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Well ID: 34-055-20188 | Loading map...
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Country: United States | |
State: Ohio | |
County: Geauga | |
Municipality: Middlefield Township | |
Operator Name: DIVERSIFIED PRODUCTION LLC | |
Well Pad ID: | |
Farm/Lease Name: MILLER JOHN M ET UX | |
License Status: Producing | |
License Date: 1982-07-22 | |
Spud Date: 1976-10-06 | |
Spud Drilling Contractor: | |
Final Drill Date: 1976-10-16 | |
Well Total Depth: 4080.00 ft | |
Configuration: Vertical | |
Latitude: 41.480000 | |
Longitude: -81.020000 |
For data sources see[1]
Well Status | Well Status Date | Comment |
---|---|---|
Original Spud | 1976-10-06 | R.I. 9-29-76 |
Completed | 1976-10-16 | R.I. 9-29-76 |
Reached Total Depth | 1976-10-16 | R.I. 9-29-76 |
CO | 1982-07-22 | 9 EDC GeoDate 7/22/82 |
Correction to Well | 2008-06-20 | DECREASE IN UNIT SIZE TO 114.86 ACRES. |
Change of Owner | 2008-07-21 | Operator changed from 9, POWER GAS MARKETING & TRANS to 1388, EXCO - NORTH COAST ENERGY INC |
Change of Owner | 2009-12-14 | Operator changed from 1388, EXCO - NORTH COAST ENERGY INC to 7578, ENERVEST OPERATING LLC |
Change of Owner | 2017-05-01 | Operator changed from 7578, ENERVEST OPERATING LLC, to 8685, M & R INVESTMENTS OHIO LLC |
Record Last Modified | 2019-06-14 | R.I. 9-29-76 |
For data sources see[2]
Perforation Date | Interval Top (ft) | Interval Base (ft) | Number of Shots |
---|---|---|---|
2006-09-11 | 3890 | 3920 | 16 |
3890 | 3920 | 16 | |
3890 | 3920 | 16 |
For data sources see[3]
Stimulation Date | Chemical Agent | Chemical Agent Concentration (%) | Fracking Fluid Volume | Mass of Proppant Used (lb) | Fracking Company | Comments |
---|---|---|---|---|---|---|
Not Treated | 0 | 516 Gal | 40000 | VOLUME=5160 M | ||
N2 | 0 | 89600 | 0 | N2=89.6 |
For data sources see[4]
Inspection ID | Inspection Date | Inspection Type | Inspection Result | Inspection Comments |
---|---|---|---|---|
-2049059166 | 2015-5-7 0:00:0 | PW | No Violations | |
0275647667 | 2015-04-14 | Production Wells | No Violations | My inspection found the well to be equipped with a concoil wellhead. The tank battery consists of a 100 BBL production tank, a buried concrete brine tank and a mechanical separator. The 2 line at the base of the production tank to drain the brine out of the production tank is leaking and the ground has a 1 ft x 1 ft stain of oil saturated stone and soil. The proper identification is located on the tank battery. The lease road is in stable condition. I contacted Kyle Ahbel a supervisor for Enervest about repairing the tank and cleaning up the oil saturated stone and soil. |
1434029523 | 2015-06-11 | Production Wells | No Violations | My inspection found the leaking 100 BBL tank has been removed from the location and the oil saturated stone inside the tank battery has been removed and replaced with new stone. A new 50 BBL production tank has been installed on the location. No other changes to the location since my last inspection. |
1581977746 | 2010-03-08 | Production Wells | No Violations | Dike around tank battery is in good repair. One hundred barrel tank, one cement in ground tank and a mechanical separator. Heat tubes on the separator and a tank. Doesnt appear heating tubes have been used. ID sign is up. |
2049059166 | 2015-05-07 | Production Wells | No Violations | My inspection found no changes since my last inspection. The company still needs to fix the leaking fitting on the production tank and clean up the oil saturated stone. I contacted Kyle Ahbel a supervisor from Enervest and he stated that his crew informed them it was completed but he will send someone out immediately to correct the issue. |
275647667 | 2015-4-14 0:00: | PW | No Violations |
For data sources see[9]