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34-035-21736

Well Details

Well ID: 34-035-21736
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Country: United States
State: Ohio
County: <County>
Municipality:
Operator Name: DUCK CREEK ENERGY INC
Well Pad ID:
Farm/Lease Name: CITY OF EUCLID
License Status: Final Restoration
License Date: 2008-06-04
Spud Date: 2002-03-20
Spud Drilling Contractor: G & H DRLG
Final Drill Date: 2002-03-28
Well Total Depth: 3120.00 ft
Configuration: Vertical
Latitude: 41.600000
Longitude: -81.520000

For data sources see[1]

Well History

Well Status Well Status Date Comment
APP 2002-02-19 Proposed Formations:ORISKANY/NEWBURG/CLINTON, Issued Date:2/19/2002, Expired Date:2/19/2003 6:00:00 AM, Drilling unit acres:20, Proposed Well Type:OG, Proposed Well Class:EW
Original Spud 2002-03-20
Completed 2002-03-28
Reached Total Depth 2002-03-28
Completion Report Received 2002-07-08
APP 2003-11-21 Proposed Formations:CLINTON, Issued Date:11/21/2003, Expired Date:11/20/2004 6:00:00 AM, Drilling unit acres:20, Proposed Well Type:OG, Proposed Well Class:
Change of Owner 2004-07-30 Operator changed from 1639, BASS ENERGY CO INC to 1902, DUCK CREEK ENERGY INC
APP 2008-06-04 Proposed Formations:CLINTON, Issued Date:6/4/2008, Expired Date:6/4/2009 6:00:00 AM, Drilling unit acres:20, Proposed Well Type:OG, Proposed Well Class:
Plugged/Abandoned 2008-07-24
Construction Permit Expires 2009-06-04
Record Last Modified 2017-02-15

For data sources see[2]

Perforation Treatments

Perforation Date Interval Top (ft) Interval Base (ft) Number of Shots
2002-08-14 2946 2966 38
2946 2966 38
2946 2966 38

For data sources see[3]

Stimulations Data

Stimulation Date Chemical Agent Chemical Agent Concentration (%) Fracking Fluid Volume Mass of Proppant Used (lb) Fracking Company Comments
H2O 15 54500 Gal 40000 500 GALLONS HCL ACID

For data sources see[4]

Production Data

Period Operator Name Gas Quantity (mcf) Oil Quantity (bbl) Production Days
2002 BASS ENERGY CO INC 6486.00 0.00 365
2003 BASS ENERGY CO INC 400.00 0.00 365
2004 BASS ENERGY CO INC 391.00 0.00 365
2005 DUCK CREEK ENERGY INC 2182.00 0.00 365
2006 DUCK CREEK ENERGY INC 534.00 0.00 365
2007 DUCK CREEK ENERGY INC 881.00 0.00 365
2008 DUCK CREEK ENERGY INC 243.00 0.00 204

For data sources see[5] [6]

Waste Data

Period Operator Name Waste Type Quantity (bbl) Production Days
2002 BASS ENERGY CO INC Brine 1026 365
2003 BASS ENERGY CO INC Brine 0 365
2004 BASS ENERGY CO INC Brine 0 365
2005 DUCK CREEK ENERGY INC Brine 82 365
2006 DUCK CREEK ENERGY INC Brine 0 365
2007 DUCK CREEK ENERGY INC Brine 80 365
2008 DUCK CREEK ENERGY INC Brine 100 204

For data sources see[7] [8]

Inspection Data

Inspections Performed

Inspection ID Inspection Date Inspection Type Inspection Result Inspection Comments
-32071850 2016-9-19 0:00: UP No Violations 1.00
0032071850 2016-09-19 UrbanProduction Wells No Violations I inspected this former well location pursuant to a complaint (#5442) of gas odor reported by a citizen. The gas odor had been reported near a soccer field, behind the police station. Upon my inspection, I observed the following: a circular area of dead grass, approximately 5 feet in diameter, at the western edge of a soccer field. I advanced several punch bar holes within the noted area of dead grass and noted LEL concentrations that exceeded 50%. Based on a review of historic documentation, the dead area corresponds very closely with the documented location of this well. I did not note any detected gas readings in the ambient area around the area, nor did I observe any other areas of dead or stressed vegetation or signs of impact. I reviewed the plugging and abandonment report for the well which indicated the following: the well had been plugged on 07/24/08 with no report of problems or incident. A final restoration inspection was performed on 08/01/2010 and final restoration was passed with no observed problems or conditions requiring attention. Pursuant to the complaint and inspection, I contacted City of Euclid Service Director Dan Knecht. I reported the results of my inspection to Director Knecht and advised that additional assessment would require excavation and exposure of the area by the city. Further, I advised that the city could elect to seek assistance from the Idle and Orphan well program, mitigate the stray gas with passive venting, or leave the condition as is. I advised that ODNR would continue to provided consultation and assistance as needed.
0979215346 2008-07-23 Plug / Plug Back No Violations company plugging well set lime plug ripped and pulling 4.5
2079274603 2010-08-17 Final Restoration No Violations
979215346 2008-7-23 0:00: PB No Violations

For data sources see[9]

References