, .05 BBL BRINE:PERMIT EXPIRED |
Plugged/Abandoned | 2015-02-11 | IP.A.F. .05MCFG, .05 BBL BRINE:PERMIT EXPIRED |
Construction Permit Expires | 2015-02-27 | IP.A.F. .05MCFG, .05 BBL BRINE:PERMIT EXPIRED |
Record Last Modified | 2017-02-15 | IP.A.F. .05MCFG, .05 BBL BRINE:PERMIT EXPIRED |
For data sources see[2]
Perforation Date | Interval Top (ft) | Interval Base (ft) | Number of Shots |
---|---|---|---|
1997-06-29 | 3547 | 3652 | 0 |
3547 | 3652 | 0 | |
2006-09-11 | 3604 | 3652 | 2 |
3604 | 3652 | 2 | |
3547 | 3652 | 0 |
For data sources see[3]
Stimulation Date | Chemical Agent | Chemical Agent Concentration (%) | Fracking Fluid Volume | Mass of Proppant Used (lb) | Fracking Company | Comments |
---|---|---|---|---|---|---|
ACID | 0 | 300 Gal | 0 | FRAC:SAND/WATER/ACID |
For data sources see[4]
Period | Operator Name | Gas Quantity (mcf) | Oil Quantity (bbl) | Production Days |
---|---|---|---|---|
1988 | DERRICK PETROLEUM INC | 7485.00 | 0.00 | 304 |
1989 | DERRICK PETROLEUM INC | 1799.00 | 136.00 | 365 |
1990 | DERRICK PETROLEUM INC | 4176.00 | 128.00 | 365 |
1991 | DERRICK PETROLEUM INC | 2866.00 | 128.00 | 365 |
1992 | DERRICK PETROLEUM INC | 1528.00 | 75.00 | 365 |
1993 | DERRICK PETROLEUM INC | 1377.00 | 39.00 | 365 |
1994 | DERRICK PETROLEUM INC | 947.00 | 45.00 | 365 |
1995 | DERRICK PETROLEUM INC | 693.00 | 94.00 | 181 |
1996 | DERRICK PETROLEUM INC | 0.00 | 0.00 | 0 |
1997 | DERRICK PETROLEUM INC | 0.00 | 0.00 | 0 |
1998 | DERRICK PETROLEUM INC | 0.00 | 0.00 | 0 |
1999 | H I SMITH OIL & GAS INC | 180.00 | 0.00 | 365 |
2000 | H I SMITH OIL & GAS INC | 9.00 | 0.00 | 365 |
2001 | H I SMITH OIL & GAS INC | 2.00 | 0.00 | 365 |
2002 | H I SMITH OIL & GAS INC | 6.00 | 0.00 | 365 |
2003 | H I SMITH OIL & GAS INC | 0.00 | 0.00 | 91 |
2004 | H I SMITH OIL & GAS INC | 53.00 | 22.00 | 365 |
2005 | H I SMITH OIL & GAS INC | 90.00 | 54.00 | 365 |
2006 | H I SMITH OIL & GAS INC | 58.00 | 0.00 | 365 |
2007 | H I SMITH OIL & GAS INC | 114.00 | 152.00 | 365 |
2008 | H I SMITH OIL & GAS INC | 54.00 | 48.00 | 320 |
2009 | H I SMITH OIL & GAS INC | 40.00 | 0.00 | 365 |
2010 | H I SMITH OIL & GAS INC | 52.00 | 44.00 | 365 |
2011 | H I SMITH OIL & GAS INC | 77.00 | 0.00 | 0 |
2012 | H I SMITH OIL & GAS INC | 90.00 | 73.00 | 366 |
2013 | H I SMITH OIL & GAS INC | 0.00 | 0.00 | 0 |
2014 | H I SMITH OIL & GAS INC | 0.00 | 0.00 | 365 |
2015 | H I SMITH OIL & GAS INC | 0.00 | 0.00 | 0 |
Inspection ID | Inspection Date | Inspection Type | Inspection Result | Inspection Comments |
---|---|---|---|---|
-1129248599 | 2015-1-30 0:00: | PB | No Violations | |
-2028790757 | 2015-10-23 0:00 | FR | No Violations | 0.50 |
-531170069 | 2009-12-17 0:00 | PW | No Violations | |
-581948645 | 2014-5-21 0:00: | AD | No Violations | |
-702129226 | 2015-1-31 0:00: | PB | No Violations | |
-719338431 | 2004-2-18 0:00: | AD | No Violations | |
0266692218 | 2016-12-05 | Final Restoration | No Violations | On the day of my inspection I found that the well site was covered with grasses and weeds. There were no erosion issues. Parts of the original access road were covered in grass and other parts had been incorporated into a new gravel drive for non-oilfield related land use. This site passes final restoration. |
0413049824 | 2015-02-11 | Plug / Plug Back | No Violations | On the day of my inspection I found that Gene Matheney had tubing ran to 195. Cemenco established circulation and pumped the surface plug with 60 sacks of class A cement. The cement was circulated to surface and fell 10 feet when they stopped pumping. Matheney cut the casing off 36 below grade and capped the well with a steel plate inscribed with 6077. |
0531170069 | 2009-12-17 | Production Wells | No Violations | Pumping well capable of production . |
0581948645 | 2014-05-21 | Annular Disposal | No Violations | At the time of my inspection I found that annular disposal was not in use at this well. |
0702129226 | 2015-01-31 | Plug / Plug Back | No Violations | On the day of my inspection I found that Gene Matheney had tubing ran to 2502. Petroset pumped 50 barrels of water and could not establish circulation. The fluid was approximately 10 down. They pumped a cement plug at the top of the Big Lime. Petroset pumped another cement plug 50 below the Berea and at the base of the surface casing. The well still did not circulate. Matheny pulled the tubing and checked the fluid level. The fluid was down approximately 250. They tried to bridge the well at 250 with stone and debris. Petroset pumped 100 barrels of cement and the fluid was still down 250. I recommended that they shut down for the day, let the cement set up and return to complete the plug job. |
0719338431 | 2004-02-18 | Annular Disposal | No Violations | No annular disposal hooked up . |
1129248599 | 2015-01-30 | Plug / Plug Back | No Violations | On the day of my inspection I found that Petroset had pumped a cement bottom plug through tubing. Gene Matheney ripped the 4.5 casing at 2510 and pulled it from the well. Then he ran tubing to set the Big Lime plug. |
1402650305 | 2015-08-21 | Final Restoration | No Violations | On the day of my inspection I found that the pit was still open and the site had not been graded out. The site and lease road were fully covered in vegetation and I found no erosion down the lease road, but the well site was very rough. There were multiple ruts and depressions from the plug job. There was also a water course that had washed out across the site. I called Rick Smith. He claimed that he was not aware that the site had been left in that condition and he would be out next week to address the restoration. |
1415564962 | 2015-09-03 | Final Restoration | No Violations | On the day of my inspection I found that the pit had been closed. The site had been graded out, seeded and covered in straw. The former tank battery site had also been graded out , seeded and covered in straw. The work was fresh and no grass had started to grow yet. |
1422720072 | 2015-01-28 | Plug / Plug Back | No Violations | On the day of my inspection I found that Gene Matheney was moved in and rigged up to plug this well. He was running tubing to set the bottom plug with cement. |
1604788456 | 2015-02-05 | Plug / Plug Back | No Violations | On the day of my inspection I used a fishing pole equipped with a weight to determine the depth of the fluid and the top of the cement. I found the fluid to be at approximately 40 and the cement was down approximately 288. I contacted Rick Smith to discuss his options for finishing the plug job. |
1652184759 | 2008-10-30 | Annular Disposal | No Violations | Well capable of production . No annular disposal hooked up |
2028790757 | 2015-10-23 | Final Restoration | No Violations | On the day of my inspection I found that there was minimal grass growth on the site. The access road was 80% grown over with grass. There were no erosion issues at the well site or down the access road. |
266692218 | 2016-12-5 0:00: | FR | No Violations | 1.00 |
413049824 | 2015-2-11 0:00: | PB | No Violations |
For data sources see[9]