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34-053-20246

Well Details

Well ID: 34-053-20246
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Country: United States
State: Ohio
County: Gallia
Municipality: Addison Township
Operator Name: OHIO VALLEY ELECTRIC CORP
Well Pad ID:
Farm/Lease Name: VAN GILDER
License Status: Final Restoration
License Date: 2007-11-02
Spud Date: 1977-08-10
Spud Drilling Contractor:
Final Drill Date: 1977-08-23
Well Total Depth: 1801.00 ft
Configuration: Vertical
Latitude: 38.920000
Longitude: -82.150000

For data sources see[1]

Well History

Well Status Well Status Date Comment
CO 1977-06-13 40 ORWIG CHAS DBA ORWIG OIL GeoDate 6/13/77
Original Spud 1977-08-10 R.L. 7-27-77
Completed 1977-08-23 R.L. 7-27-77
Reached Total Depth 1977-08-23 R.L. 7-27-77
APP 2007-11-02 Proposed Formations:BEREA, Issued Date:11/2/2007, Expired Date:11/1/2008 6:00:00 AM, Drilling unit acres:0, Proposed Well Type:OG, Proposed Well Class:
Change of Owner 2007-11-14 Operator changed from 40, ORWIG ANITA DBA ORWIG OIL to 8161, OHIO VALLEY ELECTRIC CORP
Plugged/Abandoned 2007-11-28 R.L. 7-27-77
Construction Permit Expires 2008-11-01 R.L. 7-27-77
Record Last Modified 2013-03-14 R.L. 7-27-77

For data sources see[2]

Perforation Treatments

Perforation Date Interval Top (ft) Interval Base (ft) Number of Shots
2006-09-11 1760 1788 39
1760 1788 39
1760 1788 39

For data sources see[3]

Stimulations Data

Stimulation Date Chemical Agent Chemical Agent Concentration (%) Fracking Fluid Volume Mass of Proppant Used (lb) Fracking Company Comments
H2O 0 2000 Bbl 35000

For data sources see[4]

Production Data

Period Operator Name Gas Quantity (mcf) Oil Quantity (bbl) Production Days
1984 ORWIG OIL COMPANY INC 914.00 75.00 0
1985 ORWIG OIL COMPANY INC 1289.00 68.00 0
1986 ORWIG OIL COMPANY INC 1576.00 111.00 365
1987 ORWIG OIL COMPANY INC 1548.00 67.00 365
1988 ORWIG OIL COMPANY INC 1486.00 65.00 0
1991 ORWIG OIL COMPANY INC 1314.00 54.00 365
1992 ORWIG OIL COMPANY INC 1249.00 53.00 3
2000 ORWIG OIL COMPANY INC 1007.00 49.00 365
2001 ORWIG OIL COMPANY INC 336.00 0.00 365
2002 ORWIG OIL COMPANY INC 605.00 38.00 365
2003 ORWIG OIL COMPANY INC 306.00 0.00 365
2004 ORWIG OIL COMPANY INC 90.00 0.00 365
2005 ORWIG OIL COMPANY INC 126.00 0.00 365
2006 ORWIG OIL COMPANY INC 164.00 30.00 365
2007 ORWIG OIL COMPANY INC 9.00 8.00 282

For data sources see[5] [6]

Waste Data

Period Operator Name Waste Type Quantity (bbl) Production Days
1984 ORWIG OIL COMPANY INC Brine 7 0
1985 ORWIG OIL COMPANY INC Brine 6 0
1986 ORWIG OIL COMPANY INC Brine 5 365
1987 ORWIG OIL COMPANY INC Brine 3 365
1988 ORWIG OIL COMPANY INC Brine 3 0
1991 ORWIG OIL COMPANY INC Brine 3 365
1992 ORWIG OIL COMPANY INC Brine 0 3
2000 ORWIG OIL COMPANY INC Brine 0 365
2001 ORWIG OIL COMPANY INC Brine 0 365
2002 ORWIG OIL COMPANY INC Brine 0 365
2003 ORWIG OIL COMPANY INC Brine 0 365
2004 ORWIG OIL COMPANY INC Brine 0 365
2005 ORWIG OIL COMPANY INC Brine 0 365
2006 ORWIG OIL COMPANY INC Brine 0 365
2007 ORWIG OIL COMPANY INC Brine 0 282

For data sources see[7] [8]

Inspection Data

Inspections Performed

Inspection ID Inspection Date Inspection Type Inspection Result Inspection Comments
-1460774270 2003-4-18 0:00: PW No Violations
-1469838095 2007-4-5 0:00:0 PW No Violations
-277820270 2007-11-20 0:00 PB No Violations
001269i714 2002-01-24 Production Wells No Violations Follow-up on NOV, Non - Compliance, no action to comply with the NOV.
0277820270 2007-11-20 Plug / Plug Back No Violations One of the next wells on plug list. Took GPS on well and checked status. All tubing and rods pulled and pump jack removed.
0490884593 2004-08-12 Production Wells No Violations No violations.
0989751597 2007-03-13 Production Wells No Violations The leak has been temporarily repaired by Pete Jeffers Orwig Pumper. I had a meeting with AEP and the logger to review what had happened. I advised AEP to have the logging operation leave a buffer zone around the wells in the work area. I called the Gallia Emergency Management office and advised them on the status of the well.
1199117548 2007-11-28 Plug / Plug Back No Violations On 11-21-07 I was at our meeting in Cambridge and was unable to witness the plugging of well #246 this is one of the AEP wells being plugged for their land fill. The bottom hole plug was set on 11-21-07. This is a Berea well. TD 1801. 300 7 in hole. 1800 4.5 in the hole. I did not receive any phone calls telling me that they had problems. The information from here on is second hand or taken from Timcos invoice and Formations invoice, I will try to put it in a time line.

Rig TD top of 1st cement plug at 1475. This is where it should be. Had calculated 1420 so it was close. Timco (wire line) arrived. They could only get to 1228 so with out calling me they decided to shoot it at 1190. This is above where I told them to start the Big Injun Plug at 1250 to 850. They shot one time. Rig tried to pull free. Could not pull free. They were able to circulate the hole to the surface. They decided to bullhead the 2nd plug at this time. Formation Bullheaded the 2nd plug. Timco tried to shoot again at 1161. Rig could not pull free. Circulated the hole to the surface. Formation Bullheaded 3rd plug. Timco tried to shoot at 637 Rig could not pull free. Circulated hole to the surface. Formation Bullheaded 4th plug. Timco tried to shoot at 300 Rig could not pull free. Circulated to surface. Formation Bullheaded 5th plug. 52 of 4.5 was all that was recovered. They unscrewed it.

The Cement job including setup and cleanup was from 12:40 pm to 4:00 pm. I do not feel that 3 hours and 20 minutes was enough time to make a good faith effort in recovering the casing and plugging the well correctly. I believe that a second effort should have been made to recover the casing at all areas that were attempted. One try and giving up does not in my mind make a good faith effort. I arrived on site at 4:00 pm and passed Formation on the road. I was first lead to believe that 300 of 4.5 had been recovered. The rig was all ready moving to the next location. I went to the next loca

1211241820 2007-03-12 Production Wells No Violations Well has been severely damaged by logging activity. Well casing and tubing has been bent and leaking badly. Other damage was done to the pump jack and to production piping. I informed AEP of the problem. I called the Gallia county sheriff and the Gallia Emergency Management of the leak and the location. I called Anita Orwig in Florida, she gave me the name of her tender Woody Harris. I called Woody Harris and he gave me the name of the pumper Pete Jeffers. They informed me that they would be on site in the morning. I also called the logger Art Saylor and informed him of the situation and warned him not to take any equipment near the leak for fear of ignition. The loggers are using the area around the well to stock pile logs for processing. This makes a lot of fuel around the leaking well.
1257040870 2005-05-09 Production Wells No Violations Well being serviced by Century for production problems. No ID.
1269i714 2002-1-24 0:00: PW No Violations
1329468236 2005-10-06 Production Wells No Violations Corrected ID problem. Well #20241 is shown in same location in RBMS.
1460774270 2003-04-18 Production Wells No Violations No violations at the time of inspection.
1469838095 2007-04-05 Production Wells No Violations Well is leaking again due to the damage caused by the logging activity of AEP. The leak is slight at this time. Talked to Gary Millmine and he is going to try to get a service rig on the site ASAP.
1610579627 2008-04-03 Final Restoration No Violations Ohio Valley Electric Corp. is constructing a landfill for FGD generated from the Kyger Creek Power Plant. The well site is located within the landfill project area and excavation to the location is underway. OVEC has submitted a landowner waiver for the restoration due to their construction of the landfill.
1867413950 2007-11-21 Plug / Plug Back No Violations Set bottom hole plug. Used the bullhead method to place the plug in the casing.
1931376892 2008-12-04 Administrative Inspection No Violations I called Formation Cementing Inc. 740-453-6926 and requested a Job log on the entire plug job Van Gilder #2. At 4:01pm on 12-4-08. I talked to Missy. A single page was faxed to ODNR-DMRM Jackson Office at 5:57pm on 12-4-08. Single page was for date 11-28-07 invoice # 11630. They did not send a copy of the job log for 11-21-07.
490884593 2004-8-12 0:00: PW No Violations
989751597 2007-3-13 0:00: PW No Violations

For data sources see[9]

References