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34-053-20122

Well Details

Well ID: 34-053-20122
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Country: United States
State: Ohio
County: Gallia
Municipality: Cheshire Township
Operator Name: MGA ENERGY INC
Well Pad ID:
Farm/Lease Name: CURFMAN
License Status: Final Restoration
License Date: 2007-10-24
Spud Date:
Spud Drilling Contractor:
Final Drill Date:
Well Total Depth: 1595.00 ft
Configuration: Vertical
Latitude: 38.940000
Longitude: -82.140000

For data sources see[1]

Well History

Well Status Well Status Date Comment
APP 2005-08-03 Proposed Formations:BEREA, Issued Date:8/3/2005, Expired Date:8/3/2006 6:00:00 AM, Drilling unit acres:50.5, Proposed Well Type:OG, Proposed Well Class:
APP 2007-10-24 Proposed Formations:BEREA, Issued Date:10/24/2007, Expired Date:10/23/2008 6:00:00 AM, Drilling unit acres:0, Proposed Well Type:OG, Proposed Well Class:
Construction Permit Expires 2008-10-23 I.P. BE - OIL & GAS WELL.
Plugged/Abandoned 2008-10-28 I.P. BE - OIL & GAS WELL.
Record Last Modified 2013-03-14 I.P. BE - OIL & GAS WELL.

For data sources see[2]

Inspection Data

Inspections Performed

Inspection ID Inspection Date Inspection Type Inspection Result Inspection Comments
-1221069772 2008-10-29 0:00 PB No Violations
-1251009485 2008-10-9 0:00: PB No Violations
-1566568987 2005-10-5 0:00: PW No Violations
-1683841304 2005-10-25 0:00 PW No Violations
-2047348087 2008-10-27 0:00 PB No Violations
-920277560 2010-9-29 0:00: FR No Violations
0096253974 2008-10-28 Plug / Plug Back No Violations Pumping out pit and removing tubing from location.
0316303979 2008-10-14 Plug / Plug Back No Violations Bottom hole plug set previously through 1 tubing. Wire line shot 2 tubing off at 1455 second attempt. Gas is bubbling on the outside of the 5 casing at the surface. The wellhead was excavated to 18 deep in a search for the conductor or surface casing. Neither could be found. 2 was pulled out and inspected.
0357344685 2008-10-21 Plug / Plug Back No Violations Cut casing at 1148 Possible hole in casing at 410 and 1056 according to Bruce from Appalachian Wire Line. Pulled 249 of 5. Ran 2 back in hole. Could only run 20 joints 2 and hit obstruction. Pulled 2 out to see what obstruction is. Appears to be a gray clay possibly from hole in 5. Will have to circulate the 2 in to set Injun plug.
0377411966 2008-10-17 Plug / Plug Back No Violations Ran 1435 of 2 tubing to set a 300 rip plug.
0920277560 2010-09-29 Final Restoration No Violations Site graded. Good vegetative cover established.
1221069772 2008-10-29 Plug / Plug Back No Violations Pit is closed.5 casing still on location. 2 tubing still on location. Plastic tank still on location. Dozer and winch truck with load of 1 tubing on it still on location. Stream crossing still in place.
1251009485 2008-10-09 Plug / Plug Back No Violations Plug job. 1 has been ran inside the 2 tubing to TD. Pit has been dug and lined with plastic. A plastic lined ditch from the well to the pit has been installed. A fresh water tank is on location.
1429434151 2008-10-20 Plug / Plug Back No Violations TD top of rip plug at 1294. Tried to test 5 by filling with water. 5 would not hold water. 5 must have a hole in it. Unable to determine water level in 5 at this time. Have to schedule wire line to cut casing.
1566568987 2005-10-05 Production Wells No Violations Leak in line between well head and separator.
1683841304 2005-10-25 Production Wells No Violations Leaking oil from beneath surface - pooled in hole where old surface casing had been pulled; M Altier did perform clean-up.
1704103274 2008-10-22 Plug / Plug Back No Violations Had to circulate with pump truck all day to run 2 to Injun plug zone. Did not reach zone today 4 joints short.
2047348087 2008-10-27 Plug / Plug Back No Violations Circulate last 4 joints of 2 tubing used to spot the Injun Plug. Injun plug set at 1123 to 931 had good circulation at surface. Pull 2 out and start to pull 5 out of hole. 5 has parted at 421. They retrieved 421 of 5. Ran 2 to 300 and cemented to surface in 2 stages. Good circulation and received cement at surface after second stage completed. Pulled remaining 2 out and topped off hole with cement.
316303979 2008-10-14 0:00 PB No Violations
357344685 2008-10-21 0:00 PB No Violations
377411966 2008-10-17 0:00 PB No Violations
96253974 2008-10-28 0:00 PB No Violations

For data sources see[3]

References