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Well ID: 34-055-20229 | Loading map...
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Country: United States | |
State: Ohio | |
County: Geauga | |
Municipality: Parkman Township | |
Operator Name: ENERVEST OPERATING LLC | |
Well Pad ID: | |
Farm/Lease Name: MULLETT E & M | |
License Status: Plugged and Abandoned | |
License Date: 2013-10-11 | |
Spud Date: 1976-05-12 | |
Spud Drilling Contractor: | |
Final Drill Date: 1977-08-11 | |
Well Total Depth: 4202.00 ft | |
Configuration: Vertical | |
Latitude: 41.410000 | |
Longitude: -81.070000 |
For data sources see[1]
Well Status | Well Status Date | Comment |
---|---|---|
Original Spud | 1976-05-12 | |
Completed | 1977-08-11 | |
Reached Total Depth | 1977-08-11 | |
CO | 1982-07-22 | 9 EDC GeoDate 7/22/82 |
Correction to Well | 2007-05-04 | UNIT SIZE REDUCED TO 132.46 ACRES. |
Change of Owner | 2008-07-21 | Operator changed from 9, POWER GAS MARKETING & TRANS to 1388, EXCO - NORTH COAST ENERGY INC |
Change of Owner | 2009-12-14 | Operator changed from 1388, EXCO - NORTH COAST ENERGY INC to 7578, ENERVEST OPERATING LLC |
APP | 2013-10-11 | Proposed Formations:CLINTON, Issued Date:10/11/2013, Expired Date:10/11/2015 12:00:00 PM, Drilling unit acres:132.46, Proposed Well Type:OG, Proposed Well Class: |
Plugged/Abandoned | 2014-02-11 | |
Construction Permit Expires | 2015-10-11 | |
Record Last Modified | 2017-02-10 |
For data sources see[2]
Perforation Date | Interval Top (ft) | Interval Base (ft) | Number of Shots |
---|---|---|---|
2006-09-11 | 4047 | 4146 | 23 |
4047 | 4146 | 23 | |
4047 | 4146 | 23 |
For data sources see[3]
Stimulation Date | Chemical Agent | Chemical Agent Concentration (%) | Fracking Fluid Volume | Mass of Proppant Used (lb) | Fracking Company | Comments |
---|---|---|---|---|---|---|
H2O | 0 | 1250 Bbl | 47250 |
For data sources see[4]
Inspection ID | Inspection Date | Inspection Type | Inspection Result | Inspection Comments |
---|---|---|---|---|
0137394441 | 2013-04-23 | Production Wells | No Violations | My inspection found the well to be equipped with a plunger lift unit. The demco valve and the balon valves on the wellhead are closed. I spoke with Mr McDaniels from Enervest abou the well. He informed me he would call me about the issues with the well when he returns to the office. The tank battery is in good repair. The tank battery consists of a 100 BBL production tank and a mechanical separator. The proper identification is located on the tank battery. The lease road is in stable condition. |
0429512229 | 2014-09-17 | Final Restoration | No Violations | My inspection found the area where the well was has been graded, seeded, and strawed. The tank battery has been removed and has been seeded and strawed. Once vegetation is established and the company submits a flow line waiver I will pass final restoration. |
1233338441 | 2003-11-18 | Production Wells | No Violations | tanks only 100BBL &seperator, buried salt |
137394441 | 2013-4-23 0:00: | PW | No Violations | |
1392043890 | 2014-02-10 | Plug / Plug Back | No Violations | I was on location 2/10/14, to witness the plugging of this oil and gas well. Nicks Well Plugging is the contractor doing the plug job for Enervest. Nicks ran 1.5 tubing into the hole and was attempting to get the tubing down to 4146 to set the Clinton Sand plug, but was stopped by a blockage in the well. The blockage was at 3283. Nicks attempted to rotate and pump water down the tubing to dislodge the obstruction in the well. All attempts to get the tubing deeper into the well have failed. It is determined that the casing has colapsed preventing Nicks from setting the tubing to the specified depth in the well. I received approval from Supervisor Tom Hill to set a plug at the current depth of 3283. Nicks rigged up, broke circulation and pumped 10 sacks of class A cement from 3283 to 2921. Nicks has Appalachian Well Service set up to shoot the 2 7/8 casing off on 2/11/2014 in the morning and set the remainder of the plugs. |
1412776723 | 2014-10-08 | Final Restoration | No Violations | My inspection found the location has been graded and vegetation is established. Final restoration will be passed when a flow line waiver is submitted. |
429512229 | 2014-9-17 0:00: | FR | No Violations |
For data sources see[9]