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Well ID: 34-045-21495 | Loading map...
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Country: United States | |
State: Ohio | |
County: Fairfield | |
Municipality: Bloom Township | |
Operator Name: NORTHWOOD ENERGY CORP | |
Well Pad ID: | |
Farm/Lease Name: STEBOLTON | |
License Status: Well Drilled | |
License Date: 2018-08-31 | |
Spud Date: 2013-07-15 | |
Spud Drilling Contractor: FMS DRILLING | |
Final Drill Date: 2013-07-28 | |
Well Total Depth: 3794.00 ft | |
Configuration: Vertical | |
Latitude: 39.780000 | |
Longitude: -82.740000 |
For data sources see[1]
Well Status | Well Status Date | Comment |
---|---|---|
APP | 2013-07-11 | Proposed Formations:OHIO SHALE THRU TREMPEALEAU, Issued Date:7/11/2013, Expired Date:7/11/2015 12:00:00 PM, Drilling unit acres:20, Proposed Well Type:OG, Proposed Well Class:EDPW |
Plugged Back | 2013-07-28 | |
Reached Total Depth | 2013-07-28 | |
Completion Report Received | 2018-08-22 | |
APP | 2018-08-31 | Proposed Formations:TREMPEALEAU, Issued Date:8/31/2018, Expired Date:8/30/2020 12:00:00 PM, Drilling unit acres:20, Proposed Well Type:OG, Proposed Well Class: |
Record Last Modified | 2018-09-07 | |
Construction Permit Expires | 2020-08-30 |
For data sources see[2]
Perforation Date | Interval Top (ft) | Interval Base (ft) | Number of Shots |
---|---|---|---|
2018-08-31 | 2913 | 2976 | 0 |
2913 | 2976 | 0 | |
2913 | 2976 | 0 |
For data sources see[3]
Stimulation Date | Chemical Agent | Chemical Agent Concentration (%) | Fracking Fluid Volume | Mass of Proppant Used (lb) | Fracking Company | Comments |
---|---|---|---|---|---|---|
2013-10-30 | H2O | 7 | 199625 Gal | 60000 | Producers Service Corporation |
For data sources see[4]
Period | Operator Name | Gas Quantity (mcf) | Oil Quantity (bbl) | Production Days |
---|---|---|---|---|
2014 | NORTHWOOD ENERGY CORP | 0.00 | 0.00 | 0 |
2015 | NORTHWOOD ENERGY CORP | 0.00 | 0.00 | 0 |
2016 | NORTHWOOD ENERGY CORP | 0.00 | 0.00 | 0 |
2017 | NORTHWOOD ENERGY CORP | 0.00 | 0.00 | 0 |
2018 | NORTHWOOD ENERGY CORP | 0.00 | 0.00 | 0 |
Period | Operator Name | Waste Type | Quantity (bbl) | Production Days |
---|---|---|---|---|
2014 | NORTHWOOD ENERGY CORP | Brine | 677 | 0 |
2015 | NORTHWOOD ENERGY CORP | Brine | 0 | 0 |
2016 | NORTHWOOD ENERGY CORP | Brine | 0 | 0 |
2017 | NORTHWOOD ENERGY CORP | Brine | 0 | 0 |
2018 | NORTHWOOD ENERGY CORP | Brine | 0 | 0 |
Inspection ID | Inspection Date | Inspection Type | Inspection Result | Inspection Comments |
---|---|---|---|---|
-1040403886 | 2018-6-1 0:00:0 | PW | No Violations | 0.20 |
-1171136631 | 2018-9-21 0:00: | PW | No Violations | 0.50 |
-122739477 | 2013-7-15 0:00: | DD | No Violations | 5.00 |
-1358745759 | 2017-10-5 0:00: | PW | No Violations | 1.00 |
-1427960172 | 2013-10-30 0:00 | DD | No Violations | 6.00 |
-147117672 | 2013-7-20 0:00: | DD | No Violations | 7.00 |
-248216631 | 2018-8-10 0:00: | PW | No Violations | 0.60 |
-587859933 | 2018-2-26 0:00: | PW | No Violations | 1.50 |
-597025883 | 2015-11-18 0:00 | PW | No Violations | 2.00 |
-690255482 | 2013-7-22 0:00: | DD | No Violations | 4.00 |
-76754836 | 2017-6-14 0:00: | PW | No Violations | 1.00 |
-994906612 | 2014-2-21 0:00: | DD | No Violations | 1.00 |
0033363631 | 2013-07-17 | Drill / Deepen / Reopen | No Violations | 122 of conductor was set, good cement returns. |
0076754836 | 2017-06-14 | Production Wells | No Violations | Compliance notice follow-up inspection. The well remains idle. The well consists of a wellhead, pumping unit and has the production tubing connected to a half tank. There is rust on the pulleys and the polish rod is dull. |
0122739477 | 2013-07-15 | Drill / Deepen / Reopen | No Violations | FMS drilling has installed the rat hole pipe. I instructed them to seal the annulus to prevent exposing the soil to any drilling fluids. They said they will cement the annulus on the rat and mouse hole pipes. |
0147117672 | 2013-07-20 | Drill / Deepen / Reopen | No Violations | I received a call from Bob Brock, tool pusher for FMS drilling. He stated they would be ready to cement surface casing at 1900 hours. Formation Cementing on site 2130 hours. Good cement returns. 405 of 8.62 surface casing installed. |
0180674489 | 2013-07-21 | Drill / Deepen / Reopen | No Violations | I received a call from FMS drilling to perform a BOP test. The test was 500 PSI for 30 minutes. No loss the test passed. |
0248216631 | 2018-08-10 | Production Wells | No Violations | At 8:39 AM I called Mr. Bill Arnholt who works for Northwood Energy. I left a message for Mr. Arnholt to return my call regarding the status of this well. The well consists of a pumping unit with the valves turned off and a temporary horizontal tank used to test the well. |
0587859933 | 2018-02-26 | Production Wells | No Violations | At 0819 today I called Mr. Bill Arnholt with NorthWood Energy and left a message to return my call. I issued a compliance notice on 10.28.16 for 1509:12(B), well shall be plugged. The well consists of a pumping unit and a temporary horizonal tank they used to test the well. No attempt has been made to bring the well into compliance. |
0597025883 | 2015-11-18 | Production Wells | No Violations | Production well inspection. The well has produced only brine. I have contacted Northwood Energy concerning the status of this well. |
0690255482 | 2013-07-22 | Drill / Deepen / Reopen | No Violations | They have reached 821, no problems, drilling is on schedule. |
0994906612 | 2014-02-21 | Drill / Deepen / Reopen | No Violations | The pits have been filled, the well has not been put into production. I have contacted Northwood Energy to determine when the well will be finished. |
1040403886 | 2018-06-01 | Production Wells | No Violations | At 0753 today I called Mr. Bill Arnholt with Northwood Energy and left a message to return my call. I issued a compliance notice on 10.28.16 for 1509:12(B), well shall be plugged. The well consists of a pumping unit and a temporary horizonal tank they used to test the well. The polish rod is dull and the pulleys are rusty. There has been no change in the status of the well since my last inspection. New picturs were taken during my inspection. |
1106770958 | 2017-11-21 | Production Wells | No Violations | My inspection revealed the well status has not changed. The pulleys on the motor are rusty and the polish rod is dull. There is no fuel line connected to the carburetor. The vales are turned off. There has been no change in the status of this since my last inspection. I have called well owner Northwood Energy find out when the plan on bring the well into compliance. They informed me they will plug the well in 6 months. This time frame allows them to use the production equipment on a well they will drill in Pickaway county. |
1171136631 | 2018-09-21 | Production Wells | No Violations | My inspection revealed the well consists of a pumping unit and a temporary 300 barrel tank that was used to test the well. I have received a plugging permit and a plugging plan from Northwood Energy. The well is scheduled to be plugged when the crop is harvested. |
1293346450 | 2017-08-07 | Production Wells | No Violations | There has been no change in the status of the well. I called Northwood Energy to find out when they plan on bringing the well into compliance. |
1358745759 | 2017-10-05 | Production Wells | No Violations | My inspection today revealed the well is not in production. The well consists of a pumping unit and a horizontal tank. The well has not showed production since it was completed in 2014. The polish rod is dull and the pulleys are rusty. There has been no attempt to bring the well into compliance. |
1373906130 | 2013-07-14 | Drill / Deepen / Reopen | No Violations | The pits are complete, the rig is set up. The site is graded. Bob Brock stated they will spud tonight. |
1374244179 | 2013-07-19 | Drill / Deepen / Reopen | No Violations | FMS drilling is having some problems with drift. They have stopped drilling on air and have switched to mud based fluid. 234 reached at 1030 hours today. |
1375042775 | 2013-07-28 | Drill / Deepen / Reopen | No Violations | FMS drilling reached total depth at 0600 hours. They placed a 100 bottom plug from 3795 to 3695. They will be running 4.5 production string this evening. Northwoods energy geologist has Formation cementing the production string to achieve 1000 of fill up. |
1427960172 | 2013-10-30 | Drill / Deepen / Reopen | No Violations | Producers Services on site at 0630 hours. The well is being stimulated using a slick water frac. |
1477656252 | 2016-10-28 | Production Wells | Violations Noted | |
1514295374 | 2017-12-26 | Production Wells | No Violations | My inspection revealed the well is not in compliance. The well consists of a pumping unit and a 300 barrel horizonal tank. The tank was used to pump into to test the well. I have spoken with Northwood Energy concerning the status of this well. I was told the well would be plugged in approximately 6 months and the production equipment will be used on a new well in Pickaway county. |
1547125084 | 2019-01-10 | Production Wells | No Violations | My inspection revealed the wells status remains unchanged. The well consists of a pumping unit and a temporary tank that was used to test the well. I have a plugging permit for this well and will contact Northwood Energy to find out when the well will be plugged. |
1555591523 | 2019-04-18 | Production Wells | No Violations | My inspection revealed this wells status remains unchanged. The well was cited for 1509:12(B), well shall be plugged. I have a plugging permit for this well and have spoken to plugging contractor Knox Energy. They are waiting on the ground to dry up before plugging this well. |
180674489 | 2013-7-21 0:00: | DD | No Violations | 4.00 |
2010000093 | 2013-07-29 | Drill / Deepen / Reopen | No Violations | Production casing has been installed and cemented. FMS is rigging down. |
2079081813 | 2013-07-25 | Drill / Deepen / Reopen | No Violations | FMS drilling is on schedule with their drilling production. They have reached 2854 by 0730 hours this day. No problems were observed. |
33363631 | 2013-7-17 0:00: | DD | No Violations | 2.00 |
Inspection ID | Violation ID | Violation Date | Violation Code | Violation Comments |
---|---|---|---|---|
1477656252 | US-OH-113662 | 2016-11-03 | NONE | Well shall be plugged |
For data sources see[9]