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| Well ID: 34-053-20122 | Loading map...
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| Country: United States | |
| State: Ohio | |
| County: Gallia | |
| Municipality: Cheshire Township | |
| Operator Name: MGA ENERGY INC | |
| Well Pad ID: | |
| Farm/Lease Name: CURFMAN | |
| License Status: Final Restoration | |
| License Date: 2007-10-24 | |
| Spud Date: | |
| Spud Drilling Contractor: | |
| Final Drill Date: | |
| Well Total Depth: 1595.00 ft | |
| Configuration: Vertical | |
| Latitude: 38.940000 | |
| Longitude: -82.140000 |
For data sources see[1]
| Well Status | Well Status Date | Comment |
|---|---|---|
| APP | 2005-08-03 | Proposed Formations:BEREA, Issued Date:8/3/2005, Expired Date:8/3/2006 6:00:00 AM, Drilling unit acres:50.5, Proposed Well Type:OG, Proposed Well Class: |
| APP | 2007-10-24 | Proposed Formations:BEREA, Issued Date:10/24/2007, Expired Date:10/23/2008 6:00:00 AM, Drilling unit acres:0, Proposed Well Type:OG, Proposed Well Class: |
| Construction Permit Expires | 2008-10-23 | I.P. BE - OIL & GAS WELL. |
| Plugged/Abandoned | 2008-10-28 | I.P. BE - OIL & GAS WELL. |
| Record Last Modified | 2013-03-14 | I.P. BE - OIL & GAS WELL. |
For data sources see[2]
| Inspection ID | Inspection Date | Inspection Type | Inspection Result | Inspection Comments |
|---|---|---|---|---|
| -1221069772 | 2008-10-29 0:00 | PB | No Violations | |
| -1251009485 | 2008-10-9 0:00: | PB | No Violations | |
| -1566568987 | 2005-10-5 0:00: | PW | No Violations | |
| -1683841304 | 2005-10-25 0:00 | PW | No Violations | |
| -2047348087 | 2008-10-27 0:00 | PB | No Violations | |
| -920277560 | 2010-9-29 0:00: | FR | No Violations | |
| 0096253974 | 2008-10-28 | Plug / Plug Back | No Violations | Pumping out pit and removing tubing from location. |
| 0316303979 | 2008-10-14 | Plug / Plug Back | No Violations | Bottom hole plug set previously through 1 tubing. Wire line shot 2 tubing off at 1455 second attempt. Gas is bubbling on the outside of the 5 casing at the surface. The wellhead was excavated to 18 deep in a search for the conductor or surface casing. Neither could be found. 2 was pulled out and inspected. |
| 0357344685 | 2008-10-21 | Plug / Plug Back | No Violations | Cut casing at 1148 Possible hole in casing at 410 and 1056 according to Bruce from Appalachian Wire Line. Pulled 249 of 5. Ran 2 back in hole. Could only run 20 joints 2 and hit obstruction. Pulled 2 out to see what obstruction is. Appears to be a gray clay possibly from hole in 5. Will have to circulate the 2 in to set Injun plug. |
| 0377411966 | 2008-10-17 | Plug / Plug Back | No Violations | Ran 1435 of 2 tubing to set a 300 rip plug. |
| 0920277560 | 2010-09-29 | Final Restoration | No Violations | Site graded. Good vegetative cover established. |
| 1221069772 | 2008-10-29 | Plug / Plug Back | No Violations | Pit is closed.5 casing still on location. 2 tubing still on location. Plastic tank still on location. Dozer and winch truck with load of 1 tubing on it still on location. Stream crossing still in place. |
| 1251009485 | 2008-10-09 | Plug / Plug Back | No Violations | Plug job. 1 has been ran inside the 2 tubing to TD. Pit has been dug and lined with plastic. A plastic lined ditch from the well to the pit has been installed. A fresh water tank is on location. |
| 1429434151 | 2008-10-20 | Plug / Plug Back | No Violations | TD top of rip plug at 1294. Tried to test 5 by filling with water. 5 would not hold water. 5 must have a hole in it. Unable to determine water level in 5 at this time. Have to schedule wire line to cut casing. |
| 1566568987 | 2005-10-05 | Production Wells | No Violations | Leak in line between well head and separator. |
| 1683841304 | 2005-10-25 | Production Wells | No Violations | Leaking oil from beneath surface - pooled in hole where old surface casing had been pulled; M Altier did perform clean-up. |
| 1704103274 | 2008-10-22 | Plug / Plug Back | No Violations | Had to circulate with pump truck all day to run 2 to Injun plug zone. Did not reach zone today 4 joints short. |
| 2047348087 | 2008-10-27 | Plug / Plug Back | No Violations | Circulate last 4 joints of 2 tubing used to spot the Injun Plug. Injun plug set at 1123 to 931 had good circulation at surface. Pull 2 out and start to pull 5 out of hole. 5 has parted at 421. They retrieved 421 of 5. Ran 2 to 300 and cemented to surface in 2 stages. Good circulation and received cement at surface after second stage completed. Pulled remaining 2 out and topped off hole with cement. |
| 316303979 | 2008-10-14 0:00 | PB | No Violations | |
| 357344685 | 2008-10-21 0:00 | PB | No Violations | |
| 377411966 | 2008-10-17 0:00 | PB | No Violations | |
| 96253974 | 2008-10-28 0:00 | PB | No Violations |
For data sources see[3]