If you find this page useful and would like to be notified of changes made to this page, start by inputting your email below.
powered by ChangeDetection
Well ID: 34-031-26726 | Loading map...
{"type":"SATELLITE","minzoom":false,"maxzoom":false,"types":["ROADMAP","SATELLITE","HYBRID","TERRAIN"],"mappingservice":"googlemaps3","width":"100%","height":"350px","centre":false,"title":"","label":"","icon":"","visitedicon":"","lines":[],"polygons":[],"circles":[],"rectangles":[],"wmsoverlay":false,"copycoords":false,"static":false,"zoom":14,"layers":[],"controls":["pan","zoom","type","scale","streetview","rotate"],"zoomstyle":"DEFAULT","typestyle":"DEFAULT","autoinfowindows":false,"resizable":false,"kmlrezoom":false,"poi":true,"markercluster":false,"clustergridsize":60,"clustermaxzoom":20,"clusterzoomonclick":true,"clusteraveragecenter":true,"clusterminsize":2,"imageoverlays":[],"kml":[],"gkml":[],"searchmarkers":"","enablefullscreen":false,"scrollwheelzoom":false,"locations":[{"text":"","title":"","link":"","lat":40.35,"lon":-82.03,"icon":""}]} |
Country: United States | |
State: Ohio | |
County: Coshocton | |
Municipality: Jefferson Township | |
Operator Name: KMFAD OIL AND GAS LLC | |
Well Pad ID: | |
Farm/Lease Name: HETTINGER UNIT | |
License Status: Producing | |
License Date: 1998-03-03 | |
Spud Date: 1998-04-01 | |
Spud Drilling Contractor: PEP DRLG | |
Final Drill Date: 1998-04-08 | |
Well Total Depth: 5680.00 ft | |
Configuration: Vertical | |
Latitude: 40.350000 | |
Longitude: -82.030000 |
For data sources see[1]
Well Status | Well Status Date | Comment |
---|---|---|
APP | 1998-03-03 | Proposed Formations:ROSE RUN, Issued Date:3/3/98, Expired Date:3/3/99 6:00:00 AM, Drilling unit acres:40, Proposed Well Type:OG, Proposed Well Class:POOL |
Original Spud | 1998-04-01 | RBDMS Rec |
Completed | 1998-04-08 | RBDMS Rec |
Reached Total Depth | 1998-04-08 | RBDMS Rec |
Completion Report Received | 1998-05-11 | RBDMS Rec |
Construction Permit Expires | 1999-03-03 | RBDMS Rec |
Change of Owner | 2003-03-06 | Operator changed from 124, MOORE JERRY INC to 7404, A S N F PRODUCING INC |
Change of Owner | 2014-08-19 | Operator changed from 7404, A S N F PRODUCING INC to 9316, KMFAD OIL AND GAS LLC |
Record Last Modified | 2017-02-15 | RBDMS Rec |
For data sources see[2]
Stimulation Date | Chemical Agent | Chemical Agent Concentration (%) | Fracking Fluid Volume | Mass of Proppant Used (lb) | Fracking Company | Comments |
---|---|---|---|---|---|---|
Not Treated | 0 | 0 | 0 |
For data sources see[3]
Period | Operator Name | Gas Quantity (mcf) | Oil Quantity (bbl) | Production Days |
---|---|---|---|---|
1998 | JERRY MOORE INC | 38402.00 | 1601.00 | 365 |
1999 | JERRY MOORE INC | 22987.00 | 630.00 | 365 |
2000 | JERRY MOORE INC | 32938.00 | 1076.00 | 365 |
2001 | JERRY MOORE INC | 20125.00 | 499.00 | 365 |
2002 | JERRY MOORE INC | 9181.00 | 293.00 | 365 |
2003 | JERRY MOORE INC | 337.00 | 24.00 | 365 |
2004 | A S N F PRODUCING INC | 6197.00 | 282.00 | 365 |
2005 | A S N F PRODUCING INC | 2427.00 | 98.00 | 365 |
2006 | A S N F PRODUCING INC | 1454.00 | 101.00 | 365 |
2007 | A S N F PRODUCING INC | 1093.00 | 89.00 | 365 |
2008 | A S N F PRODUCING INC | 554.00 | 47.00 | 365 |
2009 | A S N F PRODUCING INC | 287.00 | 0.00 | 365 |
2010 | A S N F PRODUCING INC | 205.00 | 15.00 | 365 |
2011 | A S N F PRODUCING INC | 11.00 | 0.00 | 365 |
2012 | A S N F PRODUCING INC | 272.00 | 0.00 | 366 |
2013 | A S N F PRODUCING INC | 109.00 | 0.00 | 365 |
2014 | KMFAD OIL AND GAS LLC | 3.00 | 32.00 | 365 |
2015 | KMFAD OIL AND GAS LLC | 10.00 | 71.00 | 365 |
2016 | KMFAD OIL AND GAS LLC | 10.00 | 35.00 | 365 |
2017 | KMFAD OIL AND GAS LLC | 10.00 | 0.00 | 365 |
Period | Operator Name | Waste Type | Quantity (bbl) | Production Days |
---|---|---|---|---|
1998 | JERRY MOORE INC | Brine | 1200 | 365 |
1999 | JERRY MOORE INC | Brine | 0 | 365 |
2000 | JERRY MOORE INC | Brine | 0 | 365 |
2001 | JERRY MOORE INC | Brine | 0 | 365 |
2002 | JERRY MOORE INC | Brine | 30 | 365 |
2003 | JERRY MOORE INC | Brine | 0 | 365 |
2004 | A S N F PRODUCING INC | Brine | 231 | 365 |
2005 | A S N F PRODUCING INC | Brine | 35 | 365 |
2006 | A S N F PRODUCING INC | Brine | 30 | 365 |
2007 | A S N F PRODUCING INC | Brine | 0 | 365 |
2008 | A S N F PRODUCING INC | Brine | 0 | 365 |
2009 | A S N F PRODUCING INC | Brine | 35 | 365 |
2010 | A S N F PRODUCING INC | Brine | 0 | 365 |
2011 | A S N F PRODUCING INC | Brine | 0 | 365 |
2012 | A S N F PRODUCING INC | Brine | 0 | 366 |
2013 | A S N F PRODUCING INC | Brine | 0 | 365 |
2014 | KMFAD OIL AND GAS LLC | Brine | 20 | 365 |
2015 | KMFAD OIL AND GAS LLC | Brine | 0 | 365 |
2016 | KMFAD OIL AND GAS LLC | Brine | 0 | 365 |
2017 | KMFAD OIL AND GAS LLC | Brine | 0 | 365 |
Inspection ID | Inspection Date | Inspection Type | Inspection Result | Inspection Comments |
---|---|---|---|---|
-1352100705 | 2019-11-21 0:00 | PW | No Violations | 1.00 |
-576361431 | 2019-11-4 0:00: | PW | No Violations | 0.50 |
-576559681 | 2012-10-3 0:00: | PW | No Violations | |
0141698016 | 2003-05-21 | Preliminary Restoration | No Violations | pasted |
0576559681 | 2012-10-03 | Production Wells | Violations Noted | I received a phone call from Dean Hettinger (740-502-2859) requesting an inspection of wells on his family property. On the day of my inspection I found that the well head was equipped with a plunger lift system and connected to a tank battery that consisted of one 210 barrel stock tank and one separator. There were no leaks or spills around the tank battery and proper identification was posted. There was a 3 to 4 diameter circle of contaminated soil under the solvent tank next to the well head. The contaminated soil needs to be cleaned up. There was a pvc drain through the wall of the dike. This drain must either be removed, capped or equipped with a valve. |
1142962076 | 2006-03-21 | Production Wells | No Violations | Well in production , 1-300 bl. Tank not diked . |
141698016 | 2003-5-21 0:00: | PL | No Violations | |
1683683002 | 2012-11-07 | Production Wells | No Violations | On the day of my inspection I found that the solvent injector had been removed from the site and all contaminated soil at the well head had been removed. The pvc drain in the dike was had also been removed. No violations at this time. |
Inspection ID | Violation ID | Violation Date | Violation Code | Violation Comments |
---|---|---|---|---|
0576559681 | US-OH-126464 | 2013-01-04 | Well operation causing pollution and contamination | |
0576559681 | US-OH-126465 | 2013-01-04 | Dike or pit not able to prevent escape of brine or other wastes |
For data sources see[8]