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Well ID: 34-035-22197 | Loading map...
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Country: United States | |
State: Ohio | |
County: <County> | |
Municipality: | |
Operator Name: GREEN ENERGY INC | |
Well Pad ID: | |
Farm/Lease Name: SCOTT | |
License Status: Final Restoration | |
License Date: 2011-11-21 | |
Spud Date: 2012-06-04 | |
Spud Drilling Contractor: POULSON DRILLING | |
Final Drill Date: 2012-06-09 | |
Well Total Depth: 3028.00 ft | |
Configuration: Vertical | |
Latitude: 41.420000 | |
Longitude: -81.760000 |
For data sources see[1]
Well Status | Well Status Date | Comment |
---|---|---|
APP | 2011-11-21 | Proposed Formations:OHIO SHALE, ORISKANY, NEWBURG, CLINTON, Issued Date:11/21/2011, Expired Date:11/20/2013 12:00:00 PM, Drilling unit acres:20, Proposed Well Type:OG, Proposed Well Class:POOL |
Reached Total Depth | 2012-06-09 | |
Plugged/Abandoned | 2012-07-27 | |
Completion Report Received | 2012-11-08 | |
Construction Permit Expires | 2012-11-20 | |
Record Last Modified | 2017-10-24 |
For data sources see[2]
Perforation Date | Interval Top (ft) | Interval Base (ft) | Number of Shots |
---|---|---|---|
2012-12-10 | 2809 | 2868 | 36 |
2809 | 2868 | 36 | |
2809 | 2868 | 36 |
For data sources see[3]
Stimulation Date | Chemical Agent | Chemical Agent Concentration (%) | Fracking Fluid Volume | Mass of Proppant Used (lb) | Fracking Company | Comments |
---|---|---|---|---|---|---|
H2O | 15 | 3214 Bbl | 50000 | Universal Well Services Inc. |
For data sources see[4]
Period | Operator Name | Gas Quantity (mcf) | Oil Quantity (bbl) | Production Days |
---|---|---|---|---|
2012 | GREEN ENERGY INC | 0.00 | 0.00 | 0 |
Period | Operator Name | Waste Type | Quantity (bbl) | Production Days |
---|---|---|---|---|
2012 | GREEN ENERGY INC | Brine | 2470 | 0 |
Inspection ID | Inspection Date | Inspection Type | Inspection Result | Inspection Comments |
---|---|---|---|---|
-2107795869 | 2012-6-5 0:00:0 | UD | No Violations | 6.00 |
-836472224 | 2014-5-15 0:00: | FR | No Violations | |
-975831254 | 2012-6-4 0:00:0 | UD | No Violations | 6.00 |
0836472224 | 2014-05-15 | Final Restoration | No Violations | I isnpected the location if this former procuding unit for completion of final restoration. Cuurently there is a 4-inch diameter vent stack which extends above grade to an approximate height of 12 feet above grade. The area around the former well has been graded and vegetation has been established. Pits have been filled and all other appurtenances from production have been removed. No further activity is warranted. Final resotration is complete. |
0975831254 | 2012-06-04 | Urban Drill / Deepen / Reopen | No Violations | My inspection today found rig being set up. Pits were being dug prior to spudding on this date and conductor casing was set in the late afternoon. Cementing report will be filed following completion of well drilling and cementing. |
1339078253 | 2012-06-09 | Urban Drill / Deepen / Reopen | No Violations | My visit to the well site today was to cement the production casing. Cement report will be filed following the completion of the drilling process. |
1350407983 | 2012-10-16 | UrbanProduction Wells | No Violations | My visit to the well today was to check progress on the restoration Process. This well was drilled from 6/4/12 through 6/9/12, due to lack of sufficient pressure the well was plugged 0n 7/25/12 and 7/27/12. A vault and vent system was installed on 10/11/12 due to minimum leakage of shale gas around the 8.625 casing. The current vent pipe will be replaced with a longer pipe in the short term, which will complete this well. Ground restoration has begun and grass is growing on the site. |
2107795869 | 2012-06-05 | Urban Drill / Deepen / Reopen | No Violations | Well inspection on this date was to cement surface casing and to conduct Blow Off Preventer (BOP) testing. Cement report will be placed on file following completion of well drilling and cementing process. |
For data sources see[9]