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Well ID: 34-055-20286 | Loading map...
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Country: United States | |
State: Ohio | |
County: Trumbull | |
Municipality: Farmington Township | |
Operator Name: BOCOR HOLDINGS, LLC | |
Well Pad ID: | |
Farm/Lease Name: HOPKINS | |
License Status: Final Restoration | |
License Date: 2016-08-03 | |
Spud Date: 1979-07-15 | |
Spud Drilling Contractor: | |
Final Drill Date: 1979-07-24 | |
Well Total Depth: 4170.00 ft | |
Configuration: Vertical | |
Latitude: 41.370000 | |
Longitude: -81.000000 |
For data sources see[1]
Well Status | Well Status Date | Comment |
---|---|---|
CO | 1979-05-03 | 182 BELDEN & BLAKE CO GeoDate 5/3/79 |
Original Spud | 1979-07-15 | R.I. 5-10-79 |
Completed | 1979-07-24 | R.I. 5-10-79 |
Reached Total Depth | 1979-07-24 | R.I. 5-10-79 |
Change of Owner | 2002-08-06 | Operator changed from 182, BELDEN & BLAKE CORPORATION to 1966, PETROX INC |
Change of Owner | 2002-12-12 | Operator changed from 1966, PETROX INC to 7033, BROAD STREET ENERGY COMPANY |
APP | 2004-01-14 | Proposed Formations:CLINTON, Issued Date:1/14/2004, Expired Date:1/13/2005 6:00:00 AM, Drilling unit acres:52, Proposed Well Type:OG, Proposed Well Class: |
Change of Owner | 2005-03-01 | Operator changed from 7033, BROAD STREET ENERGY COMPANY to 935, BOCOR HOLDINGS, LLC/BOCOR PROD |
APP | 2016-08-03 | Proposed Formations:CLINTON, Issued Date:8/3/2016, Expired Date:8/3/2018 12:00:00 PM, Drilling unit acres:0, Proposed Well Type:OG, Proposed Well Class: |
Plugged/Abandoned | 2016-08-10 | R.I. 5-10-79 |
Record Last Modified | 2017-02-15 | R.I. 5-10-79 |
Construction Permit Expires | 2018-08-03 | R.I. 5-10-79 |
For data sources see[2]
Perforation Date | Interval Top (ft) | Interval Base (ft) | Number of Shots |
---|---|---|---|
2006-09-11 | 3891 | 3981 | 16 |
3891 | 3981 | 16 | |
3891 | 3981 | 16 |
For data sources see[3]
Stimulation Date | Chemical Agent | Chemical Agent Concentration (%) | Fracking Fluid Volume | Mass of Proppant Used (lb) | Fracking Company | Comments |
---|---|---|---|---|---|---|
H2O | 0 | 1146 Bbl | 90000 | |||
N2 | 0 | 147 Mscf | 0 |
For data sources see[4]
Period | Operator Name | Gas Quantity (mcf) | Oil Quantity (bbl) | Production Days |
---|---|---|---|---|
1984 | POWER GAS MARKETING & TRANS | 1155.00 | 346.00 | 0 |
1986 | BELDEN & BLAKE CORPORATION | 455.00 | 323.00 | 365 |
1987 | BELDEN & BLAKE CORPORATION | 544.00 | 181.00 | 365 |
1988 | BELDEN & BLAKE CORPORATION | 182.00 | 229.00 | 123 |
1992 | BELDEN & BLAKE CORPORATION | 0.00 | 60.00 | 15 |
1993 | BELDEN & BLAKE CORPORATION | 383.00 | 303.00 | 111 |
1994 | BELDEN & BLAKE CORPORATION | 500.00 | 223.00 | 213 |
1995 | BELDEN & BLAKE CORPORATION | 690.00 | 405.00 | 357 |
1996 | BELDEN & BLAKE CORPORATION | 498.00 | 420.00 | 305 |
1997 | BELDEN & BLAKE CORPORATION | 849.00 | 328.00 | 274 |
1998 | BELDEN & BLAKE CORPORATION | 845.00 | 290.00 | 271 |
1999 | BELDEN & BLAKE CORPORATION | 555.00 | 343.00 | 208 |
2000 | BELDEN & BLAKE CORPORATION | 73.00 | 192.00 | 324 |
2001 | BELDEN & BLAKE CORPORATION | 0.00 | 204.00 | 290 |
2002 | BROAD STREET ENERGY COMPANY | 0.00 | 0.00 | 28 |
2003 | BROAD STREET ENERGY COMPANY | 0.00 | 0.00 | 0 |
2004 | BROAD STREET ENERGY COMPANY | 0.00 | 0.00 | 0 |
2005 | BROAD STREET ENERGY COMPANY | 0.00 | 0.00 | 48 |
2006 | BOCOR HOLDINGS, LLC | 465.00 | 82.00 | 365 |
2007 | BOCOR HOLDINGS, LLC | 1252.00 | 435.00 | 365 |
2008 | BOCOR HOLDINGS, LLC | 777.00 | 274.00 | 365 |
2009 | BOCOR HOLDINGS, LLC | 753.00 | 304.00 | 365 |
2010 | BOCOR HOLDINGS, LLC | 252.00 | 248.00 | 365 |
2011 | BOCOR HOLDINGS, LLC | 283.00 | 269.00 | 365 |
2012 | BOCOR HOLDINGS, LLC | 226.00 | 89.00 | 366 |
2013 | BOCOR HOLDINGS, LLC | 0.00 | 59.00 | 365 |
2014 | BOCOR HOLDINGS, LLC | 0.00 | 0.00 | 0 |
2016 | BOCOR HOLDINGS, LLC | 0.00 | 0.00 | 0 |
Inspection ID | Inspection Date | Inspection Type | Inspection Result | Inspection Comments |
---|---|---|---|---|
-1064277194 | 2016-9-8 0:00:0 | FR | No Violations | |
-353443638 | 2014-5-2 0:00:0 | PW | No Violations | |
0353443638 | 2014-05-02 | Production Wells | No Violations | My inspection found the motor for the pump jack has been removed from the well. I had the company plumb the annulus up to a guage in may. The guage on the annulus was not working and a new guage read the annulus had 20 psi on it. The casing did not have any pressure on it. The company still intends on using the well as a swab well. The tank battery consists of a 210 BBL production tank, a 25 BBL brine tank, and two mechanical separators. The proper identification is located on the tank battery. The tank battery and lease road are being shared by permit number 2-0769. |
1064277194 | 2016-09-08 | Final Restoration | No Violations | I conducted a final restoration inspection of this well. The wellsite has been restored and is stable with no erosion issues. The production equipment is remaining on site because it is shared with well 34-155-2-0769. The lease access is remaining per landowner waiver. Final restoration can be passed. |
1369059103 | 2013-05-20 | Production Wells | No Violations | My inspection found the annulus had been plumbed up into a guage as requested. The guage on the tubing, the casing, and the annulus read 0 psi. I placed a call to Jim Paumier of Bocor and he informed me the well has a hole in the tubing and a service rig was scheduled to come out and fix the issue. I also asked him to reclaim a section of the field that the flow line had been replaced and to clean up the scrap pipe around the pump jack. He stated he would have the issues taken care of. |
1421853414 | 2015-01-21 | Production Wells | No Violations | My inspection found no changes since my last inspection. The guages on the 8 5/8 casing, 4.5 casing and the tubing all read zero psi. The valves on the well are closed. The production tank and the brine tank are empty. The vales on both separators are closed. The production chart has not been changed since the last one was put on in March of 2013. The landowner states the well has not produced since 2012. The company has reported production for 2013. The company attempted to apply for temporary inactive status but was denied by Permitting due to the well needs to have not produced for two years. I will continue to monitor the wells status and the company will contact me before performing any operations at the location. |
1460547160 | 2016-04-12 | Production Wells | Violations Noted | My inspection found the well to be equipped with a pumpjack. The motor has been removed from the pumpjack. The valves on the wellhead are in the closed position. The tank battery consists of a 210 BBL production tank, a 35 BBL brine tank, and two mechanical separators. The proper identification is located on the tank battery. The lease road is in stable condition. The last year of reported production for the well is 2013. I have contacted Kevin Hutchinson of Bocor Holdings about the well. The well owner/operator shall submit a written plugging schedule to Inspector Perry at 3575 Forest Lake Dr. Suite 150 Uniontown, OH 44685 within 30 days, per OAC 1501:9-11-05(B), and plug the well within 180 days. The well owner/operator will be notified if the plugging schedule is approved or denied. |
1855770136 | 2013-04-04 | Production Wells | No Violations | My inspection found the well to be equipped with a pump jack. The well and tank battery are in good repair. The tank battery consists of a 210 BBL production tank, a 35 BBL brine tank, and two mechanical separator. The proper identification was located on the tank battery and pump jack. The lease road is in stable condition. |
1996706797 | 2013-09-16 | Production Wells | No Violations | I was on location today at the request of the landowner. He stated the pump jack had been removed and that the guage on the annulus was not functioning. The well is still equipped with a pump jack. I had the company plumb the annulus up to a guage in may. The guage on the annulus was not working and a new guage read the annulus had 20 psi on it. The casing did not have any pressure on it. The company has informed me that they will be converting the well into a swab well. The tank battery consists of a 210 BBL production tank, a 25 BBL brine tank, and two mechanical separators. The proper identification is located on the tank battery. The tank battery and lease road are being shared by permit number 2-0769. |
Inspection ID | Violation ID | Violation Date | Violation Code | Violation Comments |
---|---|---|---|---|
1460547160 | US-OH-113332 | 2016-06-17 | Well shall be plugged |
For data sources see[9]