X

Track changes made to this page

If you find this page useful and would like to be notified of changes made to this page, start by inputting your email below.



Privacy policy
Close this window

powered by ChangeDetection

34-045-21498

Well Details

Well ID: 34-045-21498
Loading map...
Country: United States
State: Ohio
County: Fairfield
Municipality: Liberty Township
Operator Name: BECK ENERGY CORPORATION
Well Pad ID:
Farm/Lease Name: MASA HARVEY
License Status: Final Restoration
License Date: 2014-07-16
Spud Date: 2014-10-14
Spud Drilling Contractor: POULSON DRILLING
Final Drill Date: 2014-10-19
Well Total Depth: 3749.00 ft
Configuration: Vertical
Latitude: 39.930000
Longitude: -82.690000

For data sources see[1]

Well History

Well Status Well Status Date Comment
APP 2014-07-16 Proposed Formations:TREMPEALEAU, Issued Date:7/16/2014, Expired Date:7/15/2016 12:00:00 PM, Drilling unit acres:194.75, Proposed Well Type:OG, Proposed Well Class:POOL
Plugged/Abandoned 2014-10-19
Reached Total Depth 2014-10-19
Completion Report Received 2014-12-15
Construction Permit Expires 2016-07-15
Record Last Modified 2018-12-04

For data sources see[2]

Inspection Data

Inspections Performed

Inspection ID Inspection Date Inspection Type Inspection Result Inspection Comments
-1235073894 2014-10-15 0:00 DD No Violations 4.00
-1469697100 2018-11-21 0:00 FR No Violations 0.30
0021881944 2014-10-15 Drill / Deepen / Reopen No Violations BOP/cement test. The test was held at 350PSI for 30 minutes with no loss in pressure.
0735596173 2014-10-30 Plug / Plug Back No Violations Contractor on site solidifying the pits. 48 tons of cement were used to mix with the cutting. The well casing was cut of 30 below grade and capped with a plate engraved with the permit number.
0998074269 2014-10-14 Drill / Deepen / Reopen No Violations Polson Drilling is on site. They are drilling on fluid, 198 reached by 1429 hours. They are still in drift.
1235073894 2014-10-15 Drill / Deepen / Reopen No Violations Surface casing job. Petroset Cementing on site at 0600 hours. 175 sacks class A cement with good cement returns.
1413745518 2014-10-19 Plug / Plug Back No Violations Poulson drilling is plugging well due to dry hole. The first plug was at the Trempleau at 3717-3517. Formation Cemneting ran a 200 plug at 50 sacks of class a cement @ 2 % gel. The Trenton plug was set at 3110-2960. Formation Cementing set a 150 class A cement @ 2% gel. Clinton plug was set at 1878-1728. Formation Cementing set a 150class A cement plug @ 2 %gel. The Big Lime plug was set at 1183-983. Formation Cementing set a 50 sack plug at 2%gel. The bottom of the surface plug was set at 544-344. Formation Cementing set a 200 cement plug at 50 sacks of 2%gel cement. The plugs were ran thru 60 joints of 3.5casing at 15.50lb/ft. and 58 joints of 3.5drill pipe at 13.30lb/ft. All plugs circulated. Pulled all collars out and bit and sub and broke down Blow Out Preventer. Fluid was down 200 and started to pump cement and cement did not come up to surface. Shut down and grout back in morning.
1469697100 2018-11-21 Final Restoration No Violations My inspection revealed this well was plugged in 2014. The well meets the requirements for final restoration.
2088747590 2014-10-20 Plug / Plug Back No Violations Inspector Pat Shreve witnessed the plugging of this well. The surface plug fell on 10/19/2014. 9 sack grout was used to fill up approx. 225 inside the 8.62 surface casing.
21881944 2014-10-15 0:00 DD No Violations 4.00
735596173 2014-10-30 0:00 PB No Violations 8.00
998074269 2014-10-14 0:00 DD No Violations 3.00

For data sources see[3]

References