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Well ID: 34-055-20246 | Loading map...
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Country: United States | |
State: Ohio | |
County: Geauga | |
Municipality: Huntsburg Township | |
Operator Name: DIVERSIFIED PRODUCTION LLC | |
Well Pad ID: | |
Farm/Lease Name: MILLER D | |
License Status: Producing | |
License Date: 1982-07-22 | |
Spud Date: 1976-10-10 | |
Spud Drilling Contractor: | |
Final Drill Date: 1976-10-20 | |
Well Total Depth: 4068.00 ft | |
Configuration: Vertical | |
Latitude: 41.520000 | |
Longitude: -81.060000 |
For data sources see[1]
Well Status | Well Status Date | Comment |
---|---|---|
Original Spud | 1976-10-10 | R.I. 6-23-76 COR. IN LOC. |
Completed | 1976-10-20 | R.I. 6-23-76 COR. IN LOC. |
Reached Total Depth | 1976-10-20 | R.I. 6-23-76 COR. IN LOC. |
CO | 1982-07-22 | 9 EDC GeoDate 7/22/82 |
Correction to Well | 2008-07-18 | UNIT SIZE DECREASED TO 89.68 ACRES. |
Change of Owner | 2008-07-21 | Operator changed from 9, POWER GAS MARKETING & TRANS to 1388, EXCO - NORTH COAST ENERGY INC |
Change of Owner | 2009-12-14 | Operator changed from 1388, EXCO - NORTH COAST ENERGY INC to 7578, ENERVEST OPERATING LLC |
Change of Owner | 2017-05-01 | Operator changed from 7578, ENERVEST OPERATING LLC, to 8685, M & R INVESTMENTS OHIO LLC |
Record Last Modified | 2019-06-14 | R.I. 6-23-76 COR. IN LOC. |
For data sources see[2]
Perforation Date | Interval Top (ft) | Interval Base (ft) | Number of Shots |
---|---|---|---|
2006-09-11 | 3878 | 3914 | 24 |
3878 | 3914 | 24 | |
3878 | 3914 | 24 |
For data sources see[3]
Stimulation Date | Chemical Agent | Chemical Agent Concentration (%) | Fracking Fluid Volume | Mass of Proppant Used (lb) | Fracking Company | Comments |
---|---|---|---|---|---|---|
GEL | 0 | 75850 Gal | 44000 |
For data sources see[4]
Inspection ID | Inspection Date | Inspection Type | Inspection Result | Inspection Comments |
---|---|---|---|---|
-444005077 | 2017-3-2 0:00:0 | PW | No Violations | |
0444005077 | 2017-03-02 | Production Wells | No Violations | At the time of this inspection, the well was equipped with a plunger lift assembly and the valves on the wellhead were open. Reported production for this well was current. The tank battery consisted of one 100 BBL production tank and heater treater separator. Correct spacing between the 100 BBL and separator were correct. The valves on the separator were closed and the chart showed no production. The tank valve was equipped with a flat plug. The tank battery dike needed to be rebuilt along the west side. The signage was not legible and needed to be replaced. The lease access was stable. I contacted Larry Lower of Enervest about rebuilding the dike and installing new signage. |
For data sources see[9]