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| Well ID: 34-053-20824 | Loading map...
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| Country: United States | |
| State: Ohio | |
| County: Gallia | |
| Municipality: Cheshire Township | |
| Operator Name: WYANT EXPLORATION COMPANY | |
| Well Pad ID: | |
| Farm/Lease Name: OHIO POWER CO | |
| License Status: Final Restoration | |
| License Date: 2013-02-01 | |
| Spud Date: 1983-03-22 | |
| Spud Drilling Contractor: GARD DRILLING | |
| Final Drill Date: 1983-03-25 | |
| Well Total Depth: 1781.00 ft | |
| Configuration: Vertical | |
| Latitude: 38.950000 | |
| Longitude: -82.140000 |
For data sources see[1]
| Well Status | Well Status Date | Comment |
|---|---|---|
| CO | 1983-01-26 | 161 KRAMER EXPLORATION CO GeoDate 1/26/83 |
| Oil and Gas | 1983-01-26 | Issued Date 1/26/83 Expired Date 7/25/83 Acres 0010000 Tool Type RTF Proposed Formation BEREA Proposed Depth 01781 Proposed Drill Depth 01781 |
| Original Spud | 1983-03-22 | |
| Completed | 1983-03-25 | |
| Reached Total Depth | 1983-03-25 | |
| Completion Report Received | 1983-05-02 | |
| Change of Owner | 2009-12-18 | Operator changed from 161, KRAMER EXPLORATION CO to 8592, WYANT EXPLORATION COMPANY |
| APP | 2013-02-01 | Proposed Formations:BEREA, Issued Date:2/1/2013, Expired Date:2/1/2015 12:00:00 PM, Drilling unit acres:10, Proposed Well Type:OG, Proposed Well Class: |
| Plugged/Abandoned | 2013-08-12 | |
| Construction Permit Expires | 2015-02-01 | |
| Record Last Modified | 2017-02-15 |
For data sources see[2]
| Perforation Date | Interval Top (ft) | Interval Base (ft) | Number of Shots |
|---|---|---|---|
| 1997-06-29 | 1646 | 1666 | 0 |
| 1646 | 1666 | 0 | |
| 2006-09-11 | 1712 | 1724 | 13 |
| 1712 | 1724 | 13 | |
| 1646 | 1666 | 0 |
For data sources see[3]
| Stimulation Date | Chemical Agent | Chemical Agent Concentration (%) | Fracking Fluid Volume | Mass of Proppant Used (lb) | Fracking Company | Comments |
|---|---|---|---|---|---|---|
| H2O | 0 | 1700 Bbl | 40000 | FRAC;1700BBL H2O,40M# SAND |
For data sources see[4]
| Period | Operator Name | Gas Quantity (mcf) | Oil Quantity (bbl) | Production Days |
|---|---|---|---|---|
| 1984 | KRAMER EXPLORATION CO | 5528.00 | 335.00 | 0 |
| 1985 | KRAMER EXPLORATION CO | 3657.00 | 259.00 | 365 |
| 1986 | KRAMER EXPLORATION CO | 2665.00 | 161.00 | 365 |
| 1987 | KRAMER EXPLORATION CO | 2978.00 | 137.00 | 365 |
| 1988 | KRAMER EXPLORATION CO | 1399.00 | 62.00 | 365 |
| 1989 | KRAMER EXPLORATION CO | 2505.00 | 91.00 | 365 |
| 1990 | KRAMER EXPLORATION CO | 1989.00 | 57.00 | 365 |
| 1991 | KRAMER EXPLORATION CO | 1354.00 | 75.00 | 365 |
| 1992 | KRAMER EXPLORATION CO | 984.00 | 96.00 | 365 |
| 1993 | KRAMER EXPLORATION CO | 764.00 | 65.00 | 365 |
| 1994 | KRAMER EXPLORATION CO | 647.00 | 68.00 | 365 |
| 1995 | KRAMER EXPLORATION CO | 666.00 | 67.00 | 365 |
| 1996 | KRAMER EXPLORATION CO | 589.00 | 51.00 | 365 |
| 1997 | KRAMER EXPLORATION CO | 626.00 | 99.00 | 365 |
| 1998 | KRAMER EXPLORATION CO | 621.00 | 53.00 | 365 |
| 2000 | KRAMER EXPLORATION CO | 620.00 | 66.00 | 365 |
| 2001 | KRAMER EXPLORATION CO | 592.00 | 63.00 | 365 |
| 2002 | KRAMER EXPLORATION CO | 531.00 | 44.00 | 365 |
| 2003 | KRAMER EXPLORATION CO | 455.00 | 42.00 | 365 |
| 2004 | KRAMER EXPLORATION CO | 605.00 | 55.00 | 365 |
| 2005 | KRAMER EXPLORATION CO | 454.00 | 48.00 | 365 |
| 2006 | KRAMER EXPLORATION CO | 452.00 | 37.00 | 365 |
| 2007 | KRAMER EXPLORATION CO | 313.00 | 47.00 | 365 |
| 2008 | KRAMER EXPLORATION CO | 359.00 | 29.00 | 365 |
| 2009 | KRAMER EXPLORATION CO | 370.00 | 32.00 | 365 |
| 2010 | WYANT EXPLORATION CO | 427.00 | 33.00 | 365 |
| 2011 | WYANT EXPLORATION COMPANY | 419.00 | 45.00 | 365 |
| 2012 | WYANT EXPLORATION COMPANY | 397.00 | 30.00 | 366 |
| 2013 | WYANT EXPLORATION COMPANY | 218.00 | 27.00 | 270 |
| Inspection ID | Inspection Date | Inspection Type | Inspection Result | Inspection Comments |
|---|---|---|---|---|
| -398792290 | 2015-6-16 0:00: | FR | No Violations | 1.00 |
| -538164077 | 2004-8-18 0:00: | PW | No Violations | |
| -990120817 | 2013-8-12 0:00: | PB | No Violations | 5.00 |
| 0398792290 | 2015-06-16 | Final Restoration | No Violations | On my inspection I found that the location had been restored according to 1509.072. I passed the final restoration at this time. |
| 0538164077 | 2004-08-18 | Production Wells | No Violations | No violations. |
| 0709754246 | 2013-08-09 | Plug / Plug Back | No Violations | Bowers crew mobilized to this well to set the Berea Sandstone plug over the perforated interval from 1724 to 1712-feet. They removed 1710.5 -feet of 1-1/2 inch production tubing. They bullheaded 30 sacks of Class A neet cement through the 4-1/2 inch production casing. Shut the well in and quit for the weekend. |
| 0990120817 | 2013-08-12 | Plug / Plug Back | No Violations | Bowers crew tagged the top of the Berea plug at 1250-feet. They ripped the 4-1/2 inch production casing at 1090 and removed. They prepared to run the 100-feet in/100-feet out bottom of the 7-inch surface casing plug at 250-feet using the 1-1/2 inch production tubing. They circulated 40 sacks of Class A neet cement over the bottom of the 7-inch surface casing. Came up hole and circulated and set the top of the 7-inch surface casing plug from 100-feet to surface using 20 sacks of Class A neet cement. They mobilized their equipment to the next well site before they stopped work for the day. I left this location and went to the Equity O & G, Riley #1, API# 3408720176, plug job preparation in Lawrence County. |
| 709754246 | 2013-8-9 0:00:0 | PB | No Violations | 3.00 |
For data sources see[9]