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Well ID: 34-031-26310 | Loading map...
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Country: United States | |
State: Ohio | |
County: Coshocton | |
Municipality: Linton Township | |
Operator Name: RHDK OIL & GAS LLC/DBA RED HIL | |
Well Pad ID: | |
Farm/Lease Name: BRELSFORD HOWARD | |
License Status: Producing | |
License Date: 1990-10-10 | |
Spud Date: 1990-10-21 | |
Spud Drilling Contractor: CUBBY DRLG | |
Final Drill Date: 1990-10-27 | |
Well Total Depth: 6820.00 ft | |
Configuration: Vertical | |
Latitude: 40.190000 | |
Longitude: -81.730000 |
For data sources see[1]
Well Status | Well Status Date | Comment |
---|---|---|
CO | 1990-10-10 | 168 RED HILL DEVELOPMENT GeoDate 10/10/90 |
Oil and Gas | 1990-10-10 | Issued Date 10/10/90 Expired Date 10/10/91 Acres 0132430 Tool Type RTAF Proposed Formation CL/ROSE RUN Proposed Depth 06820 Proposed Drill Depth 06820 |
Original Spud | 1990-10-18 | |
Completed | 1990-10-27 | |
Reached Total Depth | 1990-10-27 | |
Completion Report Received | 1991-05-28 | |
Construction Permit Expires | 1991-10-10 | |
Record Last Modified | 2017-02-15 |
For data sources see[2]
Perforation Date | Interval Top (ft) | Interval Base (ft) | Number of Shots |
---|---|---|---|
1997-06-29 | 4184 | 4281 | 0 |
4184 | 4281 | 0 | |
2006-09-11 | 4229 | 4268 | 7 |
4229 | 4268 | 7 | |
4184 | 4281 | 0 |
For data sources see[3]
Stimulation Date | Chemical Agent | Chemical Agent Concentration (%) | Fracking Fluid Volume | Mass of Proppant Used (lb) | Fracking Company | Comments |
---|---|---|---|---|---|---|
H2O | 0 | 77904 Gal | 0 | FRAC W/77,904 GAL SLICKWATER |
For data sources see[4]
Inspection ID | Inspection Date | Inspection Type | Inspection Result | Inspection Comments |
---|---|---|---|---|
-1471005618 | 2016-3-7 0:00:0 | PW | No Violations | 0.70 |
-1756317969 | 2011-10-28 0:00 | PW | No Violations | |
-2071064449 | 2013-3-6 0:00:0 | PW | No Violations | |
-484340718 | 2002-12-16 0:00 | PW | No Violations | |
0000010872 | Preliminary Restoration | No Violations | PASSED Y WITNESSED 11/21/91 INSPECTOR ROCKY KING DATE 11/2119/91 DATA FROM OLD VAX INFO | |
0484340718 | 2002-12-16 | Production Wells | No Violations | |
10872 | PL | No Violations | ||
1197391343 | 2007-11-01 | Production Wells | No Violations | Well in production . |
1218840511 | 2008-12-04 | Production Wells | No Violations | Well capable of production . |
1248884785 | 2009-07-29 | Production Wells | No Violations | Gas well capable of production . |
1471005618 | 2016-03-07 | Production Wells | No Violations | On the day of my inspection I found that the well was being produced with a plunger lift system. The surface casing head was buried and not visible. One of the casing valves was closed, the other was partially opened and connected to the control box with 3/8 tubing. The 2 line off of the casing also connected to a domestic gas meter and plastic line. The 2 line off of the tubing was equipped with a motor valve. The tubing gauge showed 200 psi. The tank battery consisted of one 140 barrel steel tank and one horizontal separator. The load valves on the tank were equipped with plugs. An earthen dike was in place around the production equipment. The identification sign posted on the tank was correctly filled out and legible. I found no leaks or spills around the wellhead or at the tank battery. |
1756317969 | 2011-10-28 | Production Wells | No Violations | Well capable of production. |
1926584466 | 2003-11-06 | Production Wells | No Violations | Well in production. |
2071064449 | 2013-03-06 | Production Wells | No Violations | On the day of my inspection I found that the well head was equipped with a plunger lift system. The tank battery consisted of one 210 barrel stock tank, one separator and an earthen dike. There were no leaks or spills and proper identification was posted. No violations at this time. |
For data sources see[9]