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34-031-26449

Well Details

Well ID: 34-031-26449
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Country: United States
State: Ohio
County: Coshocton
Municipality: Jackson Township
Operator Name: M & R INVESTMENTS OHIO LLC
Well Pad ID:
Farm/Lease Name: OXFORD-PEABODY
License Status: Final Restoration
License Date: 2016-02-18
Spud Date: 1994-04-20
Spud Drilling Contractor: PROFESSIONAL WELL SVC-PWS
Final Drill Date: 1994-04-23
Well Total Depth: 3845.00 ft
Configuration: Vertical
Latitude: 40.260000
Longitude: -81.960000

For data sources see[1]

Well History

Well Status Well Status Date Comment
Oil and Gas 1993-03-19 Issued Date 3/19/93 Expired Date 3/19/94 Acres 0020000 Tool Type CRAF Proposed Formation CLINTON Proposed Depth Proposed Drill Depth
CO 1994-03-25 79 OXFORD OIL CO GeoDate 3/25/94
Oil and Gas 1994-03-25 Issued Date 3/25/94 Expired Date Acres 0020000 Tool Type RTAF Proposed Formation CLINTON Proposed Depth Proposed Drill Depth
Original Spud 1994-04-20 RI 3-26-94
Completed 1994-04-23 RI 3-26-94
Reached Total Depth 1994-04-23 RI 3-26-94
CO 1994-06-15 79 OXFORD OIL CO GeoDate 3/19/93
Completion Report Received 1994-07-05 RI 3-26-94
APP 2010-07-07 Proposed Formations:CLINTON, Issued Date:7/7/2010, Expired Date:7/7/2011 6:00:00 AM, Drilling unit acres:20, Proposed Well Type:OG, Proposed Well Class:
APP 2011-07-26 Proposed Formations:CLINTON, Issued Date:7/26/2011, Expired Date:7/25/2013 12:00:00 PM, Drilling unit acres:20, Proposed Well Type:OG, Proposed Well Class:
APP 2013-02-06 Proposed Formations:CLINTON, Issued Date:2/6/2013, Expired Date:2/6/2015 12:00:00 PM, Drilling unit acres:20, Proposed Well Type:OG, Proposed Well Class:
Change of Owner 2014-02-06 Operator changed from 79, OXFORD OIL to 9216, ECLIPSE RESOURCES-OHIO LLC
APP 2014-07-15 Proposed Formations:CLINTON, Issued Date:7/15/2014, Expired Date:7/14/2016 12:00:00 PM, Drilling unit acres:20, Proposed Well Type:OG, Proposed Well Class:
APP 2016-02-18 Proposed Formations:CLINTON/MEDINA, Issued Date:2/18/2016, Expired Date:2/17/2018 12:00:00 PM, Drilling unit acres:20, Proposed Well Type:OG, Proposed Well Class:
Plugged/Abandoned 2016-07-25 RI 3-26-94
Change of Owner 2016-08-02 Operator changed from 9216, ECLIPSE RESOURCES-OHIO LLC to 8685, M & R INVESTMENTS OHIO LLC
Record Last Modified 2017-02-15 RI 3-26-94
Construction Permit Expires 2018-02-17 RI 3-26-94

For data sources see[2]

Perforation Treatments

Perforation Date Interval Top (ft) Interval Base (ft) Number of Shots
2006-09-11 3722 3757 17
3664 3756 0
1997-06-29 3664 3756 0
3706 3710 3
3664 3756 0
2006-09-11 3706 3710 3

For data sources see[3]

Stimulations Data

Stimulation Date Chemical Agent Chemical Agent Concentration (%) Fracking Fluid Volume Mass of Proppant Used (lb) Fracking Company Comments
H2O 1420 2132 Bbl 30000 FRAC W/2132 BW & 300 SX SAND

For data sources see[4]

Production Data

Period Operator Name Gas Quantity (mcf) Oil Quantity (bbl) Production Days
1994 OXFORD OIL 3948.00 713.00 205
1995 OXFORD OIL 4202.00 573.00 365
1996 OXFORD OIL 2704.00 364.00 366
1997 OXFORD OIL 6953.00 240.00 365
1998 OXFORD OIL 4104.00 122.00 365
1999 OXFORD OIL 2387.00 139.00 365
2000 OXFORD OIL 1501.00 68.00 0
2001 OXFORD OIL 1467.00 119.00 365
2002 OXFORD OIL 1343.00 74.00 365
2003 OXFORD OIL 1079.00 48.00 365
2004 OXFORD OIL 1140.00 48.00 365
2005 OXFORD OIL 829.00 0.00 365
2006 OXFORD OIL 615.00 101.00 365
2007 OXFORD OIL 503.00 49.00 365
2008 OXFORD OIL 745.00 73.00 0
2009 OXFORD OIL 661.00 45.00 0
2010 OXFORD OIL 368.00 0.00 365
2011 OXFORD OIL 280.00 0.00 0
2012 OXFORD OIL 349.00 26.00 0
2013 ECLIPSE RESOURCES-OHIO LLC 295.00 0.00 365
2014 ECLIPSE RESOURCES-OHIO LLC 259.00 14.00 365
2015 ECLIPSE RESOURCES-OHIO LLC 0.00 0.00 365
2016 M & R INVESTMENTS OHIO LLC 0.00 0.00 365

For data sources see[5] [6]

Waste Data

Period Operator Name Waste Type Quantity (bbl) Production Days
1994 OXFORD OIL Brine 225 205
1995 OXFORD OIL Brine 20 365
1996 OXFORD OIL Brine 25 366
1997 OXFORD OIL Brine 228 365
1998 OXFORD OIL Brine 27 365
1999 OXFORD OIL Brine 33 365
2000 OXFORD OIL Brine 8
2001 OXFORD OIL Brine 14 365
2002 OXFORD OIL Brine 5 365
2003 OXFORD OIL Brine 14 365
2004 OXFORD OIL Brine 0 365
2005 OXFORD OIL Brine 9 365
2006 OXFORD OIL Brine 7 365
2007 OXFORD OIL Brine 0 365
2008 OXFORD OIL Brine 33
2009 OXFORD OIL Brine 7
2010 OXFORD OIL Brine 102 365
2011 OXFORD OIL Brine 0
2012 OXFORD OIL Brine 0
2013 ECLIPSE RESOURCES-OHIO LLC Brine 0 365
2014 ECLIPSE RESOURCES-OHIO LLC Brine 7 365
2015 ECLIPSE RESOURCES-OHIO LLC Brine 0 365
2016 M & R INVESTMENTS OHIO LLC Brine 0 365

For data sources see[7] [8]

Inspection Data

Inspections Performed

Inspection ID Inspection Date Inspection Type Inspection Result Inspection Comments
-1256186053 2003-3-27 0:00: PL No Violations
-1578852493 2016-12-5 0:00: FR No Violations 1.00
-1834126907 2016-10-14 0:00 FR No Violations 1.00
-1908944857 2016-5-24 0:00: PW No Violations 0.50
-339749510 2015-12-10 0:00 PW No Violations 2.00
-696456522 2016-8-10 0:00: FR No Violations 1.00
-704502804 2015-9-16 0:00: PW No Violations
-980816604 2016-7-21 0:00: PB No Violations 2.00
0092549033 2016-07-12 Administrative Inspection No Violations I contacted Bruce Carpenter with eclipse to ask about their plans for plugging the well. Bruce claimed that the plugging contractor, Barry Bowers, was scheduled to move in and rig up on Wed. July 13.
0339749510 2015-12-10 Production Wells Violations Noted On the day of my inspection I found that the wellhead was equipped with tubing and rods. The pumping unit was removed. The valves on the tubing and casing were both closed. This well is idle and not capable of production in its current state. The well owner/operator shall submit a written plugging schedule to Chris Grimm at 5880 Memory Rd, Zanesville, OH 43701 within 30 days, per OAC 1501:9-11-05(B), and plug the well within 180 days. The well owner/operator will be notified if the plugging schedule is approved or denied.
0564246271 2007-02-16 Production Wells No Violations Well capable of production . Snow cover well site
0696456522 2016-08-10 Final Restoration No Violations On the day of my inspection I found that the flow line was still in place and the site had not been seeded. There were no signs that the plugged well was leaking, and there were no erosion issues.
0704502804 2015-09-16 Production Wells No Violations On the day of my inspection I found that the wellhead was equipped with tubing and rods. The pumping unit had been removed. The valves were closed. The former access road was overgrown with thick vegetation. This well is idle and not capable of production in its current state. I called Dale Smith of Eclipse to ask about their plans for plugging the well. There was a re-issue plugging permit issued on 7/15/2014. He acknowledged that the well was idle and said he would get back to me on its status in the plugging program.
0825994155 2005-05-05 Production Wells No Violations Well in production .
0980816604 2016-07-21 Plug / Plug Back No Violations On the day of my inspection I found that Huffman Bowers Well Service was pulling 2452 of 4.5 casing from the well, and running 1.5 tubing back down to the top of the Big Lime. They projected to be back on Monday, July 25 to set the cement plugs and finish the job.
1124806559 2016-07-14 Plug / Plug Back No Violations On the day of my inspection I found that the rods had been pulled and staged on a trailer. The tubing was still in the well. I met with Eddie Moss of Diversified Resources when he was out to haul the rods away. He claimed that the crew would not be working today. They would be back on Friday to pull tubing and then he would decide if they would steam the tubing on site to be used in the plug job, or bring in a new string.
1133795933 2016-06-01 Administrative Inspection No Violations I was contacted by Bruce Carpenter of Eclipse Resources to request a 30 day extension on the compliance notice to plug the well. Bruce alleged that the well had been sold to Diversified Resources and the purpose of the extension request was to allow adequate time for the transfer to be processed. I granted the extension.
1256186053 2003-03-27 Preliminary Restoration No Violations PASTED
1450465581 2015-12-16 Administrative Inspection No Violations I received email correspondence from Rocky King, EHSR field tech for Eclipse Resources, in response to the compliance notice. The email states that the action plan is to plug and abandon the well before the 6/10/16 due date.
1468434226 2016-07-13 Plug / Plug Back No Violations On the day of my inspection Barry Bowers was moving in and rigging up to plug the well. Rocky King, consultant for Eclipse Resources and Eddie Moss of Diversified Resources were on site. Bowers crew cleared the access road to the well and cleared the well site. They brought the rig in and rigged up. Then they dug the pit and lined it. They started pulling rods and laying them on a trailer. The area around the wellhead and the ditch to the pit were also lined. The paraffin from the rods was contained on the liner.
1468591756 2016-07-15 Plug / Plug Back No Violations On the day of my inspection I found that Barry Bowers crew was on location pulling the tubing form the well. The tubing was packed with paraffin and pulling wet. The water from the tubing was splashing on the ground around the wellhead and rig. I spoke to the rig operator and requested that he use the dozer to push a berm around the wellhead to contain the fluid being brought up with the tubing. Although the pit and the ditch to the pit were lined, the excess fluid was running in the opposite direction. The earthen berm was successful at temporarily containing the water. I wrote a plugging plan for the well and gave a copy to Eddie Moss and the service rig operator.
1469041461 2016-07-20 Plug / Plug Back No Violations On the day of my inspection I found that Huffman Bowers Well Services had 1.5 tubing set at 3755. Barry Bowers pumped a 25 sack cement bottom plug. The rig crew pulled the tubing from the well and went in to rip casing. They informed me that the original 2.375 tubing was badly corroded and deteriorated from 2500 to 2800. They ran in with ripping tools to 3200. They had brief telegraphs, but could not get the tools to set down. They pulled up and made multiple attempts with no success. They crew finally got a solid telegraph at 2452 and got the casing to part at that depth. They pulled one joint and shut down for the night. They packed the wellhead off and capped the 4.5 casing with a swage and valve before leaving.
1469453132 2016-07-25 Plug / Plug Back No Violations On the day of my inspection I found that Huffman Bowers Inc. had 1.5 tubing set at 2425. Barry Bowers pumped a 250 cement isolation plug just above the top of the Big Lime. The service rig crew pulled the tubing up to 1118 and Barry Bowers pumped a 178 cement plug through the Berea sandstone. Then they pulled up to 707 and Barry Bowers pumped a 200 cement plug at the base of the surface casing. Then they pulled up to 200 for the surface plug. Barry Bowers pumped until cement was circulated to the surface. The cement fell back 3 feet down the hole when Barry finished pumping and stayed up. The well had been plugged and abandoned. This violation is resolved.
1578852493 2016-12-05 Final Restoration No Violations On the day of my inspection I found that the well site and access road were covered in short grasses. There were no erosion issues. There were no materials or debris left behind. The tank battery is still in use for permits 6649 and 6650. This site passes final restoration.
1834126907 2016-10-14 Final Restoration No Violations On the day of my inspection I found that the flow line had been removed. I found no other oilfield related materials or debris at the plugged well site. The soil had been final graded and seeded. There was moderate grass growth, with only 50 to 60 percent coverage. There were no issues with erosion.
1908944857 2016-05-24 Production Wells No Violations On the day of my inspection I found that the well was still equipped with tubing and rods, and the valves were closed. I contacted Bruce Carpenter with Eclipse to ask what the plan was for the well. The outstanding compliance notice requires that the well be plugged by 6/10/16. Bruce took the information and said that he would get back to me tomorrow to let me know if the well was included in the transfer to Diversified Resources or retained by Eclipse.
2006210207 2016-08-02 Plug / Plug Back No Violations On the day of my inspection I found that the pit had been closed and the site had been final graded. There were no plugging materials or debris left behind. There was one section of 2 flow line that was still in place along the tree line toward the access road. There was also a dozer left at the site. Eddie Moss of Diversified Resources arrived to pick up the dozer while I was on the site. He claimed that Dale Smith had the casing cut off and capped the well with a steel plate prior to grading the site. I pointed out the flow line to Eddie. He said that they would get it out of there when they were out to seed the site. The tank battery is still in use for permits 6649 and 6650.
564246271 2007-2-16 0:00: PW No Violations
825994155 2005-5-5 0:00:0 PW No Violations
92549033 2016-7-12 0:00: AM No Violations

Violations Commited

Inspection ID Violation ID Violation Date Violation Code Violation Comments
0339749510 US-OH-123542 2016-08-12 Well shall be plugged

For data sources see[9]

References