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| Well ID: 34-037-20078 | Loading map...
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| Country: United States | |
| State: Ohio | |
| County: Darke | |
| Municipality: Brown Township | |
| Operator Name: KNOWLTON REALTY INC | |
| Well Pad ID: | |
| Farm/Lease Name: KNOWLTON # 1 | |
| License Status: Producing | |
| License Date: 2001-02-09 | |
| Spud Date: 2001-03-07 | |
| Spud Drilling Contractor: BOB HUWER DRLG | |
| Final Drill Date: | |
| Well Total Depth: | |
| Configuration: Vertical | |
| Latitude: 40.210000 | |
| Longitude: -84.620000 |
For data sources see[1]
| Well Status | Well Status Date | Comment |
|---|---|---|
| APP | 2001-02-09 | 6920 KNOWLTON REALTY INC Proposed Formation QUEENSTON Issued Date 2/9/01 Expired Date 2/9/02 6:00:00 AM |
| Original Spud | 2001-03-07 | RBDMS Rec |
| Construction Permit Expires | 2002-02-09 | RBDMS Rec |
| Record Last Modified | 2015-09-24 | RBDMS Rec |
For data sources see[2]
| Inspection ID | Inspection Date | Inspection Type | Inspection Result | Inspection Comments |
|---|---|---|---|---|
| -1334617572 | 2004-7-14 0:00: | PW | No Violations | |
| -1375287411 | 2004-5-19 0:00: | PW | No Violations | |
| 1036114788 | 2016-05-10 | Production Wells | No Violations | Compliance notice follow-up. The well consists of what appears to be 7 surface casing with a 7 to 2 swage. There is a gauge on a 1/4 nipple. The vales are off. No odor of gas was observed. New coordinates were taken during my inspection. |
| 1055333361 | 2003-06-09 | Preliminary Restoration | Violations Noted | Check well for Sherry Young for NOMSV since no well completion report received.
Site review indicated the well had been completed. Pressure valve at top indicated 0 PSI. Two valves at top of the well were closed off. No lines seen running from the well. No tank battery present. The well is not in production. Preliminary restoration has been done. Pit has been closed. File checked and no production reports submitted. -Well must be put into production or plugged within 30 days. |
| 1061387428 | 2003-08-15 | Production Wells | No Violations | Status check on well. No change from last inspection on 6/9/03. Well still incapable of production. |
| 1080585489 | 2004-03-18 | Production Wells | No Violations | -NOV follow up inspection. NOV 1055333361 issued 6/11/03. NOV was issued for failure to submit a well completion report although the well was completed. No production has been reported since the well was drilled. Several sections of pipe have been connection to the well but the pipes do not run anywhere. Well was incapable of production.
-On site with Jeff Fry. Valve to the well shut off. When opened, well producing 5 lbs of pressure. -Digital photos taken of the well. -Well still incapable of production. No change in the status since the NOV was issued in 2003. -Well was on Sherry Youngs list of wells from 2003. |
| 1255017162 | 2009-10-07 | Production Wells | No Violations | -Status check on well. Since last inspection on 7/14/04, a portion of the 1 line was removed and capped. Chiefs Order 2004-26 was issued 4/21/04 for failure to comply with N.O.V. 10553361 issued 6/3/03 for failure to produce or plug the well, failure to submit the well completion record, and failure to submit the geophysical well log. The values are closed on the well including a pressure value on top. The well is not attached to a service line either to vacated whareshouse or elsewhere. The whareshoue/Industrial bldg is still for sale by Everest Real Estate. Photos taken. Will check with Jeff Fry re: further action. None of the orders in the Chiefs Order have been complied with. |
| 1334617572 | 2004-07-14 | Production Wells | No Violations | -Status check on well. No change from last inspection on 5/19/04. Chiefs Order 2004-26 issued 4/21/04 for failure to comply with N.O.V. 10553361 issued 6/3/03 for failure to plug the well, failure to submit the well completion record, and failure to submit the geophysical well log. Since last inspection, Tom Tugend sent an e-mail that the Chiefs Order was returned to the Columbus office undelivered. Will attempt to hand carry a copy to the well owners address on the order in Dayton Ohio. |
| 1375287411 | 2004-05-19 | Production Wells | No Violations | -On site for Chiefs Order # 2004-26 compliance inspection. Joint inspection with Jeff Fry. Chiefs Order issued on 4/21/04 for failure to comply with N.O.V. 10553361 issued 6/11/03 for failure to plug the well, failure to submit the well completion record, and failure to submit the Geophysical Well Log. Since last inspection, no change to the well has been noted. Values shut off. Valves either rusted shut or pressure is on the line, and line is not connected. Several sections of pipe attached to the well are still present but do not run anywhere. Digital photos taken. Further administrative action to be taken. |
| Inspection ID | Violation ID | Violation Date | Violation Code | Violation Comments |
|---|---|---|---|---|
| 1055333361 | US-OH-101011 | 2003-06-11 | Well shall be plugged |
For data sources see[3]