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34-053-20958

Well Details

Well ID: 34-053-20958
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Country: United States
State: Ohio
County: Gallia
Municipality: Addison Township
Operator Name: OHIO VALLEY ELECTRIC CORP
Well Pad ID:
Farm/Lease Name: REESE MICHAEL
License Status: Final Restoration
License Date: 2007-11-02
Spud Date: 1991-10-31
Spud Drilling Contractor: R WOLFE DRLG
Final Drill Date: 1991-11-05
Well Total Depth: 1800.00 ft
Configuration: Vertical
Latitude: 38.910000
Longitude: -82.140000

For data sources see[1]

Well History

Well Status Well Status Date Comment
Oil and Gas 1991-10-30 Issued Date 10/30/91 Expired Date 10/29/92 Acres 0068620 Tool Type RTA Proposed Formation BEREA Proposed Depth 01800 Proposed Drill Depth 01800
Original Spud 1991-10-31
Completed 1991-11-05
Reached Total Depth 1991-11-05
CO 1991-11-15 40 ORWIG CHAS DBA ORWIG OIL GeoDate 10/30/91
Completion Report Received 1992-01-10
APP 2007-11-02 Proposed Formations:BEREA, Issued Date:11/2/2007, Expired Date:11/1/2008 6:00:00 AM, Drilling unit acres:0, Proposed Well Type:OG, Proposed Well Class:
Change of Owner 2007-11-14 Operator changed from 40, ORWIG ANITA DBA ORWIG OIL to 8161, OHIO VALLEY ELECTRIC CORP
Plugged/Abandoned 2007-12-12
Construction Permit Expires 2008-11-01
Record Last Modified 2017-02-15

For data sources see[2]

Perforation Treatments

Perforation Date Interval Top (ft) Interval Base (ft) Number of Shots
1997-06-29 1702 1720 3
1702 1720 3
2006-09-11 1710 1720 18
1710 1720 18
1702 1720 3

For data sources see[3]

Stimulations Data

Stimulation Date Chemical Agent Chemical Agent Concentration (%) Fracking Fluid Volume Mass of Proppant Used (lb) Fracking Company Comments
H2O 0 1500 Bbl 35000 FRAC W/1500 BW & 350 SX SAND

For data sources see[4]

Production Data

Period Operator Name Gas Quantity (mcf) Oil Quantity (bbl) Production Days
1991 T & H DRILLING 693.00 0.00 365
2000 ORWIG OIL COMPANY INC 696.00 58.00 365
2001 ORWIG OIL COMPANY INC 142.00 69.00 365
2002 ORWIG OIL COMPANY INC 114.00 73.00 365
2003 ORWIG OIL COMPANY INC 55.00 45.00 365
2004 ORWIG OIL COMPANY INC 18.00 22.00 365
2005 ORWIG OIL COMPANY INC 22.00 108.00 365
2006 ORWIG OIL COMPANY INC 29.00 66.00 365
2007 ORWIG OIL COMPANY INC 2.00 23.00 282

For data sources see[5] [6]

Waste Data

Period Operator Name Waste Type Quantity (bbl) Production Days
1991 T & H DRILLING Brine 15 365
2000 ORWIG OIL COMPANY INC Brine 0 365
2001 ORWIG OIL COMPANY INC Brine 0 365
2002 ORWIG OIL COMPANY INC Brine 0 365
2003 ORWIG OIL COMPANY INC Brine 0 365
2004 ORWIG OIL COMPANY INC Brine 0 365
2005 ORWIG OIL COMPANY INC Brine 0 365
2006 ORWIG OIL COMPANY INC Brine 0 365
2007 ORWIG OIL COMPANY INC Brine 0 282

For data sources see[7] [8]

Inspection Data

Inspections Performed

Inspection ID Inspection Date Inspection Type Inspection Result Inspection Comments
-1040563475 2007-11-21 0:00 PB No Violations
-1482730644 2007-12-12 0:00 PB No Violations
-1847032885 2006-5-22 0:00: PW No Violations
-2003783026 2007-12-10 0:00 PB No Violations
0163322337 2007-12-07 Plug / Plug Back No Violations Circulated well. Set bottom hole plug. Rig TD top of 1st plug at 1576. Attempted to rip at 1591, again at 1561 both attempts to rip failed to free the casing.
0187037603 2003-01-22 Preliminary Restoration No Violations Preliminary restoration meets state requirements.
0465074878 2008-04-03 Final Restoration No Violations Ohio Valley Electric Corp. is constructing a landfill for FGD generated from the Kyger Creek Power Plant. The well site is located within the landfill project area and excavation to the location is underway. OVEC has submitted a landowner waiver for the restoration due to their construction of the landfill.
1040563475 2007-11-21 Plug / Plug Back No Violations One of the next wells to be plugged. Took GPS on well and checked status of well. Rods and tubing have been pulled. Pump jack has been removed.
1099438202 2004-11-02 Production Wells No Violations No ID, stuffing box rubbers worn; well site in good condition.
1173984495 2007-03-08 Production Wells Violations Noted Well head is leaking oil. Leak has contaminated an area 3 by 20 around the 2 production pipe. Another contaminated area 8 by 10 around the well head. Electric line to the pump jack is on the ground and is a hazard. Well is not in production due to the logging operation for AEP.
1198868113 2007-04-19 Production Wells No Violations Dike at wellhead is clean of oil . The oil and soil has been moved to a plastic lined small pit next to the well. The power lines are still low. AEP is in the process of buying this well and plugging it.
1199279456 2007-12-06 Plug / Plug Back No Violations Rig TD of well at 1763. Ran 1759 of tubing and circulated the hole. Circulated 50Bbls had oil returns to the surface. Water truck ran out of water. Will set bottom plug tomorrow.
1482730644 2007-12-12 Plug / Plug Back No Violations Wire line shot 4.5 at 891 it came free. Pulled 4 joints to 763 set Cow run plug. In 200 stages. Continued this process of plugging to the surface. Cement returns at the surface. Cement stayed at the surface.
1599796983 2007-12-11 Plug / Plug Back No Violations I arrived on location at 12:45 and the pit liner was still down on one side and oil and fluid were still not contained in the pit. I told the rig crew that until the pit is corrected and cleaned up they could not continue plugging. Pit was pumped out and new liner installed. Rig Td top of 2nd plug at 1050. Started rip at 971 with tools. Rip was not successful.
163322337 2007-12-7 0:00: PB No Violations
1847032885 2006-05-22 Production Wells No Violations Line repaired and well turned back on line.
187037603 2003-1-22 0:00: PL No Violations
2003783026 2007-12-10 Plug / Plug Back No Violations Wire line could only get to 1349. 1st shot at 1292 casing did not come free. 2nd shot at 1197 casing moved. Pumped 200 plug using the casing. Pulled a partial joint and a full joint then got hung up in the hole. Decided to let 200 plug set up and try to shoot above this plug tomorrow. Pit liner fell in. I told Kramer to pump it tonight and cleanout pit. Then reline pit for next plug.
465074878 2008-4-3 0:00:0 FR No Violations

Violations Commited

Inspection ID Violation ID Violation Date Violation Code Violation Comments
1173984495 US-OH-104591 2007-03-15 Well operation causing pollution and contamination
1173984495 US-OH-104592 2007-03-15 General Safety
1173984495 US-OH-104593 2007-03-15 Well insufficiently equipped to prevent escape of oil and gas

For data sources see[9]

References