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Well ID: 34-031-27178 | Loading map...
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Country: United States | |
State: Ohio | |
County: Coshocton | |
Municipality: Tuscarawas Township | |
Operator Name: BUCKEYE BRINE LLC | |
Well Pad ID: | |
Farm/Lease Name: ADAMS (SWIW #11) | |
License Status: Active Injection | |
License Date: 2011-10-31 | |
Spud Date: 2013-10-12 | |
Spud Drilling Contractor: WILDCAT DRILLING | |
Final Drill Date: 2013-11-07 | |
Well Total Depth: 7016.00 ft | |
Configuration: Vertical | |
Latitude: 40.300000 | |
Longitude: -81.840000 |
For data sources see[1]
Well Status | Well Status Date | Comment |
---|---|---|
APP | 2011-10-31 | Proposed Formations:ROSE RUN - MT. SIMON SANDSTONE, Issued Date:10/31/2011, Expired Date:10/30/2013 12:00:00 PM, Drilling unit acres:0, Proposed Well Type:SWD, Proposed Well Class:SWIW |
Last Compliance Report | 2011-10-31 | |
Correction to Well | 2011-11-10 | CORRECTION TO FOOTAGE |
Original Spud | 2013-10-12 | |
Construction Permit Expires | 2013-10-30 | |
Reached Total Depth | 2013-11-07 | |
Change of Owner | 2014-03-19 | Operator changed from 8613, PREFERRED FLUIDS MGT LLC to 9245, BUCKEYE BRINE LLC |
Completion Report Received | 2014-09-30 | |
Record Last Modified | 2015-09-24 |
For data sources see[2]
Inspection ID | Inspection Date | Inspection Type | Inspection Result | Inspection Comments |
---|---|---|---|---|
-1046160860 | 2017-4-10 0:00: | SW | No Violations | |
-1057381170 | 2019-6-26 0:00: | SW | No Violations | |
-1100675638 | 2018-5-1 0:00:0 | SW | No Violations | |
-1165054830 | 2020-8-4 0:00:0 | SW | No Violations | |
-1195004129 | 2017-12-20 0:00 | SW | No Violations | |
-1203275818 | 2014-10-17 0:00 | SW | No Violations | |
-1237097182 | 2017-10-16 0:00 | SW | No Violations | |
-1240427421 | 2015-12-28 0:00 | SW | No Violations | |
-1240600126 | 2015-9-22 0:00: | SW | No Violations | |
-126439358 | 2014-11-6 0:00: | SW | No Violations | |
-1290366762 | 2018-12-14 0:00 | SW | No Violations | |
-1297202599 | 2016-4-18 0:00: | SW | No Violations | |
-1311907757 | 2019-8-29 0:00: | SW | No Violations | |
-1366400626 | 2017-6-19 0:00: | SW | No Violations | |
-1435043998 | 2015-11-23 0:00 | SW | No Violations | |
-1495330398 | 2016-9-1 0:00:0 | SW | No Violations | |
-1504996033 | 2016-11-3 0:00: | SW | No Violations | |
-1514791716 | 2015-8-3 0:00:0 | SW | No Violations | |
-1652717491 | 2013-11-4 0:00: | SW | No Violations | |
-1672668482 | 2015-7-9 0:00:0 | PL | No Violations | |
-1699471152 | 2015-2-25 0:00: | SW | No Violations | |
-1710506952 | 2018-3-23 0:00: | SW | No Violations | |
-1735757767 | 2017-3-24 0:00: | SW | No Violations | |
-1740583739 | 2014-6-2 0:00:0 | PL | No Violations | |
-1746479876 | 2015-12-18 0:00 | SW | No Violations | |
-177317997 | 2018-6-21 0:00: | SW | No Violations | |
-1790955866 | 2017-7-18 0:00: | SW | No Violations | |
-1832466926 | 2017-4-19 0:00: | SW | No Violations | |
-2012450470 | 2014-6-25 0:00: | SW | No Violations | |
-2013020827 | 2019-7-24 0:00: | SW | No Violations | |
-2032990822 | 2013-9-23 0:00: | DD | No Violations | |
-2115705947 | 2015-6-22 0:00: | SW | No Violations | |
-224363530 | 2018-10-16 0:00 | SW | No Violations | |
-225479679 | 2016-2-2 0:00:0 | SW | No Violations | |
-226208644 | 2016-11-18 0:00 | SW | No Violations | |
-285455196 | 2013-11-7 0:00: | DD | No Violations | |
-307300214 | 2019-4-14 0:00: | SW | No Violations | |
-31557423 | 2018-1-17 0:00: | SW | No Violations | |
-348688084 | 2015-2-13 0:00: | SW | No Violations | |
-353483128 | 2016-7-14 0:00: | SW | No Violations | |
-354668962 | 2017-11-30 0:00 | SW | No Violations | |
-358827378 | 2017-12-27 0:00 | SW | No Violations | |
-36642610 | 2014-7-11 0:00: | SW | No Violations | |
-436692089 | 2018-8-13 0:00: | SW | No Violations | |
-440930857 | 2013-11-25 0:00 | SW | No Violations | |
-50575651 | 2014-2-11 0:00: | SW | No Violations | |
-53342308 | 2015-8-21 0:00: | SW | No Violations | |
-539407053 | 2014-5-22 0:00: | SW | No Violations | |
-549250741 | 2015-4-7 0:00:0 | SW | No Violations | |
-549331222 | 2018-2-20 0:00: | SW | No Violations | |
-553432621 | 2017-5-22 0:00: | SW | No Violations | |
-559246575 | 2015-10-19 0:00 | SW | No Violations | |
-560877534 | 2014-4-29 0:00: | SW | No Violations | |
-563770336 | 2014-5-7 0:00:0 | SW | No Violations | |
-628934263 | 2015-12-11 0:00 | SW | No Violations | |
-661677613 | 2016-12-27 0:00 | SW | No Violations | |
-684799276 | 2014-12-8 0:00: | SW | No Violations | |
-692456961 | 2014-8-26 0:00: | SW | No Violations | |
-733757063 | 2019-3-19 0:00: | SW | No Violations | |
-743535543 | 2016-12-8 0:00: | SW | No Violations | |
-806803884 | 2014-2-19 0:00: | SW | No Violations | |
-814964348 | 2014-8-15 0:00: | SW | No Violations | 1.00 |
-82236385 | 2014-1-17 0:00: | SW | No Violations | |
-836355266 | 2015-11-9 0:00: | SW | No Violations | |
-843552778 | 2018-9-6 0:00:0 | SW | No Violations | |
-887961865 | 2015-8-27 0:00: | SW | No Violations | |
-891490552 | 2018-5-30 0:00: | SW | No Violations | |
-905000129 | 2020-4-14 0:00: | SW | No Violations | |
-911100335 | 2014-4-14 0:00: | SW | No Violations | |
-914461849 | 2019-10-7 0:00: | SW | No Violations | |
-939580406 | 2014-2-24 0:00: | SW | No Violations | |
-967443891 | 2014-2-7 0:00:0 | SW | No Violations | 6.00 |
-974517651 | 2018-3-7 0:00:0 | SW | No Violations | |
0027762493 | 2014-01-31 | Salt Water Injection Well | No Violations | Stopped by service rig for update on possibly bond logging operation of liner string we placed into well last week operator stated that they would possibly be ready to log well tomorrow afternoon. |
0031557423 | 2018-01-17 | Salt Water Injection Well | No Violations | Inspection today revealed that injection pump was in operation during my inspection and it was noted that facility was extremely busy during my inspection. |
0036642610 | 2014-07-11 | Salt Water Injection Well | No Violations | Inspection revealed that injection pump was just started prior too our inspection. |
0050575651 | 2014-02-11 | Salt Water Injection Well | No Violations | Inspection revealed that service rig was drilling on cement retainer and once it is drilled they will start drilling on bridge plug and once that is achieved they will start drilling on cement below the liner string. |
0053342308 | 2015-08-21 | Salt Water Injection Well | No Violations | Bakerwell service rig on site to packer and tubing from well and make clean out run to bottom to flush any buildup within the bottom of the hole. |
0082236385 | 2014-01-17 | Salt Water Injection Well | No Violations | On site with company rep Rex Baker to discuss upcoming casing job and cementing of said casing. |
0126439358 | 2014-11-06 | Salt Water Injection Well | No Violations | Inspection revealed that injection pump too this well was in operation today and as noted on previous report all storage tanks have been repainted. |
0135389985 | 2013-12-12 | Salt Water Injection Well | No Violations | Waiting on service rig to arrive on site to complete remedial work on casing and then they will bond log casing again and if it is confirmed that they have good bond they will run new packer and tubing into well and test. |
0170123069 | 2018-04-19 | Salt Water Injection Well | No Violations | Inspected site today along with two engineers from central office to explain the workings of a Salt Water Injection Well. |
0177146171 | 2015-01-02 | Salt Water Injection Well | No Violations | Inspection revealed that injection pump was in operation during my inspection and it was noted that several vacuum trucks were waiting to unload at the facility on this day. |
0177317997 | 2018-06-21 | Salt Water Injection Well | No Violations | Inspection revealed that injection pumps were not in operation during my inspection.
Note: Four ECM tankers and one Wise tanker and one Dow Cameron truck on site during my inspection. |
0224363530 | 2018-10-16 | Salt Water Injection Well | No Violations | Appalachian Well Surveys on site running caliper tools inside of injection string to determine scale build up they will check all three wells today. |
0225479679 | 2016-02-02 | Salt Water Injection Well | No Violations | Inspection revealed that injection pump was in operation during my inspection. |
0226208644 | 2016-11-18 | Salt Water Injection Well | No Violations | Injection pump to this well not in operation during our inspection.
Note: Emergency Response group on site for tour of rail offload and facility inspection. |
0285455196 | 2013-11-07 | Drill / Deepen / Reopen | No Violations | Inspection revealed that drilling contractor was rigging down and they reached a total depth of 7016 and planned total depth was 7320 they encountered suspected parted casing@5610 they will regroup and plans are to run liner string into well @6200-5200 and cement it in place. |
0292013975 | 2015-03-27 | Salt Water Injection Well | No Violations | Inspection revealed that injection pump was not in operation during my inspection and it was noted that several vacuum trucks were waiting to unload at the time of my inspection. |
0307300214 | 2019-04-14 | Salt Water Injection Well | No Violations | Inspection today revealed that injection pumps were not in operation during my inspection.
|
0314319587 | 2017-02-10 | Salt Water Injection Well | No Violations | Well not in operation during my inspection.
Note: One Energy Transportation vacuum truck on site during inspection. |
0329557931 | 2013-10-31 | Drill / Deepen / Reopen | No Violations | On site to witness running of temperature log and collar locator and bond log of well casing it was determined that cement top on backside of casing was at 1750 and fluid level inside of casing was noted at 250 down from ground level according to temperature log. |
0348688084 | 2015-02-13 | Salt Water Injection Well | No Violations | Inspection revealed that well is shut in at this time. |
0353483128 | 2016-07-14 | Salt Water Injection Well | No Violations | Well not in operation during my inspection.
Four IBEX vacuum trucks on site during my inspection.25-522 |
0354668962 | 2017-11-30 | Salt Water Injection Well | No Violations | Rail car offload today and inspection revealed that injection pump was in operation during my inspection. |
0358827378 | 2017-12-27 | Salt Water Injection Well | No Violations | Inspection today revealed that injection pump was in operation and railcar offload was taking place today. |
0436692089 | 2018-08-13 | Salt Water Injection Well | No Violations | Bakerwell Service rig on site to run stem and jars in well to check total depth of well(checking for possible fill-up) tools sat down at 6915. |
0440930857 | 2013-11-25 | Salt Water Injection Well | No Violations | Baker Wire line Services were on site logging well. |
0539407053 | 2014-05-22 | Salt Water Injection Well | No Violations | Injection pump was in operation during my inspection.
Note: On site with Central Office staff to confirm UIC numbers on brine hauling trucks. |
0549250741 | 2015-04-07 | Salt Water Injection Well | No Violations | Inspection revealed that owner had just started injection pump prior to my arrival at the site and it was noted that nine Elite Oilfield Services vacuum trucks were waiting to unload at the facility on this day of my inspection. |
0549331222 | 2018-02-20 | Salt Water Injection Well | No Violations | Inspection revealed that injection pump was in operation during my inspection.
Note: 28 brine trucks on site waiting to offload during my inspection. |
0553432621 | 2017-05-22 | Salt Water Injection Well | No Violations | Inspection today indicated that injection pump too this well was not in operation during my inspection and it was noted they offloaded at the rail yard today. |
0559246575 | 2015-10-19 | Salt Water Injection Well | No Violations | Well is not in operation today due to work being performed on the number one well. |
0560877534 | 2014-04-29 | Salt Water Injection Well | No Violations | Inspection revealed that well is not being used at this time and it was noted that owner has placed a new set of steps at wellhead so inspector has better access to testing ports on wellhead. |
0563770336 | 2014-05-07 | Salt Water Injection Well | No Violations | On site along with Producers Services to perform 2000 gallon acid treatment on said well.
Note:This well is not used much it is used for back up well. |
0594539023 | 2014-07-28 | Salt Water Injection Well | No Violations | Inspection revealed that injection pump was in operation today and it was noted that owner is preparing to paint all storage tanks and make some small upgrades to the facility. |
0628934263 | 2015-12-11 | Salt Water Injection Well | No Violations | Inspection revealed that injection pump was not in operation during my inspection.
Note: Met company rep for Buckeye Brine at local rail yard to smoke test sewer drains and culverts that were located at site we were trying to determine there discharge points, Buckeye is planning on having brine delivered to site by rail and we wanted to know the discharge points in the event of spill they will have map drawn up of what we observed today and submit it to the division along with plan to address building up containment around current drainage system. |
0631375941 | 2017-10-30 | Salt Water Injection Well | No Violations | Inspection today revealed that injection pump was in operation during my inspection and it was noted that three Wise tankers were offloading at the facility during my inspection. |
0641625668 | 2015-07-13 | Salt Water Injection Well | No Violations | Inspection revealed that well is not in operation at this time. |
0661677613 | 2016-12-27 | Salt Water Injection Well | No Violations | Inspection today revealed that the injection was not in operation during my inspection.
Note: Brine hauler number 25-459 was on pad unloading during my inspection. |
0669844072 | 2017-12-04 | Salt Water Injection Well | No Violations | On site to witness Producers Services perform 2000 gallon acid treatment on said well they started out with 1000 gal of 28%HF and placed 500 gallon spacer and then pumped 500 gal of HCL and another spacer and then another 500 gal HCL and then placed spacer behind acid and then injection pump displaced treatment into formation at a predetermined rate. |
0684799276 | 2014-12-08 | Salt Water Injection Well | No Violations | Inspection revealed that Producers Services was on site to perform acid treatment on said well, they pumped a total of 2000 gallon 500 gal 28% 1000 gal of HF and then 500 gal of 28% and displaced it with 100 bbl. of brine and once brine was in wellbore we shut well down for 1 hour before resuming injection operations. |
0685333295 | 2013-09-26 | Drill / Deepen / Reopen | No Violations | On site for pre spud drill meeting they plan on moving drilling rig in on site the second week of October. |
0692456961 | 2014-08-26 | Salt Water Injection Well | No Violations | Producers Well Service on site to perform 2000 gallon acid treatment job on said well.
Pressure charts forwarded to central office. |
0733757063 | 2019-03-19 | Salt Water Injection Well | No Violations | Inspection revealed that injection pumps were not in operation during my inspection.
|
0743535543 | 2016-12-08 | Salt Water Injection Well | No Violations | Well not in operation during my inspection,
|
0806803884 | 2014-02-19 | Salt Water Injection Well | No Violations | Inspection revealed that service rig was pulling tubing from well it was plugged with sand. |
0814964348 | 2014-08-15 | Salt Water Injection Well | No Violations | I am accompanied by Inspector David Ball and Regional Supervisor Rocky King. The well is not in use. |
0836355266 | 2015-11-09 | Salt Water Injection Well | No Violations | Injection pumps not in operation during my inspection. |
0838518389 | 2016-08-17 | Salt Water Injection Well | No Violations | Injection pump was not in operation today and there was three IBEX vacuum trucks on site unloading during my inspection. |
0843552778 | 2018-09-06 | Salt Water Injection Well | No Violations | Inspection today indicated that injection pump was in operation during my inspection.
Note: 18 Brine trucks were on site during my inspection. |
0880912601 | 2018-11-23 | Salt Water Injection Well | No Violations | Inspection revealed that injection pump was in operation during my inspection. |
0887961865 | 2015-08-27 | Salt Water Injection Well | No Violations | On site to witness setting of packer and pressure test annulus of tubing.
Setting depth is 6125 center of elements and Universal Well Services pumped 228 bbl. Of fresh water and 15 gallon of inhibitor and we pressure tested at 1520 psi for 15 minutes with no decline in pressure. |
0891490552 | 2018-05-30 | Salt Water Injection Well | No Violations | Inspection today indicated that injection pump was not in operation during my inspection. |
0902895382 | 2017-11-27 | Salt Water Injection Well | No Violations | Inspection revealed that injection pump to this well was in operation during my inspection.
Witness railcar offload today. |
0911100335 | 2014-04-14 | Salt Water Injection Well | No Violations | Inspection revealed that injection pump was in operation today and it was noted that several vacuum trucks were unloading at facility during my inspection.
Note: Well not being used today they are currently using the number one well. |
0939580406 | 2014-02-24 | Salt Water Injection Well | No Violations | Great White coil tubing unit rigging on well to wash sand from bottom of hole once sand fill up is removed they will be ready to run tubing and packer into well. |
0967443891 | 2014-02-07 | Salt Water Injection Well | No Violations | On site along with Andrew Adgate to witness bond logging of well be Archer Wire line and log indicated that cement top was noted at 5203 just below casing hanger which was set at 5193. |
0974517651 | 2018-03-07 | Salt Water Injection Well | No Violations | Inspection revealed that injection pump was in operation during my inspection.
|
1006260148 | 2014-03-14 | Salt Water Injection Well | No Violations | On site to pressure test flow line going to wellhead. They filled flow line with fresh water and we pressure tested it at 1525 psi and monitored it for 15 minutes with no decline in pressure.
Note:Flow line is 1100 long and it is 4.5 and 11.6# per foot and is encased within 8.625 which is 24# casing and we also pressure tested annulus of flow line at 1525 psi also. |
1011635313 | 2017-01-04 | Salt Water Injection Well | No Violations | Inspection today revealed that injection pump was not in operation during my inspection. |
1046160860 | 2017-04-10 | Salt Water Injection Well | No Violations | Injection pumps were not in operation during my inspection. |
1057849257 | 2014-03-27 | Salt Water Injection Well | No Violations | Inspection revealed that injection pumps were not in operation during my inspection. |
1072093696 | 2014-09-11 | Salt Water Injection Well | No Violations | Inspection revealed that injection pump to this well was not in operation during my inspection. |
1100675638 | 2018-05-01 | Salt Water Injection Well | No Violations | Inspection today indicated that injection pump was in operation.
Note: On site to audit truck traffic at the facility. |
1122362658 | 2017-11-20 | Salt Water Injection Well | No Violations | Inspection today revealed that injection pump to this well was in operation during my inspection.
Note: Eleven brine hauling trucks were in line to offload during my inspection. |
1122604924 | 2014-03-06 | Salt Water Injection Well | No Violations | |
1145634747 | 2015-03-05 | Salt Water Injection Well | No Violations | Inspection revealed that injection pump was not in operation during my inspection and it was noted that nine Oilfield Solutions vacuum trucks were waiting to unload at the facility during my inspection. |
1160407714 | 2014-02-27 | Salt Water Injection Well | No Violations | On site to witness tubing and packer run into well and flush annulus with fresh water and inhibitor and pressure test annulus. |
1176605142 | 2019-11-4 0:00: | SW | No Violations | |
1195004129 | 2017-12-20 | Salt Water Injection Well | No Violations | Producers Services was on site to perform 16,309 gallon injection test on said well they pumped at 1000 psi at a rate of 4.67 bpm and then we bumped up pressure to 1100 psi at a rate of 7.36 bpm and then bumped up pressure again to 1250 psi at a rate of 7.60 bpm and repeated the 1050 psi at a rate of 6.79 bpm then washed up and job was complete.
ISIP WAS NOTED AT 552 PSI. |
1200790268 | 2014-08-11 | Salt Water Injection Well | No Violations | Inspection revealed that injection pump too this well was not in service during my inspection. |
1203275818 | 2014-10-17 | Salt Water Injection Well | No Violations | Inspection revealed that injection pump too this well was in operation during my inspection and it was noted that all of the storage tanks at the facility are in the process of being repainted. |
1227640926 | 2018-04-03 | Salt Water Injection Well | No Violations | Inspection today indicated that injection pump was in operation during my inspection.
Note: Two Wise trucking tankers were offloading at the site during my inspection. |
1237097182 | 2017-10-16 | Salt Water Injection Well | No Violations | Injection pump not in operation during my inspection. |
1240427421 | 2015-12-28 | Salt Water Injection Well | No Violations | Injection pump too this well was in operation during my inspection. |
1240600126 | 2015-09-22 | Salt Water Injection Well | No Violations | Inspection revealed that injection pump was in operation during my inspection and it was noted that three Infinity vacuum trucks were unloading at the facility on this day of my inspections. |
1290366762 | 2018-12-14 | Salt Water Injection Well | No Violations | Inspection today revealed that injection pump was not in operation during my inspection.
|
1294447033 | 2019-01-29 | Salt Water Injection Well | No Violations | Inspection today revealed that injection pump to this well was not in operation during my inspection and it was noted that one Wise Trucking vacuum truck was on site during my inspection. |
1297202599 | 2016-04-18 | Salt Water Injection Well | No Violations | Inspection revealed that injection pump was in operation during my inspection and it was noted that three IBEX vacuum trucks were unloading at the facility on this day of my inspection. |
1306063930 | 2016-01-12 | Salt Water Injection Well | No Violations | Inspection revealed that injection pumps were not in operation during my inspection. |
1351050865 | 2015-03-12 | Salt Water Injection Well | No Violations | Inspection on this day revealed that injection pump was in operation and it was noted that several vacuum trucks/tankers were waiting to unload at the facility. |
135389985 | 2013-12-12 0:00 | SW | No Violations | |
1366400626 | 2017-06-19 | Salt Water Injection Well | No Violations | Inspection today revealed that injection pump to this well was in operation during my inspection. |
1368778999 | 2019-12-12 0:00 | SW | No Violations | |
1381956781 | 2013-10-16 | Salt Water Injection Well | No Violations | On site to witness testing of BOP rig personnel closed BOP and we pressured up to 500# and monitored pressure for 15 minutes with no decline in pressure. |
1382042070 | 2013-10-17 | Salt Water Injection Well | No Violations | Drilling on fluid@1958 converted to fluid type drilling@1768due to fact that they were not able to keep up with cleaning cuttings that were coming from well. |
1383063780 | 2013-10-25 | Drill / Deepen / Reopen | No Violations | Inspection revealed that drilling rig was drilling@4100 and while on site I inspected 8.625 casing that is to be run in well at a later date. |
1383150287 | 2013-10-30 | Casing String Witnessed | No Violations | On site to witness running and cementing of 5905of 8.625casing Universal Cemented with 1163 sacks,plug did not land and decision was made to run bond log in well and confirm cement top and check for pipe separation. |
1383150553 | 2013-10-30 | Casing String Witnessed | No Violations | On the day of my inspection I witnessed the first stage of a two stage cement job. Wildcat Drilling had drilled an 11.625 hole on fluid to 5933. They ran 8.625 casing equipped with a DV tool. Universal broke circulation and pumped 600 sacks of cement. Good circulation was maintained throughout the job. |
1383324727 | 2013-11-01 | Drill / Deepen / Reopen | No Violations | On site to attempt to pressure casing, arrived on site and rig crew loaded casing with 15 bbl fresh water and then DB Energy Management used there solvent truck to apply pressure and he pumped additional 7 bbl of water with a pressure reading of 180 psi maximum so at that point decision was made to trip in hole and drill out stage tool and run bit to bottom and then set bridge plug in bottom of casing and load hole again and then pressure test casing. |
1383525462 | 2013-11-01 | Drill / Deepen / Reopen | No Violations | On site to witness Appalachian Well Surveys run 8 retrievable bridge plug inside of casing and set it at 5875 and then rig crew loaded casing and we pressured tested casing@1500# and pressure dropped to 1485# during the 15 minute test which was a 1% decline.
Note: Appalachian had to make two runs with collar locator log due to faulty equipment. |
1385066962 | 2013-11-21 | Drill / Deepen / Reopen | No Violations | Inspection revealed that stone haulers are placing stone across entire location preparing site for down hole E-Logging of well on 11/24/13. |
1387406683 | 2013-12-18 | Salt Water Injection Well | No Violations | On site to witness tracer testing of potential injection zones in well bore, Coastal Wireline Company and Producers Services performed testing and it was determined that injection zone was identified@6550-6640 according to tracer logs.
Producers pumped 7.5 bpm@800 psi and once pump truck shut down it took six minutes for pressure to drop to 0 pressure. |
1390338649 | 2014-01-21 | Salt Water Injection Well | No Violations | On site to witness Bakerwell Service company try and release casing hanger from tubing they were unable to do so this morning due to well flowing after circulating bottoms up with 8.7#brine so they had to call for heavy brine to load hole with and once circulated again flow stopped and we released casing hanger and they started out of hole with working string and the will start cementing packer into well in the morning. |
1390516128 | 2014-01-22 | Casing String Witnessed | No Violations | On site to witness cementing of liner string in SWIW well they ran 1010 of 5.5 and cemented it in place with 200 sacks of Type 1 cement and once cemented they released cementing packer and reversed circulation with 200 bbl of brine water and they will remove remaining tubing tomorrow. |
1391809746 | 2014-02-05 | Salt Water Injection Well | No Violations | On site to cement liner string in place again, Universal Well Services mixed 150 sacks of Type 1 cement and they pumped it through tubing and they will bond log well again on 2/7/14 to confirm cement top. |
1397748319 | 2014-04-17 | Salt Water Injection Well | No Violations | This report correlates with complaint #4667. I received a call from Ginger Maple with concerns that the new injection well in Coshocton was causing fluid to bubble out of her yard. The injection well in question is approximately 8.8 miles from Mrs. Maples home. I met her at her home to conduct my inspection. I found that there was a steady flow of water from the yard. I also observed periodic bubbling from the ground where the water was pooled. They had dug a small hole at the source of the water and a small ditch to divert the water away from the yard. I conducted a field test of the water with a Quantab and I sampled the air from the bubbles with a hand held gas detector. The results were negative for chlorides and negative for CH4 or H2S. I also tasted the water and found it to be fresh. I concluded that the flow of water from the yard was not related to this injection well. |
1434237038 | 2015-06-09 | Salt Water Injection Well | No Violations | Inspection revealed that injection pump to this well was in operation on the day of my inspection. |
1435043998 | 2015-11-23 | Salt Water Injection Well | No Violations | Well not in operation during my inspection. |
1440967137 | 2015-08-26 | Salt Water Injection Well | No Violations | On site to witness packer and tubing run into well rig crew ran ASI-X Nickel coated packer and 1102 of 3.5 tubing and 4984 of 4.5 tubing and we plan on setting packer in the morning and fill annulus with fresh water and inhibitor and pressure test. |
1461665764 | 2018-07-10 | Salt Water Injection Well | No Violations | Inspection revealed that injection pump was in operation today. |
1471609721 | 2020-7-10 0:00: | SW | No Violations | |
1484775368 | 2017-01-18 | Salt Water Injection Well | No Violations | Inspection today revealed that injection pump was not in operation during my inspection. |
1495330398 | 2016-09-01 | Salt Water Injection Well | No Violations | Inspection revealed that injection pump was not in operation during my inspection. |
1504996033 | 2016-11-03 | Salt Water Injection Well | No Violations | Injection pump not in operation during my inspection of facility. |
1514791716 | 2015-08-03 | Salt Water Injection Well | No Violations | Wire line on site to run tools in well to determine if well owner has obstruction within well bore, the tools sat down at 6247 and it was determined that there is a obstruction in hole and they will make plans on releasing packer and cleaning out well bore.
Told operator to submit plan to the division so the UIC dept. could approve said plan. |
1540052005 | 2020-6-5 0:00:0 | SW | No Violations | |
1544526229 | 2019-11-6 0:00: | SW | No Violations | |
1551151771 | 2016-06-01 | Salt Water Injection Well | No Violations | Injection pump to this well was not in operation today and it was noted that four IBEX vacuum trucks were unloading at the facility during my inspection. |
1551985630 | 2017-09-05 | Salt Water Injection Well | No Violations | Inspection today indicated that injection pump was not in operation during my inspection.
|
1577483264 | 2019-12-23 0:00 | SW | No Violations | |
1578341308 | 2020-1-6 0:00:0 | SW | No Violations | |
1580934757 | 2020-2-4 0:00:0 | SW | No Violations | |
1585562969 | 2017-08-28 | Salt Water Injection Well | No Violations | Injection pump was in operation during our inspection. |
1598114363 | 2020-8-17 0:00: | SW | No Violations | |
1620525600 | 2019-7-18 0:00: | SW | No Violations | |
1628363131 | 2017-07-06 | Salt Water Injection Well | No Violations | Inspection revealed that injection pump was in operation during my inspection and it was noted that three Wise Trucking tankers were unloading at the facility today. |
1652717491 | 2013-11-04 | Salt Water Injection Well | No Violations | Inspection revealed that Wildcat Drilling presently drilling on fluid@6450 should be at total depth later this week. |
1672668482 | 2015-07-09 | Preliminary Restoration | No Violations | Restoration work at site satisfactory, pits have been filled in and site restored and vegetation has been established. |
1681528870 | 2019-03-05 | Salt Water Injection Well | No Violations | Inspection today indicated that injection pump was not in operation during my inspection.
Note: 2 Wise trucks 1-BWS TRUCK 1 -ECM TRUCK on site during my inspection |
1699471152 | 2015-02-25 | Salt Water Injection Well | No Violations | Inspection revealed that well is not in operation at this time,operator stated they plan on starting pump for this well later this afternoon. |
170123069 | 2018-4-19 0:00: | SW | No Violations | |
1710506952 | 2018-03-23 | Salt Water Injection Well | No Violations | Inspection today revealed that injection pumps were in operation during my inspection.
Note: 2-Wise tankers and 4-ECM tankers were at the facility at the time of my inspection. |
1735757767 | 2017-03-24 | Salt Water Injection Well | No Violations | Injection pump to this well was in operation today.
Six Wise trucking tankers were on site unloading during my inspection. |
1740583739 | 2014-06-02 | Preliminary Restoration | No Violations | Inspection revealed that restoration work at site has been completed and vegetation has been established. |
1746479876 | 2015-12-18 | Salt Water Injection Well | No Violations | Well not in operation today due too lack of water being hauled into the facility. |
177146171 | 2015-1-2 0:00:0 | SW | No Violations | |
1780194173 | 2015-01-15 | Salt Water Injection Well | No Violations | Inspection revealed that injection pump was in operation during my inspection and it was noted that several Elite Oilfield Services vacuum trucks were waiting to unload at the facility during my inspection. |
1790955866 | 2017-07-18 | Salt Water Injection Well | No Violations | Inspection revealed that injection pump to this well was in operation during my inspection.
|
1832466926 | 2017-04-19 | Salt Water Injection Well | No Violations | Injection pump was in operation today.
Note: Six Wise Trucking tankers were on site unloading during our inspection. |
1868362510 | 2014-01-24 | Salt Water Injection Well | No Violations | Bakerwell Service company along with Blue-Dot Services on site going in hole with4.750 bit to drill out cement within 5.5 casing once cement &cement shoe is drilled they will come out of hole to bond log casing and if log looks good they will go back in hole and clean it out to bottom and once that is achieved we will run new packer and injection string into well. |
1871522882 | 2013-10-21 | Drill / Deepen / Reopen | No Violations | Wild Cat drilling was at 3255 drilling on fluid during my inspection. |
1926505439 | 2020-3-17 0:00: | SW | No Violations | |
1951334660 | 2014-01-14 | Salt Water Injection Well | No Violations | Bakerwells service rig moving in on site to run 5.5 liner string into well and cement it in place.
Note: Informed owner that once casing has been cemented in place and cement drilled out that they would need to run another bond log to verify that they have good integrity with casing. |
2012450470 | 2014-06-25 | Salt Water Injection Well | No Violations | Injection pump not in operation today. |
2032990822 | 2013-09-23 | Drill / Deepen / Reopen | No Violations | Inspection revealed that lease road to new well site has been made and they are currently working on clearing area to build drill site for SWIW well. |
2045727413 | 2014-06-11 | Salt Water Injection Well | No Violations | Inspection revealed that injection pump was in operation today and it was noted that several Oilfield Services vacuum trucks were waiting to unload at facility while I was performing my inspection. |
2049702011 | 2016-09-15 | Salt Water Injection Well | No Violations | Injection pump to this well not in operation today. |
2055506203 | 2014-06-18 | Salt Water Injection Well | No Violations | Inspection revealed that injection pump too this well was not in operation today due to low volume of trucks today. |
2115705947 | 2015-06-22 | Salt Water Injection Well | No Violations | Inspection revealed that injection pump was in operation today and it was noted that six Infinity vacuum trucks were at the facility during my inspection. |
2117103875 | 2019-04-22 | Salt Water Injection Well | No Violations | Inspection today indicated that injection pump was in operation during my inspection.
Note: Owner is currently having tanks cleaned out. |
2121842668 | 2017-01-30 | Salt Water Injection Well | No Violations | Inspection today revealed that injection pumps were not in operation during my inspection.
Note: Four Wise trucking tankers were unloading at the facility during my inspection and the drivers stated that they were hauling Accent Resources water from various well pads within the state. |
27762493 | 2014-1-31 0:00: | SW | No Violations | |
285351284 | 2019-9-25 0:00: | SW | No Violations | |
292013975 | 2015-3-27 0:00: | SW | No Violations | |
314319587 | 2017-2-10 0:00: | SW | No Violations | |
329557931 | 2013-10-31 0:00 | DD | No Violations | 8.00 |
40930832 | 2020-5-6 0:00:0 | SW | No Violations | |
594539023 | 2014-7-28 0:00: | SW | No Violations | |
631375941 | 2017-10-30 0:00 | SW | No Violations | |
641625668 | 2015-7-13 0:00: | SW | No Violations | |
669844072 | 2017-12-4 0:00: | SW | No Violations | |
685333295 | 2013-9-26 0:00: | DD | No Violations | |
838518389 | 2016-8-17 0:00: | SW | No Violations | |
880912601 | 2018-11-23 0:00 | SW | No Violations | |
901403009 | 2020-1-9 0:00:0 | SW | No Violations | |
902895382 | 2017-11-27 0:00 | SW | No Violations |
For data sources see[3]