If you find this page useful and would like to be notified of changes made to this page, start by inputting your email below.
powered by ChangeDetection
Well ID: 34-045-21505 | Loading map...
{"type":"SATELLITE","minzoom":false,"maxzoom":false,"types":["ROADMAP","SATELLITE","HYBRID","TERRAIN"],"mappingservice":"googlemaps3","width":"100%","height":"350px","centre":false,"title":"","label":"","icon":"","visitedicon":"","lines":[],"polygons":[],"circles":[],"rectangles":[],"wmsoverlay":false,"copycoords":false,"static":false,"zoom":14,"layers":[],"controls":["pan","zoom","type","scale","streetview","rotate"],"zoomstyle":"DEFAULT","typestyle":"DEFAULT","autoinfowindows":false,"resizable":false,"kmlrezoom":false,"poi":true,"markercluster":false,"clustergridsize":60,"clustermaxzoom":20,"clusterzoomonclick":true,"clusteraveragecenter":true,"clusterminsize":2,"imageoverlays":[],"kml":[],"gkml":[],"searchmarkers":"","enablefullscreen":false,"scrollwheelzoom":false,"locations":[{"text":"","title":"","link":"","lat":39.89,"lon":-82.68,"icon":""}]} |
Country: United States | |
State: Ohio | |
County: Fairfield | |
Municipality: Liberty Township | |
Operator Name: ARTEX OIL COMPANY | |
Well Pad ID: | |
Farm/Lease Name: KUHN-HARVEY UNIT | |
License Status: Final Restoration | |
License Date: 2018-09-18 | |
Spud Date: 2018-10-15 | |
Spud Drilling Contractor: | |
Final Drill Date: 2019-03-12 | |
Well Total Depth: 3701.00 ft | |
Configuration: Vertical | |
Latitude: 39.890000 | |
Longitude: -82.680000 |
For data sources see[1]
Well Status | Well Status Date | Comment |
---|---|---|
APP | 2018-09-18 | Proposed Formations:KNOX, Issued Date:9/18/2018, Expired Date:9/17/2020 12:00:00 PM, Drilling unit acres:22.71, Proposed Well Type:OG, Proposed Well Class:EOUT |
Plugged/Abandoned | 2019-03-12 | |
Record Last Modified | 2019-05-25 | |
Construction Permit Expires | 2020-09-17 |
For data sources see[2]
Perforation Date | Interval Top (ft) | Interval Base (ft) | Number of Shots |
---|---|---|---|
3543 | 3564 | 0 | |
3543 | 3564 | 0 |
For data sources see[3]
Inspection ID | Inspection Date | Inspection Type | Inspection Result | Inspection Comments |
---|---|---|---|---|
-1077769770 | 2018-10-10 0:00 | DD | No Violations | 0.30 |
-1122192574 | 2018-10-12 0:00 | DD | No Violations | 0.80 |
-1450198268 | 2019-3-11 0:00: | PB | No Violations | 4.30 |
-148490049 | 2019-5-15 0:00: | FR | No Violations | 1.30 |
-1527014017 | 2019-3-7 0:00:0 | PB | No Violations | 3.60 |
-1887197181 | 2018-10-16 0:00 | DD | No Violations | 5.50 |
-266228584 | 2018-12-4 0:00: | PL | No Violations | 0.30 |
-322167174 | 2018-10-22 0:00 | DD | No Violations | 0.90 |
-567581111 | 2018-10-9 0:00: | DD | No Violations | 0.90 |
-7051739 | 2018-11-5 0:00: | DD | No Violations | 0.50 |
-753531895 | 2018-11-21 0:00 | CT | No Violations | 0.20 |
0007051739 | 2018-11-05 | Drill / Deepen / Reopen | No Violations | My inspection revealed Artex Oil Company has hired a service rig to perforate the 4.5 inch diameter casing. This will be accomplished today. After they perforate the casing the well will be treated to help the well to produce hydrocarbons. |
0148490049 | 2019-05-15 | Final Restoration | No Violations | My inspection revealed this well meets requirements for final restoration. The area where the well was located is in agricultural field. The owners of the well respreads the topsoil. This is all that is required to meet requirements for final restoration. |
0174920969 | 2018-11-07 | Completion Testing | No Violations | My inspection revealed the well has been perforated and treated with acid. Artex oil is in the process of completing this well. Equipment was on site during my inspection working on the restoration. |
0179600304 | 2018-10-16 | Drill / Deepen / Reopen | No Violations | Kilbarger rig number 5 has reached 219 feet at the time of my inspection. 216 feet of 9.62 inch diameter casing was ran using 200 sacks of class A cement with 600 pounds of accelerator and 80 pounds lost circulation material. The permit was displayed in the dog house. The site was neat and orderly. There is a power broom on site to keep the public road clear of debris. |
0266228584 | 2018-12-04 | Preliminary Restoration | No Violations | My inspection reveled the well does not meet the requirement for preliminary restoration. The pits have been left open to use for plugging the well. The well will be plugged by 12.7.2018. |
0322167174 | 2018-10-22 | Drill / Deepen / Reopen | No Violations | Kilbarger rig number 5 current drilling depth was 3173 feet at 8:10 AM. They plan on switching to drilling on fluid at 3450 feet. The permit was posted in the doghouse. I spoke with drilling manager Mr. Heath Halsted and he said they should be switching to drilling on fluid at 6:00 PM. |
0416266646 | 2019-01-10 | Production Wells | No Violations | My inspection revealed this well consists of casing wellhead. Artex Oil Company has decided to plug this well. The well will be plugged using the drilling permit that is still valid. The pits have not been filled as they will be used to plug this well. I spoke with Artexs drilling manager and he said the well would be plugged by the end of January 2019. |
0567581111 | 2018-10-09 | Drill / Deepen / Reopen | No Violations | I met Artex drilling superintendent Mr. Heath Halstead and Kilbarger drilling superintendent Mr. Gary Smith on site. Kilbarger has delivered the mud pump and several loads of drilling equipment to the location. The pits have not yet been constructed. Mr. Gary Smith expects to move the rig late today or early tomorrow. |
0712335228 | 2018-09-28 | Drill / Deepen / Reopen | No Violations | My inspection revealed the location has not been built yet. I will perform an inspection once the location has been started. |
0753531895 | 2018-11-21 | Completion Testing | No Violations | I met with Artex Oil Company regarding the future of this well. Mr. Don Huck stated the well would likely be plugged in the near future. I asked Mr. Huck to keep me informed when they made a decision on weather or not the well would be plugged. |
0917878013 | 2018-10-18 | Drill / Deepen / Reopen | No Violations | I received a call from Artex drilling manager Mr. Heath Halstead at 10:22 AM. Heath told me he would be ready for the BOP test at 1:00 PM. I arrived at 12:45 PM. The test was not ready when it was time for me to leave. On 10.17.18, they tested the blind rams at 500 psi for 15 minutes with 5 psi pressure loss. This test was not witnessed by myself. |
1077769770 | 2018-10-10 | Drill / Deepen / Reopen | No Violations | Kilbarger has rigged up and began setting up to start drilling on 10.15.18. |
1122192574 | 2018-10-12 | Drill / Deepen / Reopen | No Violations | Kilbarger number 5 has been set up. Mud pump in place and working. The mud pit has been dug and lined, this is a two part pit. One part has been filled with fresh water, the second pit will be filled with fresh water based drilling mud. The well will spud on 10.15.18. |
1205158450 | 2018-10-15 | Drill / Deepen / Reopen | No Violations | Kilbarger rig number 5 has reached 29 feet at the time of this inspection. Pits are filled. There is a power broom on site to keep street clean of mud and debris. |
1339810380 | 2019-04-18 | Final Restoration | No Violations | My inspection revealed Kilbarger Construction is working on the final restoration. The lease road through the farm field has been graded. The pits have been filled. They are working on leveling the site before topsoil respreads. |
1364902736 | 2019-03-12 | Plug / Plug Back | No Violations | Bishop Well Service on site, they ran tubing down to 502 feet to set the bottom of surface plug. Formation Cementing on site at 8:00 AM. 40 sacks of class A cement was used to set the bottom of surface plug. The tubing was pulled up to 187 feet and 35 sacks of class A cement was used to set the surface plug. |
1450198268 | 2019-03-11 | Plug / Plug Back | No Violations | My inspection revealed Bishp Well Service on site to set the Clinton sandstone plug. Formation Cementing on site at 8:40 AM. They obtained circulation and set 40 sacks of class A cement through the 4.5 inch diamter casing. The 4.5 inch diameter casing was set at 1785 feet. Bishop Well Service pulled 4.5 inch diameter casing up to 1785 feet and Formation Cementing set a 40 sack Lime plug. Bishop Well Service pulled the remainder of the 4.5 inch diameter casing from the wellbore. The bottom of surface and surface plugs will be set through tubing on 3.12.19. |
1527014017 | 2019-03-07 | Plug / Plug Back | No Violations | Formation Cementing on site at 10:45 AM. They loaded the hole with fluid and pumped 35 sacks of class A cement. They added 50 pounds of accelerator, 10 pounds of flake and 55 pounds of lcm(cotton seed hulls) to the cement. This plug will be allowed to set up until they continue plugging this well on 3.11.19. |
174920969 | 2018-11-7 0:00: | CT | No Violations | 0.30 |
179600304 | 2018-10-16 0:00 | DD | No Violations | 2.60 |
1887197181 | 2018-10-16 | Drill / Deepen / Reopen | No Violations | Kilbarger rig number 5 reached 472 feet. They tripped out of the hole with the drill pipe. They ran 6 joints of 7 inch diameter surface casing. When they attempted to screw on the last joint of 7 inch diameter surface casing they found the collar was bad and destroyed the threads on the collar and on the joint of 7 inch diameter casing. This caused a delay due to the fact they had to acquire a new 7 inch collar. Formation Cementing ran 75 sacks of class A cement with good cement returns. The casing will be pressure tested when they test the BOP. |
2144153205 | 2018-10-24 | Drill / Deepen / Reopen | No Violations | My inspection today revealed the well has been drilled to 3670 feet. Mud loggers on site analyzing the cutting from the well. I spoke with Artex to see if they would be running production casing. They said they would know by the end of today. |
416266646 | 2019-1-10 0:00: | PW | No Violations | 0.50 |
639796197 | 2019-6-19 0:00: | FR | No Violations | 0.30 |
712335228 | 2018-9-28 0:00: | DD | No Violations | 0.10 |
917878013 | 2018-10-18 0:00 | DD | No Violations | 1.30 |
For data sources see[4]